Event Notification Report for January 6, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/05/1999 - 01/06/1999 ** EVENT NUMBERS ** 35155 35214 35215 35216 35217 35218 35219 35220 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35155 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/16/1998| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 11:07[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/16/1998| +------------------------------------------------+EVENT TIME: 07:24[EST]| | NRC NOTIFIED BY: BOB KIDDER |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN JACOBSON R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - DIVISION 3 NORMAL BATTERY CHARGER FAILED AND WAS REPLACED BY THE RESERVE | | CHARGER - | | | | AT 0724 ON 12/16/98, THE CONTROL ROOM RECEIVED ANNUNCIATOR ALARMS INDICATING | | TROUBLE ON THE DIVISION 3 DIESEL GENERATOR (DG) AND DIVISION 3 BATTERY. BUS | | AND BATTERY VOLTAGE HAD DECREASED FROM 129 VDC TO APPROXIMATELY 122 VDC, AND | | THE BATTERY WAS DISCHARGING APPROXIMATELY 5 AMPS. SUBSEQUENT INVESTIGATION | | DETERMINED THAT THE DIVISION 3 NORMAL BATTERY CHARGER HAD NO OUTPUT. | | | | AT 0746, PLANT OPERATORS PLACED THE DIVISION 3 DG AND THE HIGH PRESSURE CORE | | SPRAY (HPCS) SYSTEM IN SECURE STATUS TO PREVENT A POTENTIAL AUTOMATIC | | INITIATION DUE TO VOLTAGE PROBLEMS AND SHIFTED THE DIVISION 3 ON-LINE | | BATTERY CHARGER FROM THE NORMAL BATTERY CHARGER TO THE RESERVE BATTERY | | CHARGER. THE LICENSEE DECLARED THE DIVISION 3 DG AND THE HPCS SYSTEM | | INOPERABLE [14-DAY LIMITING CONDITION FOR OPERATION (LCO)] EVEN THOUGH THEY | | ARE FUNCTIONAL. | | | | AT 1010, THE LICENSEE VERIFIED THE RESERVE BATTERY CHARGER AND ALL DIVISION | | 3 SYSTEMS TO BE OPERABLE AND EXITED THE HPCS SYSTEM LCO. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR AND PLANS TO REPAIR/REPLACE | | THE FAILED BATTERY CHARGER. | | | | * * * UPDATE 1007 EST ON 01/05/99 FROM STERLING SANFORD TO S.SANDIN * * * | | | | THIS EVENT IS BEING RETRACTED BASED ON THE FOLLOWING: | | | | "AFTER FURTHER REVIEW, IT HAS BEEN DETERMINED THAT THIS EVENT IS NOT | | REPORTABLE AS A LOSS OF SAFETY FUNCTION. BATTERY VOLTAGE ON DIVISION 3 | | REMAINED AT APPROXIMATELY 122 VDC. ENGINEERING CALCULATIONS SHOW THIS | | VOLTAGE TO BE ABOVE THAT WHICH IS REQUIRED FOR HPCS TO PERFORM ITS SAFETY | | FUNCTION. | | | | "OPERATIONS CONSERVATIVELY SECURED DIVISION 3 TO ENSURE THAT NO [ENGINEERED | | SAFETY FEATURE] ACTUATIONS OCCURRED WHILE TRANSFERRING FROM THE NORMAL TO | | THE RESERVE BATTERY CHARGER. REASONABLE OPERATOR ACTIONS COULD HAVE BEEN | | TAKEN TO RESTORE HPCS, IF REQUIRED. THIS IS IN ACCORDANCE WITH NUREG-1022 | | GUIDANCE. | | | | "DURING THIS EVENT, [AUTOMATIC DEPRESSURIZATION SYSTEM], ALL LOW-PRESSURE | | [EMERGENCY CORE COOLING SYSTEMS], AND [REACTOR CORE ISOLATION COOLING] WERE | | OPERABLE." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. THE NRC OPERATIONS | | OFFICER NOTIFIED THE R3DO (CLAYTON). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35214 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 01/05/1999| | UNIT: [] [2] [] STATE: CA |NOTIFICATION TIME: 03:19[EST]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 01/04/1999| +------------------------------------------------+EVENT TIME: 20:51[PST]| | NRC NOTIFIED BY: HOWARD SMITH |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOSEPH TAPIA R4 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE DETERMINED THAT THE CCW SYSTEM MAY NOT MEET ITS REQUIREMENT TO | | OPERATE FOR 7 DAYS WITHOUT MAKE-UP FOLLOWING A SEISMIC EVENT. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | | | "AT SAN ONOFRE, THE COMPONENT COOLING WATER (CCW) SYSTEM IS REQUIRED TO | | PROVIDE COOLING FOR 7 DAYS WITHOUT MAKE-UP. CCW TRAINS 'A' AND 'B' ARE | | SEISMICALLY QUALIFIED; THE NON-CRITICAL LOOP IS NOT SEISMICALLY QUALIFIED." | | | | "UNIT 2 ENTERED MODE 5 AT APPROXIMATELY 0544 PST ON JANUARY 3, 1999, FOR A | | PLANNED REFUELING/MAINTENANCE OUTAGE. AT 2051 ON JANUARY 4, 1999, WHILE | | UNIT 2 WAS IN MODE 5, SCE DETERMINED THAT ISOLATION VALVE LEAKAGE BETWEEN | | CCW TRAIN 'B' AND THE CCW NON-CRITICAL LOOP OBSERVED DURING A [TECHNICAL | | SPECIFICATION] SURVEILLANCE EXCEEDED ITS ACCEPTABLE LIMIT FOR OPERATION IN | | MODES 1 THROUGH 4, AND TRAIN B CCW COULD HAVE BEEN INOPERABLE PRIOR TO SHUT | | DOWN. TESTS WERE PERFORMED TO ATTEMPT TO DETERMINE WHETHER THIS LEAKAGE | | EXISTED DURING OPERATION IN MODES 1 THROUGH 4 PRIOR TO PLANT SHUT DOWN. | | HOWEVER, THE TESTS WERE UNABLE TO DETERMINE THAT THE LEAKAGE DID NOT EXIST | | PRIOR TO SHUT DOWN. DURING THE PAST CYCLE OF PLANT OPERATION, IF A SEISMIC | | EVENT WERE TO HAVE OCCURRED WHILE TRAIN 'A' WAS OUT OF SERVICE, THERE WAS A | | POTENTIAL FOR THE CCW TO FAIL TO MEET ITS REQUIRED 7 DAYS OF OPERATION | | WITHOUT MAKEUP. THEREFORE, SCE IS CONSERVATIVELY MAKING THIS REPORT AS A | | NON-EMERGENCY 4-HOUR REPORT IN ACCORDANCE WITH 10CFR50.72(b)(2)(iii) - A | | CONDITION THAT ALONE COULD HAVE PREVENTED THE FULFILLMENT OF THE SAFETY | | FUNCTION OF THE CCW. | | | | "CCW IS PRESENTLY CAPABLE OF PERFORMING ITS SUPPORT FUNCTION FOR SHUTDOWN | | COOLING IN MODES 5 AND 6. THE ISOLATION VALVES' ACTUATORS WERE | | DISCONNECTED, THE VALVES WERE MANUALLY SEATED. THE MEASURED LEAKAGE WAS | | WELL BELOW THE ACCEPTABLE LEVEL FOR OPERATION IN MODES 1 THROUGH 4. THE | | ACTUATORS WERE RE-CONNECTED TO PROVIDE FOR REMOTE OPERATION. THE | | INVESTIGATION OF THE CAUSE AND CORRECTIVE ACTIONS IS ON-GOING. | | | | "UNIT 3 IS IN MODE 1 AND UNAFFECTED BY THIS CONDITION." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35215 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 01/05/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 15:12[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 01/05/1999| +------------------------------------------------+EVENT TIME: 13:40[CST]| | NRC NOTIFIED BY: TIM BORGEN |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |BRENT CLAYTON R3 | |10 CFR SECTION: |CHRIS GRIMES, NRR EO | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |JOSEPH GIITTER, AEOD IRD | |ARPS 50.72(b)(2)(ii) RPS ACTUATION |JOHN HANNON, NRR EO | |AESF 50.72(b)(2)(ii) ESF ACTUATION |WAYNE STORE FEMA | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT, AUTOMATIC REACTOR TRIP, AND PARTIAL LOSS OF OFFSITE POWER DUE | | TO AN EXPLOSION OF A STATION AUXILIARY TRANSFORMER | | | | At 1311 CST, a Unit 1 automatic reactor trip occurred due to an explosion of | | the '1M' station auxiliary transformer. The licensee's fire brigade | | responded to the subsequent fire and extinguished the fire within several | | minutes. The '1R' reserve transformer (which is located next to the '1M' | | transformer) was also lost possibly due to its proximity to the explosion. | | The loss of both the '1M' and 1R' transformers (which are located outside of | | the main turbine building) caused the loss of non-safeguards buses 11, 12, | | 13, and 14. This in turn caused the loss of all condensate and feedwater | | pumps, circulating water pumps, and reactor coolant pumps. Auxiliary | | feedwater automatically initiated as required. All Unit 1 safeguards buses | | remained energized from normal offsite power. All rods fully inserted upon | | receipt of the reactor trip. There were three first out indicators (low-low | | steam generator pressure on the 11 steam generator, steam generator low-low | | level on the 12 steam generator, and high flux rate trip), and the exact | | causes of the reactor trip and transformer explosion are currently under | | investigation. There were no emergency core cooling system actuations, and | | none were expected. All systems functioned as required, and there were no | | personnel injuries. | | | | Unit 1 is currently stable in Hot Shutdown. Normal charging and letdown, | | auxiliary spray and one pressurizer heater, and natural circulation are | | being used to maintain primary system inventory, pressure, and transport | | control. Auxiliary feedwater is supplying water to the steam