Event Notification Report for January 5, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/04/1999 - 01/05/1999 ** EVENT NUMBERS ** 35200 35212 35214 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35200 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 12/28/1998| | UNIT: [1] [2] [] STATE: VA |NOTIFICATION TIME: 11:16[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 12/28/1998| +------------------------------------------------+EVENT TIME: 11:00[EST]| | NRC NOTIFIED BY: JAMES HELM |LAST UPDATE DATE: 01/04/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PIERCE SKINNER R2 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY SIRENS INOPERABLE DUE TO WINTER WEATHER | | | | Virginia Power polled the 61 emergency sirens around Surry and found 17 that | | did not respond. Troubleshooting is in progress on the sirens in question. | | The cause of the failures is believed to be freezing rain which passed | | through the area on 12/24/98. The polling was completed at 1100 EST this | | morning. | | | | The licensee informed the NRC resident inspector and the State of Virginia | | Department of Emergency Services. | | | | ***UPDATE AT 1012 EST ON 01/04/99 FROM WEBSTER TAKEN BY MACKINNON*** | | | | The licensee reported that the emergency sirens were returned to service at | | 0930 EST on 01/04/99. | | | | NRC resident inspector was notified of this event update by the licensee. | | The NRC operations officer notified the R2DO (Pierce Skinner). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35212 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 01/02/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 08:51[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/02/1999| +------------------------------------------------+EVENT TIME: 07:45[CST]| | NRC NOTIFIED BY: MARSHALL FUNKHOUSER |LAST UPDATE DATE: 01/04/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MONTE PHILLIPS R3 | |10 CFR SECTION: |JOHN HANNON NRR | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP |ROSEMARY HOGAN IRD | | |JOSEPH HIMES RCT | | |CHARLES MILLER NRR | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE CONCLUDED THAT THE EMERGENCY RESPONSE ORGANIZATION COULD NOT MEET | | THE STAFFING TIME REQUIREMENT DUE TO ADVERSE WEATHER CONDITIONS. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | | | "10CFR50.72(b)(v) REQUIRES THE FACILITY TO NOTIFY THE NRC OPERATIONS CENTER | | DURING ANY EVENT THAT RESULTS IN THE MAJOR LOSS OF EMERGENCY OFFSITE | | RESPONSE CAPABILITY." | | | | "WEATHER CONDITIONS HAVE DETERIORATED DRIVING CONDITIONS PREVENTING MULTIPLE | | PERSONNEL FROM REACHING THE PLANT. BASED ON THESE RESULTS AND PRESENT | | WEATHER CONDITIONS, IT IS DOUBTFUL THAT THE EMERGENCY RESPONSE ORGANIZATION | | WOULD BE FILLED WITHIN THE REQUIRED TIME. THUS, THIS NOTIFICATION [IS] | | BEING MADE." | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | | | | ***UPDATE ON 01/04/99 AT 1240 EST FROM R. POWERS TAKEN BY MACKINNON*** | | | | WEATHER AND DRIVING CONDITIONS ARE NO LONGER HAZARDOUS, AND THE LICENSEE CAN | | FILL THE EMERGENCY RESPONSE ORGANIZATION POSITIONS AS OF 1135 CST ON | | 01/04/99. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS UPDATE BY THE LICENSEE. THE | | NRC OPERATIONS OFFICER NOTIFIED THE R3DO (BRENT CLAYTON). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35214 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 01/05/1999| | UNIT: [] [2] [] STATE: CA |NOTIFICATION TIME: 03:19[EST]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 01/04/1999| +------------------------------------------------+EVENT TIME: 20:51[PST]| | NRC NOTIFIED BY: HOWARD SMITH |LAST UPDATE DATE: 01/05/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOSEPH TAPIA R4 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE DETERMINED THAT THE CCW SYSTEM MAY NOT MEET ITS REQUIREMENT TO | | OPERATE FOR 7-DAYS WITHOUT MAKE-UP FOLLOWING A SEISMIC EVENT | | | | "AT SAN ONOFRE, THE COMPONENT COOLING WATER (CCW) SYSTEM IS REQUIRED TO | | PROVIDE COOLING FOR 7 DAYS WITHOUT MAKE-UP. CCW TRAINS A AND B ARE | | SEISMICALLY QUALIFIED; THE NON-CRITICAL LOOP IS NOT SEISMICALLY QUALIFIED. | | | | "UNIT 2 ENTERED MODE 5 AT APPROXIMATELY 0544 PST ON JANUARY 3, 1999, FOR A | | PLANNED REFUELING/MAINTENANCE OUTAGE. AT 2051 ON JANUARY 4, 1999, WHILE | | UNIT 2 WAS IN MODE 5, SCE DETERMINED THAT ISOLATION VALVE LEAKAGE BETWEEN | | CCW TRAIN B AND THE CCW NON-CRITICAL LOOP OBSERVED DURING A TS SURVEILLANCE | | EXCEEDED IT ACCEPTABLE LIMIT FOR OPERATION IN MODES 1 THROUGH 4 AND TRAIN B | | CCW COULD HAVE BEEN INOPERABLE PRIOR TO SHUT DOWN. TESTS WERE PERFORMED TO | | ATTEMPT TO DETERMINE WHETHER THIS LEAKAGE EXISTED DURING OPERATION IN MODES | | 1 THROUGH 4 PRIOR TO PLANT SHUT DOWN. HOWEVER, THE TESTS WERE UNABLE TO | | DETERMINE THAT THE LEAKAGE DID NOT EXIST PRIOR TO SHUT DOWN. DURING THE | | PAST CYCLE OF PLANT OPERATION, IF A SEISMIC EVENT WERE TO HAVE OCCURRED | | WHILE TRAIN A WAS OUT OF SERVICE, THERE WAS A POTENTIAL FOR THE CCW TO FAIL | | TO MEET ITS REQUIRED 7-DAYS OF OPERATION WITHOUT MAKEUP. THEREFORE, SCE IS | | CONSERVATIVELY MAKING THIS REPORT AS A NON-EMERGENCY 4-HOUR REPORT IN | | ACCORDANCE WITH 10CFR50.72(b)(2)(iii) - A CONDITION THAT ALONE COULD HAVE | | PREVENTED THE FULFILLMENT OF THE SAFETY FUNCTION OF THE CCW. | | | | "CCW IS PRESENTLY CAPABLE OF PERFORMING ITS SUPPORT FUNCTION FOR SHUT DOWN | | COOLING IN MODES 5 AND 6. THE ISOLATION VALVES' ACTUATORS WERE | | DISCONNECTED, THE VALVES WERE MANUALLY SEATED. THE MEASURED LEAKAGE WAS | | WELL BELOW THE ACCEPTABLE LEVEL FOR OPERATION IN MODES 1 THROUGH 4. THE | | ACTUATORS WERE RE-CONNECTED TO PROVIDE FOR REMOTE OPERATION. THE | | INVESTIGATION OF THE CAUSE AND CORRECTIVE ACTIONS IS ON-GOING.. | | | | "UNIT 3 IS IN MODE 1 AND UNAFFECTED BY THIS CONDITION." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+
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