Event Notification Report for January 4, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/31/1998 - 01/04/1999 ** EVENT NUMBERS ** 35207 35208 35209 35210 35211 35212 35213 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35207 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 12/31/1998| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 11:43[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 12/31/1998| +------------------------------------------------+EVENT TIME: 10:45[EST]| | NRC NOTIFIED BY: ED FIRTH |LAST UPDATE DATE: 12/31/1998| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK DURR R1 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTROL ROOM VENTILATION OUTSIDE DESIGN BASIS CALCULATION | | | | The Licensee made the following voluntary notification: "On December 31, | | 1998, while the plant was in operation, it was determined that based upon a | | review of a previous Nuclear Safety Evaluation (NSE-98-3-015), # 33 Safety | | Injection (SI) pump seal leakage placed the Control Room Ventilation System | | outside its system design basis calculation assumption for external | | recirculation system leakage (approximately 0.7 gph). The Control Room | | Ventilation System continues to remain operable as per an existing | | Operability Determination (#98-16). The New York Power Authority is | | currently evaluating repair options for this SI pump seal." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35208 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 12/31/1998| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 13:22[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 12/31/1998| +------------------------------------------------+EVENT TIME: 11:25[CST]| | NRC NOTIFIED BY: RICHARD HUBBARD |LAST UPDATE DATE: 12/31/1998| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INOPERABLE ATMOSPHERIC RELIEF VALVES | | | | The Licensee made the following notification: | | | | "On December 31, I998, WCNOC concluded that due to inoperable local control | | of Atmospheric Relief Valve (ARV), AB PV-2, LCO 3.7.1.6 was not met during | | certain periods of time. WCNOC Technical Specifications states that at | | least three ARVs shall be operable and with more than one inoperable, | | restore to operable within 24 hours. In addition to Technical Specification | | requirements, the USAR requires four ARVs to be operable to meet design | | basis cooldown requirements. To ensure the USAR requirements are met, WCNOC | | has implemented Operations Special Order #17 which is more restrictive than | | T.S. 3.7.1.6 by one additional ARV for all cases. This variance will be | | corrected when Improved Technical Specifications are implemented. During | | the period when the local control was not available for AB PV-2 other ARVs | | have been removed from service for longer than the 24 hour LCO time. | | Therefore, design bases requirements for safe shut down could not have been | | met in the event of a fire. | | | | "A local control modification was installed for two ARV to satisfy fire | | protection criteria in response to Generic Letter 92-08. During maintenance | | in June 1998, it appears that tubing, was re-installed incorrectly on the | | local control for AB PV-2. This condition was discovered during normally | | scheduled surveillance testing on December 30/31, 1998. Therefore, the | | potential operability for exceeding the LCO, was from June through December | | 1998. Engineering and Maintenance are continuing to evaluate this | | condition. | | | | "Maintenance activities are ongoing at this time to correct the tubing | | installation on AB PV-2. This work activity is expected to be completed by | | end of the day. Until that time, WCGS has entered the appropriate LCO." | | | | The Licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35209 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 12/31/1998| | UNIT: [] [] [3] STATE: SC |NOTIFICATION TIME: 15:57[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 12/31/1998| +------------------------------------------------+EVENT TIME: 14:35[EST]| | NRC NOTIFIED BY: REGIS REPKO |LAST UPDATE DATE: 12/31/1998| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PIERCE SKINNER R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 A/R Y 100 Power Operation |0 Hot Shutdown | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP DURING CONTROL ROD DRIVE BREAKER TESTING | | | | At 1435 hours on December 31, 1998, Oconee Unit 3 reactor tripped from 100% | | steady state operation. Control Rod Drive breaker testing was in progress | | at the time of the reactor trip. The 3A Reactor Protective System (RPS) | | channel was in bypass for the breaker testing. When the associated CRD | | breaker was tripped from the 3A RPS cabinet, the remaining three RPS | | channels actuated causing the reactor trip. All rods fully inserted and the | | plant responded properly to the reactor trip. The Unit is presently stable | | at hot shutdown in forced circulation cooling, main feedwater supplying the | | steam generators, and heat is being removed through the turbine bypass | | valves to the main condenser. The cause of the trip is unknown at this time | | and under investigation. | | | | The Licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35210 