Information Notice No. 84-80: Plant Transients Induced by Failure of Non-Nuclear Instrumentation Power
SSINS NO.: 6835 IN 84-80 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C. 20555 November 8, 1984 Information Notice No. 84-80: PLANT TRANSIENTS INDUCED BY FAILURE OF NON-NUCLEAR INSTRUMENTATION POWER Addressees: All Babcock and Wilcox Company (B&W) designed power reactor facilities holding an operating license (OL) or construction permit (CP). Purpose: This information notice is to alert recipients of potentially significant problems caused by failure of non-nuclear instrumentation (NNI) power supplies at B&W designed reactor facilities. It is expected that recipients will review the information for applicability to their facilities and consider actions, if appropriate, to preclude similar problems occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements and, therefore, no specific action or written response is required. Description of Circumstances: Rancho Seco: Repeated Partial Loss of NNI Power on March 19, 1984 The plant was operating at 92% power when a ground fault on a land steam exhauster caused the supply breaker to a motor control center (MCC) to trip. This supply breaker could not be reclosed. The loss of the MCC resulted in a loss of the hydrogen side seal oil pump for the main generator that is powered from that MCC. The plant continued operation as the licensee procedures and technical manual of the turbine-generator manufacturer (Westinghouse) allow full-load operation with the hydrogen side seal oil pump shut down. When operators initiated implementation of a procedure to restore the seal oil system, a small hydrogen explosion occurred and a reactor power reduction was initiated. Shortly thereafter, with the plant at 85% power, a large explosion and fire occurred and the turbine was immediately tripped. The reactor was automatically tripped by the recently installed anticipatory trip circuit. Following the large explosion, the fire burned for several minutes and was extinguished by the CO2 system. The explosion resulted in the generator housing lower skirts being thrown into some neighboring equipment. The missiles also broke two large handwheels for valves and damaged some small test valves and non-safety-related level instruments. 8411060254 . IN 84-80 November 8, 1984 Page 2 of 4 Shortly after the reactor trip, the operators proceeded to start auxiliary boilers to provide for the auxiliary steam loads. The small boiler was successfully fired. When the control power for the big boiler was turned on, in preparation for its start, the small boiler tripped and control power to both boilers was lost. At the same time, several alarms were annunciated in the control room indicating NNI power failure and nonvital power bus trouble. Investigation by the licensee revealed that the voltmeters on the non-Class 1E J inverter were pegged low. The J inverter provides alternate power to NNI-X and Y, and control power for auxiliary boilers. The licensee believes that some of the equipment damaged during the fire and explosion caused several grounds in the 125-V dc supply bus to the J inverter, resulting in voltage degradation. During restoration of the J inverter to operability, + - 24-V dc power of the NNI-X power distribution system was lost for approximately 4 minutes as a result of deenergization of the inverter along with the spurious loss of the -24-V dc bus. The licensee believes that the loss of the -24-V dc bus was caused by drift of the low output voltage set point of the power supply. The loss of NNI-X + - 24-V dc was perceived to be a total loss of NNI power in the control room because numerous instrumentation failed to midscale and "Power On" lights on NNI cabinets appeared to be off. Based on these indications, operators implemented the "Complete Loss of NNI Power" procedure which required manual initiation of the safety features actuation system (SFAS). SFAS initiation started the high pressure injection (HPI) pumps and opened the HPI valves. As the reactor coolant system pressure began to increase, a pressurizer code safety valve opened prematurely (about 140 psi below the 2,500 psig set point). The safety valve opened twice and reseated both times during the event. At Rancho Seco, the power-operated relief valve (PORV) is kept in the locked closed position. During the event, an atmospheric dump valve also opened as a result of NNI-X loss, but it was recognized and closed from the control room. The licensee personnel continued troubleshooting the NNI power supplies when a second partial loss of NNI power occurred approximately 3 hours after the explosion. The 115-V ac power of the NNI-X power distribution system was lost for approximately 5 minutes when the supply breaker from Class 