Event Notification Report for February 1, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/29/1999 - 02/01/1999 ** EVENT NUMBERS ** 35323 35324 35325 35326 35327 35328 35329 35330 35331 35332 35333 35334 35335 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35323 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MD RADIOLOGICAL HEALTH DEPT |NOTIFICATION DATE: 01/29/1999| |LICENSEE: SYNCOR INTERNATIONAL CORP |NOTIFICATION TIME: 09:35[EST]| | CITY: TIMONIUM REGION: 1 |EVENT DATE: 01/27/1999| | COUNTY: STATE: MD |EVENT TIME: 12:00[EST]| |LICENSE#: MD-05-058-01 AGREEMENT: Y |LAST UPDATE DATE: 01/29/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID SILK R1 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: DONNA GAINES | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Moly Generator shipping box apparently contaminated at Syncor - | | | | On 01/28/99, a Moly Generator shipped by FedEx from Dupont received at | | Syncor International Corporation in Timonium, MD, was found to have external | | contamination but no internal contamination. The wipes from outside of the | | generator shipping box read 224,590 cpm (244,385 dpm). The generator was | | taken out of the shipping box and used since there was no internal | | contamination. The shipping box was isolated and rewiped later in the | | afternoon, and no contamination was detected. | | | | The shipping box was labeled RADIII Mo-99 287.59 GBq with a TI of 4.1. | | | | The FedEx driver and his delivery truck were surveyed and no contamination | | above background was found. | | | | Based on the above events, it appears that the shipping box was contaminated | | once in the restricted area at Syncor. The person conducting the survey | | could have touched something contaminated and subsequently contaminated the | | shipping box. | | | | Syncor's package receipt procedures were reviewed by a MD inspector with | | emphasis on their protocol for contaminated packages. | | | | Syncor is conducting an investigation and plans to submit a written report | | of this incident and follow-up action taken to MD within 30 days. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35324 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 01/29/1999| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 09:48[EST]| | RXTYPE: [3] CE |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 07:57[CST]| | NRC NOTIFIED BY: VICTOR COLLINS |LAST UPDATE DATE: 01/29/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 94 Power Operation |94 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT - | | | | UNACCOUNTED FOR PERSONNEL DOOR LOCK PULLER. COMPENSATORY MEASURES | | IMMEDIATELY TAKEN UPON DISCOVERY. THE LICENSEE NOTIFIED THE NRC RESIDENT | | INSPECTOR. REFER TO THE HOO LOG FOR ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35325 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: DETROIT MACOMB HOSPITAL |NOTIFICATION DATE: 01/29/1999| |LICENSEE: DETROIT MACOMB HOSPITAL |NOTIFICATION TIME: 11:28[EST]| | CITY: DETROIT REGION: 3 |EVENT DATE: 01/28/1999| | COUNTY: STATE: MI |EVENT TIME: 16:10[EST]| |LICENSE#: 21-01190-05 AGREEMENT: N |LAST UPDATE DATE: 01/29/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |TONY VEGEL R3 | | |DONALD COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ARTHUR EWALD | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION DUE TO PATIENT INTERVENTION | | | | During brachytherapy treatment of a patient's endobronchial area, the | | patient dislodged the catheter approximately 25 cm, causing the treatment | | site to receive only 3.8% of the prescribed dose. Additionally, the | | patient's nasal area received approximately 13 rads (13 cGy) due to the | | displacement. The licensee estimates that the catheter was dislodged for | | approximately 10 minutes before being discovered. | | | | The patient's referring physician has been informed of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35326 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SAINT MARY'S HOSPITAL |NOTIFICATION DATE: 01/29/1999| |LICENSEE: SAINT MARY'S HOSPITAL |NOTIFICATION TIME: 11:49[EST]| | CITY: RICHMOND REGION: 2 |EVENT DATE: 01/08/1998| | COUNTY: STATE: VA |EVENT TIME: 11:50[EST]| |LICENSE#: 451136702 AGREEMENT: N |LAST UPDATE DATE: 01/29/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRIAN BONSER R2 | | |DON COOL NMSS EO | +------------------------------------------------+ | | NRC NOTIFIED BY: ANTHONY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | SAINT MARY'S HOSPITAL IN RICHMOND, VIRGINIA DISCOVERED, ON 1/28/99 @ 1150 | | DURING AN ANNUAL REVIEW OF THEIR QUALITY MANAGEMENT PROGRAM, THEY HAD | | ADMINISTERED THE WRONG DOSAGE DURING TREATMENT OF A PATIENT WITH GRAVES | | DISEASE. THE PRESCRIBED DOSAGE WAS 8 MILLICURIES OF I-131, BUT THE | | ADMINISTERED DOSAGE WAS 9.8 MILLICURIES OF | | I-131. THE PATIENT'S PHYSICIAN WAS NOTIFIED, BUT SHE DID NOT THINK IT WAS | | NECESSARY TO NOTIFY THE PATIENT. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35327 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 01/29/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 13:57[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 12:03[EST]| | NRC NOTIFIED BY: FIELDER |LAST UPDATE DATE: 01/29/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID SILK R1 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT ENTERED A 14 DAY LCO DUE TO HPCI BEING DECLARED INOPERABLE. | | | | THE HPCI SYSTEM WAS ISOLATED AND DECLARED INOPERABLE DUE TO A SUSPECTED | | PROBLEM WITH STEAMLINE FLOW SWITCH TRIP SETPOINT. IT WAS DETERMINED THERE | | WAS A POSSIBILITY THAT THE SETSCREW INTERNAL TO THE BARTON DIFFERENTIAL | | PRESSURE SWITCH HAD NOT BEEN TIGHTEN AFTER PERFORMANCE OF THE LAST | | CALIBRATION. THIS CONDITION COULD CAUSE EXCESSIVE DRIFT. | | | | A SECOND CONCERN IS THE SWITCH'S RESPONSE DURING A SEISMIC EVENT MAY BE | | AFFECTED WITH A LOOSE SCREW. HPCI WAS ISOLATED TO MAINTAIN PRIMARY | | CONTAINMENT INTEGRITY AND A MAINTENANCE REQUEST HAS BEEN SUBMITTED. THIS | | CONCERN MAY ALSO BE APPLICABLE TO OTHER SAFETY RELATED SYSTEMS AND THEY WILL | | BE CHECKED TO ENSURE THE SETSCREW IS APPROPRIATELY TIGHTENED. RCIC IS | | OPERABLE. