Information Notice No. 85-99: Cracking in Boiling-Water-Reactor Mark I and Mark II Containments caused by Failure of the Inerting System
SSINS No.: 6835 IN 85-99 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, DC 20555 December 31, 1985 Information Notice No. 85-99: CRACKING IN BOILING-WATER-REACTOR MARK I AND MARK II CONTAINMENTS CAUSED BY FAILURE OF THE INERTING SYSTEM Addressees: All boiling-water-reactor (BWR) facilities having a Mark 1 or Mark II con- tainment. Purpose: Information Notice No. 84-17, "Problems with Liquid Nitrogen Cooling Compon- ents Below the Nil-Ductility Temperature," was issued to describe a large crack in the vent header of Hatch Unit 2 that was attributed to brittle fracture caused by the injection of cold nitrogen during inerting system operation. The purpose of this information notice is to advise licensees and applicants of a crack discovered in the nitrogen inerting and purge line of Hatch Unit 1, and to re-emphasize the concern regarding inerting system failures that may result in cooling of components below the nil-ductility temperature (NDT) of associated materials susceptible to brittle fracture. It is expected that the recipients of this notice will review the information for applicability to their facilities and consider actions, if appropriate, to preclude similar problems at their facilities. However, suggestions contained in this notice do not constitute NRC requirements; therefore, no specific action or written response is required. Description of Circumstances: Hatch Unit 2 Vent Header Crack and Subsequent Actions - On February 3, 1984, Georgia Power Company reported a through-wall crack almost completely around the vent header within the containment torus of Hatch Unit 2. Later that day IE Bulletin 84-01, "Cracks in Boiling Water Reactor Mark 1 Containment Vent Headers," was issued for action to licensees of BWR facilities with Mark 1 containments that were in cold shutdown. The bulletin required inspection for cracks in the containment vent header and in the main vents in the region near the intersection with the vent header. The inspections by the licensees revealed no cracks. The bulletin also suggested that the operating BWR plants with Mark I containments should review their plant data on differential pressures between the wetwell and drywell for anomalies that could be indicative of cracks. The licensees who performed the review reported no anomalies. 8512270164 . IN 85-99 December 31, 1985 Page 2 of 3 Following the event, the Regulatory Response Group (RRG) of the BWR Owners Group (BWROG) met twice with the NRC staff, on February 6 and 23, 1984, to present the results of their investigation into,the cause of the event and the industry's plans to voluntarily take measures to prevent this type of event. The large crack in the Hatch 2 vent header was confirmed to be the result of brittle fracture caused by the injection of cold nitrogen into the torus during inerting. As a part of the industry plan, the RRG sent General Electric (GE) Service Information Letter (SIL) No. 402, "Wetwell/Drywell Inerting," to the BWROG representatives on February 17, 1984, and advised the owners to contact their respective NRC project manager on implementation status. The SIL contained several recommended actions to be taken by owners to confirm that equipment damage had not occurred and that inerting system design and operation was proper so that damage would not occur in the future. On March 5, 1984, Information Notice No. 84-17 was issued to describe the cause and safety significance of the vent header crack. During the meetings with the RRG, the NRC staff emphasized the need for each utility to contact its NRC project manager and provide a schedule and plans for actions relative to the SIL in order to ensure the regulatory closeout of the issue. By October 1, 1984, all utilities had provided written responses concerning their plans with respect to the SIL. The written responses varied significantly both in content and in level of detail. However, they all indicated that the SIL recommended actions or appropriate alternatives had already been taken or were planned. This led to a general conclusion by the NRC staff that the industry was taking all the necessary actions regarding this important safety issue. Hatch Unit 1 Nitrogen Inerting and Purge Line Crack - On December 15, 1984, inservice inspection (ISI) tests using a magnetic particle inspection method were being performed on selected pipe welds of Hatch Unit 1. During this testing, a linear through-wall crack approximately 2-3/4 inches long was discovered in a weld located in the 18-inch nitrogen inerting and purge line between the drywell penetration and inboard containment isolation valve (Ref: LER 84-25). The crack was ground out, and the weld was repaired and satisfactorily tested. The crack represented a breach of containment integrity. The licensee's investigation as described in the LER indicated that the crack was likely caused by thermally induced stress. The location of the crack is shown on the attached Figure 1. A 2-inch nitrogen makeup line enters the 18-inch purge line approximately 2 feet upstream from the crack. Cold nitrogen entering the purge line from the makeup line makes contact with the purge line in the area of the weld, the contour of which makes it a likely spot for a thermally induced failure to occur. Discussion: The NRC staff met with Georgia Power Company and its consultants on November 8, 1985, to discuss the safety and regulatory issues stemming from the Hatch Unit 1 crack. The primary conclusions reached at the meeting were as follows: . IN 85-99 December 31, 1985 Page 3 of 3 1. The likely cause of the Unit 1 crack Was the growth of a pre-existing weld defect. It is possible that cold nitrogen injection from the makeup system contributed to the growth of the crack. The nitrogen temperature is not monitored during a makeup evolution and there is no automatic shutoff on low temperature. A Nitrogen Inert System Makeup Low Temperature alarm exists, but this alarm was not covered in any annunciator response procedures. The licensee's corrective actions included raising the nitrogen makeup low temperature alarm set point to 10F from 0 F and revising the annunciator response procedures to terminate nitrogen makeup when the annunciator is actuated. 2. The licensee performed only a visual inspection of the Unit 1 nitrogen inerting and purge line welds rather than the ultrasonic testing recommended by the SIL. The visual inspections would not have discovered the crack found during the ISI. Therefore, the crack could have existed at the time the SIL was implemented. 3. The nitrogen makeup line was not considered by the licensee to be covered within the scope of the SIL as a source of cold nitrogen (less than 40 F) into containment systems, because of: the use of rela- tively low flow rates; and the long run if bare piping inside the warm reactor building. The licensee did confirm, however, that the makeup portion of the inerting system was in use for an 18 1/2-hour period in February 1984 when the ambient temperature did not get above 22 F. Makeup line nitrogen temperatures during this period were not known. No specific action or written response is required by this information, notice. If you have any questions about this matter, please contact the Regional Administrator of the appropriate regional office or this office. Edward L. Jordan, Director Division of Emergency Preparedness and Engineering Response Office of Inspection and Enforcement Technical Contact: R. Singh, IE (301) 492-4149 Attachments: 1. Figure 1: Hatch Unit 1 Nitrogen Inerting and Purge System 2. List of Recently Issued IE Information Notices
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021