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… 1 100 Salem 2 100 Seabrook 1 100 Susquehanna 1 100 * Susquehanna 2 100 Three … Point 3 100 Turkey Point 4 29 REDUCED POWER FOR STEAM LEAK REPAIR * Vogtle 1 100 Vogtle 2 100 … Byron 1 100 Byron 2 100 Clinton 98 100% ELECTRICAL CAPABILITY D.C. Cook 1 100 D.C. Cook …
Power Reactor Status Report for December 20, 2015
… AWAY FROM OPERATING AT 800 MW (PER LOAD DISPATCH) Susquehanna 1 100 Susquehanna 2 100 Three … Sequoyah 2 80 INCREASING POWER FOLLOWING HIGH PRESSURE STEAM LINE LEAK REPAIR * Summer 100 Surry 1 100 … Byron 1 100 Byron 2 100 Clinton 99 100% ELECTRICAL CAPABILITY D.C. Cook 1 100 D.C. Cook …
Power Reactor Status Report for December 19, 2015
… AWAY FROM OPERATING AT 800 MW (PER LOAD DISPATCH) Susquehanna 1 100 Susquehanna 2 100 Three … * Sequoyah 2 74 HOLDING POWER TO REPAIR HIGH PRESSURE STEAM LINE LEAK * Summer 100 Surry 1 100 … Byron 1 100 Byron 2 100 Clinton 99 100% ELECTRICAL CAPABILITY D.C. Cook 1 100 D.C. Cook …
Power Reactor Status Report for December 18, 2015
… AWAY FROM OPERATING AT 800 MW (PER LOAD DISPATCH) Susquehanna 1 100 * Susquehanna 2 100 * Three … * Sequoyah 2 75 HOLDING POWER TO REPAIR HIGH PRESSURE STEAM LINE LEAK * Summer 100 Surry 1 100 … Byron 1 100 Byron 2 100 Clinton 99 100% ELECTRICAL CAPABILITY D.C. Cook 1 100 * D.C. Cook …
Power Reactor Status Report for December 17, 2015
… AWAY FROM OPERATING AT 800 MW (PER LOAD DISPATCH) Susquehanna 1 100 HIGH SYSTEM VOLTAGE ACTION … Sequoyah 2 74 HOLDING POWER TO REPAIR HIGH PRESSURE STEAM LINE LEAK * Summer 100 Surry 1 100 … Byron 1 100 Byron 2 100 Clinton 99 100% ELECTRICAL CAPABILITY D.C. Cook 1 100 HIGH SYSTEM …
Power Reactor Status Report for May 25, 2015
… 1 100 Salem 2 100 Seabrook 1 100 Susquehanna 1 100 HIGH SYSTEM VOLTAGE ACTION MINIMUM … Byron 1 100 Byron 2 100 Clinton 99 100% ELECTRICAL CAPABILITY D.C. Cook 1 100 MINIMUM … La Salle 1 100 La Salle 2 65 MAIN TURBINE STEAM VALVE TESTING AND POWER SUPPRESSION TO IDENTIFY …
Power Reactor Status Report for May 24, 2015
… 1 100 Salem 2 100 Seabrook 1 100 Susquehanna 1 100 HIGH SYSTEM VOLTAGE ACTION MINIMUM … Byron 1 100 Byron 2 100 Clinton 99 100% ELECTRICAL CAPABILITY * D.C. Cook 1 100 MINIMUM … * La Salle 1 100 La Salle 2 61 MAIN TURBINE STEAM VALVE TESTING AND POWER SUPPRESSION TO IDENTIFY …
Power Reactor Status Report for October 21, 2014
… ONE CONTINGENCY AWAY FROM DOWNPOWER DUE TO LINE OUTAGE * Susquehanna 1 100 * Susquehanna 2 100 * Three … Byron 2 0 09/28/2014 REFUELING OUTAGE Clinton 98 100% ELECTRICAL CAPABILITY D.C. Cook 1 0 09/23/2014 REFUELING … REFUELING OUTAGE Fermi 2 100 La Salle 1 25 STEAM LEAK REPAIR CONTINUING INCREASING POWER * La Salle 2 …
Power Reactor Status Report for October 20, 2014
… OUTAGE * Salem 2 100 Seabrook 1 100 * Susquehanna 1 100 HIGH SYSTEM VOLTAGE ACTION … Byron 2 0 09/28/2014 REFUELING OUTAGE * Clinton 98 100% ELECTRICAL CAPABILITY D.C. Cook 1 0 09/23/2014 REFUELING … Fermi 2 100 La Salle 1 15 HOLDING POWER FOR STEAM LEAK REPAIR * La Salle 2 100 Monticello 31 …
Power Reactor Status Report for February 19, 2019
… Salem 1 100 Salem 2 100 Seabrook 1 100 Susquehanna 1 100 Susquehanna 2 90 COASTDOWN TO … REDUCED POWER TO MAINTAIN CONDENSATE VACUUM WHILE REPAIRING STEAM JET * Browns Ferry 3 100 Brunswick 1 100 … Byron 1 100 Byron 2 100 Clinton 98 100% ELECTRICAL CAPABILITY D.C. Cook 1 95 COASTDOWN TO …