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 12/31/1998| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 16:02[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 12/31/1998| +------------------------------------------------+EVENT TIME: 15:15[EST]| | NRC NOTIFIED BY: TOM McELHINNEY |LAST UPDATE DATE: 12/31/1998| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK DURR R1 | |10 CFR SECTION: | | |ADEG 50.72(b)(1)(ii) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY RELATED PUMP ROOM TEMPERATURE LESS THAN DESIGN | | | | FSAR Table 10.9-1 specifies that intake structure design temperature is 60 | | -105�F with an outdoor temperature of 21�F. The Licensee determined that | | the intake structure temperature was below 60�F. Specifically, in safety | | related pump rooms (Salt Service Water) the temperatures were: | | | | Pump rooms A &B - 57�F | | Pump rooms D & E- 56�F | | Pump room C - 52�F | | | | Engineering has done a preliminary review of design requirements for | | safety-related equipment and has thus far shown that the equipment can | | perform its design function down to 32�F. | | | | Actions are underway to install temporary heaters and align ventilation to | | raise temperatures above 60�F. | | | | The Licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35211 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 01/01/1999| | UNIT: [1] [2] [3] STATE: AZ |NOTIFICATION TIME: 18:29[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 01/01/1999| +------------------------------------------------+EVENT TIME: 15:45[MST]| | NRC NOTIFIED BY: ALAN BRIESE |LAST UPDATE DATE: 01/01/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SIRENS FOUND INOPERABLE IN THE EMERGENCY PLANNING ZONE | | | | At 1545 MST on 1/1/99, PVNGS Unit 1 was informed by the Maricopa County | | Sheriff's Department that a routine Siren Interrogation Test failed for all | | (39) offsite sirens in the emergency planning zone. Appropriate personnel | | have been dispatched to troubleshoot and repair. Although the cause is | | currently unknown, there are no adverse weather conditions in the vicinity. | | Contingency procedures are in place to compensate for a failure of the | | offsite siren system. | | | | The licensee intends to inform the NRC Resident Inspector. | | | | Note similar events numbers 35174 and 35166 in December 1998. | | | | * * * UPDATE AT 1949 EST ON 01/01/99 BY ALAN BRIESE TO FANGIE JONES * * * | | | | At 1722 MST all offsite sirens have been returned to operation. The | | licensee intends to inform the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R4DO (Charles Marschall) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35212 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 01/02/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 08:51[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/02/1999| +------------------------------------------------+EVENT TIME: 07:45[CST]| | NRC NOTIFIED BY: MARSHALL FUNKHOUSER |LAST UPDATE DATE: 01/02/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MONTE PHILLIPS R3 | |10 CFR SECTION: |JOHN HANNON NRR | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP |ROSEMARY HOGAN IRD | | |JOSEPH HIMES RCT | | |CHARLES MILLER NRR | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE CONCLUDED THAT THE EMERGENCY RESPONSE ORGANIZATION COULD NOT MEET | | THE STAFFING TIME REQUIREMENT DUE TO ADVERSE WEATHER CONDITIONS. | | | | "10CFR50.72(b)(v) REQUIRES THE FACILITY TO NOTIFY THE NRC OPERATIONS CENTER | | DURING ANY EVENT THAT RESULTS IN THE MAJOR LOSS OF EMERGENCY OFFSITE | | RESPONSE CAPABILITY. | | | | "WEATHER CONDITIONS HAVE DETERIORATED DRIVING CONDITIONS PREVENTING MULTIPLE | | PERSONNEL FROM REACHING THE PLANT. BASED ON THESE RESULTS AND PRESENT | | WEATHER CONDITIONS, IT IS DOUBTFUL THAT THE EMERGENCY RESPONSE ORGANIZATION | | WOULD BE FILLED WITHIN THE REQUIRED TIME. THUS, THIS NOTIFICATION [IS] | | BEING MADE." | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35213 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 01/03/1999| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 13:54[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/03/1999| +------------------------------------------------+EVENT TIME: 11:15[CST]| | NRC NOTIFIED BY: STEVEN SEWELL |LAST UPDATE DATE: 01/03/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO TURBINE CONTROL SYSTEM MALFUNCTION | | | | The licensee reported that the turbine control system instantaneously | | reduced turbine load from 1161 MWe to about 200 MWe for an unknown reason. | | Multiple steam generator alarms were received, control rods began inserting, | | and the steam dumps opened in response to the turbine load decrease. | | Pressurizer relief valve PCV-455A opened momentarily due to the pressure | | transient. The reactor was manually tripped, all rods fully inserted, and | | the auxiliary feedwater pumps, both motor and steam turbine driven, started | | and restored steam generator level in all steam generators. The unit is | | stable in Mode 3, Hot Standby. All safety systems responded as expected and | | restart will be evaluated after further investigation of the cause of the | | event. | | | | The licensee notified the resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021