generators, | | and secondary steam is being dumped to atmosphere. There is no indication | | of steam generator tube leakage. Efforts are currently underway to restore | | power to non-safeguards buses 13 and 14. | | | | Unit 2 was unaffected by this event. It is currently operating at 60% | | reactor power following performance of an outage, and power ascension is in | | progress. | | | | At 1340 CST, the licensee declared a Notification of Unusual Event due to | | conditions warranting increased awareness by the plant operations staff. | | This was later revised to be conditions hazardous to plant operations (near | | or onsite explosion). The licensee currently plans to terminate the Unusual | | Event when one reactor coolant pump has been returned to service. | | | | The licensee notified the NRC resident inspector as well as the applicable | | state and local agencies. The licensee may also issue a press release. | | | | ******************** UPDATE AT 1953 EST ON 01/05/99 FROM TIM BORGEN TO | | TROCINE ******************** | | | | The licensee terminated the Unusual Event at 1843 CST. Unit 1 is currently | | in a stable condition meeting all technical specification requirements. | | Power has been restored to the 11, 12, 13, and 14, non-safeguards buses via | | back feed from the '2R' transformer. The 12 reactor coolant pump was | | started at 1835 CST, and the licensee plans to start the 11 reactor coolant | | pump within a few minutes. The circulating pumps were restored to service | | several hours ago, and the licensee plans to restore condensate pumps | | shortly. | | | | The licensee notified the NRC resident inspector and plans to notify the | | applicable state and local agencies. The licensee may also issue a press | | release tomorrow. The NRC Operations Officer notified the R3DO (Clayton), | | NRR EO (Hannon), AEOD IRD (Giitter), and FEMA (Ken Ciboch). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35216 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 01/05/1999| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 15:12[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 01/05/1999| +------------------------------------------------+EVENT TIME: 13:40[CST]| | NRC NOTIFIED BY: RANDY HASTINGS |LAST UPDATE DATE: 01/06/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: |CHRIS GRIMES, EO NRR | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS |JOHN HANNON, EO NRR | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS |JOSEPH GIITTER IRD | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - UNIT 1 SHUTTING DOWN DUE TO INOPERABLE SI SYSTEM DUE TO FROZEN | | RECIRCULATION LINE - | | | | UNIT 1 IS AT 100% POWER, AND UNIT 2 IS DEFUELED IN A REFUELING OUTAGE. | | | | A PORTION OF THE UNIT 1 SAFETY INJECTION PUMPS' RECIRCULATION LINE TO THE | | UNIT 1 REFUELING WATER STORAGE TANK APPEARS TO BE FROZEN DUE TO A LOSS OF | | HEAT TRACING DURING EXTREMELY COLD WEATHER. THIS CONDITION RENDERS BOTH | | TRAINS OF THE UNIT 1 SAFETY INJECTION SYSTEM INOPERABLE. THE UNIT 1 | | CONTAINMENT SPRAY PUMPS USE THE SAME RECIRCULATION LINE AND ARE ALSO | | RENDERED INOPERABLE. THE CONDITIONS OF TECHNICAL SPECIFICATION 15.3.0.B | | APPLY, AND THIS CONDITION APPEARS TO BE REPORTABLE AS A CONDITION THAT IS | | OUTSIDE THE PLANT DESIGN BASIS. | | | | THE ACTION STATEMENT FOR TECHNICAL SPECIFICATION 15.3.0.B REQUIRES THE | | LICENSEE TO INITIATE ACTION WITHIN 1 HOUR TO PLACE UNIT 1 IN HOT SHUTDOWN | | WITHIN 7 HOURS OF ENTERING THIS SPECIFICATION AND IN COLD SHUTDOWN WITHIN 37 | | HOURS. | | | | THE LICENSEE IS CURRENTLY ATTEMPTING TO THAW THE LINE. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | ****************** UPDATE AT 1615 EST ON 01/05/98 FROM RANDY HASTINGS TO | | TROCINE ****************** | | | | The licensee initiated the technical specification required load reduction | | at 1506 CST on 01/05/99. | | | | The licensee informed the NRC resident inspector. The NRC operations | | officer notified the R3DO (Clayton), NRR EOs (Grimes and Hannon),and AEOD | | IRD (Giitter). | | | | ****************** UPDATE AT 2132 EST ON 01/05/99 FROM JOHN CELL TO TROCINE | | ****************** | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Enforcement discretion was requested [at approximately 1625 CST] and | | granted [at approximately 1820 CST] by the NRC regarding the [Unit 1] | | shutdown required by the frozen [recirculation] line. Unit 1 is presently | | at 23% reactor power. Plans are to raise reactor power to 30% and hold. | | | | "Actions underway include [a] 50.59 evaluation of an alternate recirculation | | path that will restore the operability of one [safety injection] pump. An | | operability determination is being written to evaluate the operability of | | the [containment spray pumps] without the recirculation line. These actions | | are expected to be completed before the expiration of the enforcement | | discretion at 0140 CST [on 01/06/99]." | | | | The licensee plans to notify the NRC resident inspector. The NRC Operations | | Officer notified the R3DO (Clayton), NRR EO (Hannon), and AEOD IRD | | (Giitter). | | | | * * * UPDATE 0152 EST 1/6/98 FROM JOHN SELL TAKEN BY STRANSKY * * * | | | | "The original frozen line has been thawed and is being maintained warm by | | fluid circulation. An alternate SI pump recirculation path is currently | | being utilized which restores the Unit 1 'B' SI pump to operable. The use of | | this path is supported by a 50.59 evaluation and an operability | | determination. The same operability determination restores both Unit 1 CSPs | | to operable status with minor compensatory measures. | | | | "Unit 1 is being returned to 100% reactor power. The unit is in a 72-hour | | LCO until the normal SI recirculation path is restored, which will allow the | | 'A' SI pump to be declared operable. This is anticipated later today after | | restoration procedures are approved and the SI recirc line heat tracing is | | restored." | | | | The NRC resident inspector will be informed of this update by the licensee. | | Notified R3DO (Clayton), EO (Hannon). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35217 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 01/05/1999| | UNIT: [1] [] [] STATE: MD |NOTIFICATION TIME: 15:17[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 01/05/1999| +------------------------------------------------+EVENT TIME: 15:12[EST]| | NRC NOTIFIED BY: TOM O'MEARA |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM COOK R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING A SMALL STEAM LEAK ON A MOISTURE SEPARATOR | | REHEATER DRAIN TANK | | | | The licensee plans to notify the State Department of Labor Licensing and | | Regulation of a small steam leak on the 11 moisture separator reheater drain | | tank, which is an ASME Section VIII pressure vessel. There is no indication | | of steam generator tube leakage, there is no effect on plant operations, and | | there were no personnel injuries. The area has been cordoned off as a | | precaution, but the licensee does not expect the tank to catastrophically | | fail. There are two welds for the 1-inch pad on top of the tank that are | | still holding, and the licensee stated that the steam leak appears to be | | coming from an inside weld through a tell tail on the 1-inch pad. The | | outside welds appear to be intact. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35218 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 01/05/1999| | UNIT: [1] [2] [] STATE: VA |NOTIFICATION TIME: 15:18[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/05/1999| +------------------------------------------------+EVENT TIME: 13:56[EST]| | NRC NOTIFIED BY: JEFF MOSHER |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LEN WERT R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING INOPERABILITY OF THE SPILLWAY EMERGENCY | | DIESEL GENERATOR | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 1356 hours on 01/05/99, the Federal Emergency Regulatory