1E D inverter to NNI-X was manually tripped and the automatic bus transfer (ABT) switch did not transfer the loads to the J inverter as it was still operating at degraded voltage. The D inverter provides the normal power to NNI-X and Y. Crystal River Unit 3: Loss of NNI-Y Power on April 26, 1984 The plant was operating at 97% power when the dc power supply of the NNI-Y power distribution system failed as a result of the failure of a capacitor with wrong ratings installed by the manufacturer in the + - 24-V dc supply. The loss of NNI-Y dc power caused erroneous signals to be sent to the integrated control system (ICS). The ICS rapidly reduced the feedwater flow to one of the steam generators causing an undercooling transient. The reactor tripped on high reactor coolant system pressure. The atmospheric dump valves (ADVs) and main steam safety valves (MSSVs) subsequently opened. One ADV and several MSSVs failed to reseat resulting in a small radioactive release since there was a . IN 84-80 November 8, 1984 Page 3 of 4 previously identified small steam generator tube leak. The release did not cause any regulatory limits to be exceeded. The ADV was manually isolated and the MSSVs reseated after steam generator pressure was reduced. The NNI-Y power failure caused erroneous indications and prevented the automatic control of some non-safety-related systems. However, plant operators were able to identify the erroneous indications immediately and control the plant by using the redundant set of instrumentation powered from the NNI-X power distribution system. Other systems affected by the loss of NNI-Y included the condensate system, the plant computer, and a number of annunciator event alarms. Discussion: These recent operating events at Rancho Seco and Crystal River Unit 3 have again demonstrated that the failure of NNI power has the potential of causing transients as well as challenges to an operator's capability to mitigate those transients at B&W reactor plants. The NRC staff has met recently with licensees and the B&W Owners Group to discuss the implications of such events and the effectiveness of improvements made in responding to transients caused by loss of NNI power supplies since publication of IE Bulletin 79-27, "Loss of Non-Class IE Instrumentation and Control Power During Power Operation." From the responses to the Rancho Seco and Crystal River events, it was evident to the staff that significant improvements have been made since the bulletin. In addition, the corrective actions taken by both licensees after the events are expected to further reduce the frequency of loss of NNI power events. The corrective actions taken before the restart of Rancho Seco included readjusting of NNI and ICS dc power supplies overvoltage and undervoltage trip set points. The licensee's long-term actions include: consideration for installation of an automatic transfer switch between the normal supply and backup supply for the J 120-V ac bus to reduce the chance of loss of NNI dc power on loss of a single inverter; investigation into the possibility of providing a single computer manual action that would place the appropriate computer points, unaffected by loss of NNI, on analog trend (the current procedure takes several minutes); scheduling the calibration of + - 24-V NNI and ICS power supply alarm and trip settings once every refueling outage; revising operating procedure NNI drawings and plaques on the NNI panels to more correctly indicate system functions; revising the plant training manual to include more detailed NNI and ICS power supply descriptions; and modification of NNI/ICS panels, as necessary, to eliminate physical contact of the doors with power supply wiring. For Crystal River Unit 3, the corrective actions included: inspection of power supplies similar to the failed NNI-Y +24-V dc power supply for correct capacitors; scheduling inspection of NNI-X power supplies; and future installation of redundant power supplies for NNI-Y. The redundant power supplies would prevent a transient, similar to the one caused by a failed capacitor, from occurring as a result of a single 24-V dc power supply failure. After this modification, both NNI-X and NNI-Y will have redundant power supplies. . IN 84-80 November 8, 1984 Page 4 of 4 No specific action or written response is required by this information notice. If you have any questions regarding this matter, please contact the Regional Administrator of the appropriate NRC regional office or this office. Edward L. Jordan, Director Division of Emergency Preparedness and Engineering Response Office of Inspection and Enforcement Technical Contact: R. N. Singh, IE (301) 492-8985 Attachment: List of Recently Issued IE Information Notices
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