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35328 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 01/29/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 15:31[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 13:59[CST]| | NRC NOTIFIED BY: LANDIN |LAST UPDATE DATE: 01/29/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TONY VEGEL R3 | |10 CFR SECTION: | | |AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT DECLARED DIVISION 1 AND 2 SERVICE WATER INOPERABLE. | | | | THE DIV 1 AND DIV 2 SERVICE WATER PUMPS(SX) BEARINGS WERE DETERMINED TO BE | | DEGRADED AND THIS CONDITION REPRESENTED A REASONABLE DOUBT THAT THE SX PUMPS | | WOULD BE UNABLE TO PERFORM THEIR DESIGN FUNCTION FOR AN EXTENDED 30 DAY TIME | | PERIOD. THESE PUMPS ARE REQUIRED TO SUPPORT ACCIDENT MITIGATION, SAFE | | SHUTDOWN AND RESIDUAL HEAT REMOVAL. THIS CONDITION PUT THE PLANT IN A LCO | | FOR THE SUPPORTED SYSTEMS TO SUSPEND ALL FUEL MOVEMENT AND OPERATIONS WHICH | | HAVE THE POTENTIAL FOR DRAINING THE VESSEL. | | | | THIS CONDITION WAS DISCOVERED 1/9/99 AND CORRECTIVE ACTIONS WERE INITIATED | | THE SAME DAY ON BOTH DIVISIONS AND COMPLETED WITHIN THE LAST SEVERAL DAYS. | | DIV 1 IS REPAIRED AND DECLARED OPERABLE AND DIV 2 IS REPAIRED AND WILL BE | | DECLARED OPERABLE UPON COMPLETION OF POST-REPAIR DOCUMENTATION REVIEW. | | | | THE LICENSEE DID NOT DETERMINE THIS EVENT REPORTABLE UNTIL 1/29/99 @ 1359. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35329 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SWAGELOK COMPANY |NOTIFICATION DATE: 01/29/1999| |LICENSEE: SWAGELOK COMPANY |NOTIFICATION TIME: 16:04[EST]| | CITY: SOLON REGION: 3 |EVENT DATE: 01/28/1999| | COUNTY: STATE: OH |EVENT TIME: [EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 01/29/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID SILK R1 | | |BRIAN BONSER R2 | +------------------------------------------------+VERN HODGE NRR | | NRC NOTIFIED BY: BRUCE FLUSCHE (FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE SWAGELOK COMPANY IS SUBMITTING A POSSIBLE 10CFR PART 21 NOTIFICATION | | BECAUSE OF A POSSIBLE MATERIAL DEFECT IN A SWAGELOK PIPE FITTING TEE, PART # | | SS-6-T. THE DEFECT IS A CRACK IN THE CENTER OF THE FORGING. THEY ARE | | CONTINUING THEIR ANALYSIS OF THE PART. | | THIS PART WAS SUPPLIED TO PUBLIC SERVICE ELECTRIC & GAS(20 PCS.) IN HANCOCKS | | BRIDGE N.J. AND SOUTH CAROLINA ELECTRIC & GAS CO., VC SUMMER STATION(3 PCS.) | | THE PRODUCT ID IS R27GE0123B. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35330 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 01/29/1999| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 17:03[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 13:45[CST]| | NRC NOTIFIED BY: BAKER |LAST UPDATE DATE: 01/29/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TONY VEGEL R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ALCOHOL FOUND IN THE VITAL AREA (AUXILIARY BUILDING). | | | | THE LICENSEE FOUND A 200ML JACK DANIELS BOTTLE, CONTAINING APPROXIMATELY ONE | | TEASPOON OF LIQUID, IN A VITAL AREA COMMON TO BOTH UNITS. THE BOTTLE WAS | | FOUND INSIDE OF A TUBE STEEL STRUCTURAL SUPPORT DURING A ROUTINE RADIATION | | PROTECTION HOUSE CLEANING AND WALKDOWN. THEY TOOK POSSESSION OF THE BOTTLE | | AND CONTINUED THE INSPECTION. A SECURITY INVESTIGATION WILL FOLLOW. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35331 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ALABAMA RADIATION CONTROL |NOTIFICATION DATE: 01/29/1999| |LICENSEE: TUSCALOOSA STEEL |NOTIFICATION TIME: 17:11[EST]| | CITY: TUSCALOOSA REGION: 2 |EVENT DATE: 01/29/1999| | COUNTY: STATE: AL |EVENT TIME: 15:10[CST]| |LICENSE#: 1190 AGREEMENT: Y |LAST UPDATE DATE: 01/29/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRIAN BONSER R2 | | |DAVID SILK R1 | +------------------------------------------------+LARRY CAMPER NMSS | | NRC NOTIFIED BY: DAVID WALTER |STUART RUBIN IRD | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE ALABAMA RADIATION CONTROL OFFICE WAS NOTIFIED BY TUSCALOOSA STEEL OF AN | | UNAUTHORIZED TRANSFER OF RADIOACTIVE MATERIAL. | | | | TUSCALOOSA STEEL REPORTED THAT A TRANSFER OF A DEVICE (RONAN MODEL SA-15, | | S/N GG390), CONTAINING A 100 MILLICURIE CESIUM-137 SOURCE, TO THE GLADWIN | | COMPANY IN PITTSBURGH, PA FOR REPAIR HAD OCCURRED. THE MOLD CASTER, WHICH | | IS THE SOURCE HOLDER, WAS SENT FOR REPAIR INADVERTENTLY WITH THE SOURCE | | STILL INSIDE. IT IS NOT BELIEVED, HOWEVER, THAT THE SOURCE HOLDER'S SHUTTER | | WAS OPEN, SINCE NO RADIATION MONITORS WENT OFF WHEN THE MOLD CASTER WAS | | LEAVING THE PLANT. TUSCALOOSA STEEL CONTACTED THE GLADWIN COMPANY TO HAVE | | THEM MOVE THE MOLD CASTER TO A REMOTE AREA OF THEIR PLANT AND WAIT FOR RONAN | | ENGINEERS TO ARRIVE SO THEY CAN REMOVE THE SOURCE AND RETURN IT TO | | TUSCALOOSA STEEL. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35332 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: OKLAHOMA DEPT OF ENVIR. PROTECTION. |NOTIFICATION DATE: 01/29/1999| |LICENSEE: N/A |NOTIFICATION TIME: 18:17[EST]| | CITY: OKLAHOMA CITY REGION: 4 |EVENT DATE: 01/29/1999| | COUNTY: STATE: OK |EVENT TIME: 15:30[CST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 01/29/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES MARSCHALL R4 | | |LARRY CAMPER NMSS | +------------------------------------------------+STUART RUBIN IRD | | NRC NOTIFIED BY: BRODERICK | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE OKLAHOMA CITY FIRE DEPARTMENT NOTIFIED THE OKLAHOMA DEPARTMENT OF | | ENVIRONMENTAL PROTECTION THAT AN INDIVIDUAL HAD A 10 LB. DEPLETED URANIUM | | SOURCE (POSSIBLY AN AIRCRAFT COUNTER WEIGHT) MEASURING 1.8 MILLIREM/HR AT | | HIS HOUSE. THE INDIVIDUAL PURCHASED THE SOURCE AT A SURPLUS STORE. THE | | INDIVIDUAL WAS INFORMED TO KEEP THE SOURCE ISOLATED UNTIL IT IS REMOVED FROM | | HIS HOUSE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35333 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 01/29/1999| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 18:20[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 14:50[CST]| | NRC NOTIFIED BY: GREEN |LAST UPDATE DATE: 01/29/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE YANDELL R4 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT DECLARED RCIC INOPERABLE DUE TO LOW TURBINE OIL LEVEL. | | | | THE RCIC OUTBOARD TURBINE BEARING OIL LEVEL WAS SLIGHTLY BELOW THE LOW LEVEL | | MARK AND THE RCIC SYSTEM WAS THEREFORE DECLARED INOPERABLE AT 1450. HPCI | | HAS BEEN VERIFIED TO BE OPERABLE. THIS CONDITION CAUSED ENTRY INTO A 14 DAY | | LCO DUE TO RCIC BEING INOPERABLE. AN INSPECTION OF THE OIL SYSTEM DID NOT | | INDICATE ANY LEAKAGE AND OIL LEVEL HAD ONLY LOWERED SLIGHTLY FROM THE | | PREVIOUS DAY. MAINTENANCE PERSONNEL HAVE BEEN CALLED IN TO ADD OIL TO THE | | BEARING. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | *** UPDATE ON 1/29/99 @ 2135 BY WHEELER TO GOULD *** | | | | RCIC RETURNED TO OPERABLE CONDITION AT 1848 WHEN THE OIL LEVEL ON THE | | OUTBOARD TURBINE BEARING WAS RESTORED TO ITS PROPER LEVEL. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | THE REG 4 RDO (YANDELL) WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35334 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 01/29/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 18:55[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 18:00[EST]| | NRC NOTIFIED BY: COTTER |LAST UPDATE DATE: 01/29/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID SILK R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AN ERRONEOUS ASSUMPTION WAS MADE IN THE FIRE PROTECTION SAFE SHUTDOWN | | REPORT. | | | | A REVIEW ASSOCIATED WITH AN ENGINEERING FIRE PROTECTION SELF-ASSESSMENT HAS | | IDENTIFIED AN ERRONEOUS ASSUMPTION REGARDING AN OPERATOR ACTION CREDITED IN | | THE FIRE PROTECTION SAFE SHUTDOWN REPORT. POTENTIAL FIRE-INDUCED SPURIOUS | | OPERATION OF THE REACTOR COOLANT SYSTEM (RCS) LOOP DRAIN VALVES 2RCS-MOV557A | | , B, OR C, IN CONJUNCTION WITH SPURIOUS OPERATION OF THE DOWNSTREAM VALVES, | | RCS EXCESS LETDOWN VALVES 2CHS-HCV137 AND 2CHS-MOV201 WAS NOT ADEQUATELY | | CONSIDERED. THE UNIT 2 FIRE PROTECTION SAFE SHUTDOWN REPORT STATES THAT IN | | THE EVENT OF A FIRE-INDUCED SPURIOUS OPERATION OF 2RCS-MOV557A, B, OR C, THE | | OPERATOR COULD MANUALLY CLOSE EITHER 2CHS-MOV201 OR 2CHS-HCV137 TO ISOLATE | | THE RESULTING EXCESS LETDOWN FLOW. OPERATION OF THESE VALVES FROM THE | | CONTROL ROOM DOES NOT SATISFY THE REQUIREMENT SINCE THE FIRE MAY HAVE | | DAMAGED THE CONTROL AND/OR POWER CIRCUITS. LOCAL MANUAL OPERATION OF THESE | | VALVES WOULD NOT BE FEASIBLE WITHIN THE REQUIREMENTS OF THE SAFE SHUTDOWN | | ANALYSIS BECAUSE OF INACCESSIBILITY IN CONTAINMENT. | | | | AT 1806 POWER WAS REMOVED FROM THE RCS LOOP DRAIN VALVES TO ISOLATE THIS | | POTENTIAL FLOW PATH AND THUS RESTORE COMPLIANCE WITH THEIR POST-FIRE SAFE | | SHUTDOWN ANALYSIS. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35335 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 01/29/1999| | UNIT: [2] [] [] STATE: PA |NOTIFICATION TIME: 19:12[EST]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 18:30[EST]| | NRC NOTIFIED BY: PAUTLER |LAST UPDATE DATE: 01/29/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID SILK R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONDITION THAT WOULD RESULT IN A NON-CONSERVATIVE INPUT TO THE ROD BLOCK | | MONITORING SYSTEM. | | | | DURING A UNIT 2 MINOR MAINTENANCE INVESTIGATION ON A LOCAL POWER RANGE | | MONITOR (LPRM) BYPASS LIGHT, TROUBLESHOOTING PERSONNEL FOUND A WIRING | | CONCERN INVOLVING LPRM INPUTS TO THE UNIT 2 ROD BLOCK MONITORING (RBM) | | SYSTEM. TWO LPRM LOCATIONS WERE FOUND SWAPPED WITHIN THE RBM SYSTEM. THIS | | CONDITION WOULD CAUSE A NON-CONSERVATIVE INPUT TO THE RBM SYSTEM DURING | | CONTROL ROD MOVEMENT, THEREFORE ALLOWING UNIT 2 TO POTENTIALLY OPERATE | | OUTSIDE ITS DESIGN BASIS. PER PROCEDURE, BOTH LPRMS WERE BYPASSED TO RETURN | | BOTH CHANNELS BACK TO OPERABLE STATUS. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021