Commission | | (FERC) was notified of the inoperability of the North Anna spillway | | emergency diesel generator in accordance with the requirements of | | 18CFR12.10(a). The diesel generator failed its operability test due to the | | engine water temperature being below the acceptable range of 165 - 195�F. | | Water temperature during the test was 155�F. A work request has been | | initiated to identify and correct the cause of this problem in a timely | | manner. The diesel generator remains available." | | | | The licensee stated that the spillway emergency diesel generator is not | | safety related and that the units are not in any limiting conditions for | | operation as a result of this issue. | | | | In addition to the FERC, the licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35219 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 01/05/1999| | UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 16:15[EST]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 01/05/1999| +------------------------------------------------+EVENT TIME: 16:13[EST]| | NRC NOTIFIED BY: BOB SMITH |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM COOK R1 | |10 CFR SECTION: |SUSAN SHANKMAN, EO NMSS | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION |FEMA, DOE, USDA, HHS FAX | | |EPA, DOT/NAT RES CTR FAX | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Connecticut notified that 840 gallons of waste water containing trace | | amounts of tritium leaked into Niantic Bay - | | | | At 0200 on 01/04/99, a leak in a heater loop for the Unit 3 'A' waste test | | tank (WTT) was discovered. Waste water in the WTT contained radioactivity | | and boric acid. The leak (approximately 1 - 2 gallons per minute) was | | isolated. Initial indications were that this waste water was contained | | within the yard drain system. Upon subsequent investigations, it was | | determined that, conservatively estimated, 840 gallons of liquid (4% of tank | | volume) leaked from the WTT. A berm surrounding the tank had been installed | | due to a prior leak but did not contain this leak. Sampling performed at | | discharge serial number DSN-006 taken after the event indicated the presence | | of tritium. | | | | Based on the above, it is believed that waste water from this leak flowed to | | a nearby yard drain and then discharged to Niantic Bay via DSN-006. The | | waste water from this leak contained radioactivity which is not addressed in | | the Millstone NPDES permit at DSN-006 nor are the WTTs listed as a source of | | waste water for DSN-006. Additionally, upon subsequent surveys of the storm | | drain system, tritium was detected at the DSN-006 sample point. As a | | result, this event was reported by the licensee to the Connecticut | | Department of Environmental Protection Spills Division and Permitting | | Division and local officials. | | | | The licensee plans to inform the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35220 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 01/05/1999| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 19:14[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/05/1999| +------------------------------------------------+EVENT TIME: 15:18[EST]| | NRC NOTIFIED BY: FREDERICK SMITH |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 95 Power Operation |95 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC START OF AN ANNULUS EXHAUST GAS TREATMENT SYSTEM FAN DURING TRAIN | | RESTORATION | | | | While returning annulus exhaust gas treatment system (AEGTS) train 'B' to | | standby readiness from secured status, the 'B' fan automatically started | | when the fan control switch was placed in the 'standby' position. The | | licensee believes that the initiating signal may not have been valid and | | that the cause may have been a faulty flow switch. Reportability is still | | under investigation. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
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