Information Notice No. 84-74: Isolation of Reactor Coolant System from Low-pressure Systems Outside Containment
SSINS No.: 6835 IN 84-74 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, DC 20555 September 28, 1984 Information Notice No. 84-74: ISOLATION OF REACTOR COOLANT SYSTEM FROM LOW-PRESSURE SYSTEMS OUTSIDE CONTAINMENT Addressees: All nuclear power reactor facilities holding an operating license (OL) or a construction permit (CP). Purpose: This information notice is provided as a notification of potentially significant problems in maintaining isolation boundaries between the high-pressure reactor coolant system (RCS) and low-pressure piping systems outside containment. These problems contribute to an increased likelihood of an intersystem loss-of-coolant accident (LOCA) which would bypass primary containment. It is expected that recipients will review the information for applicability to their facilities and consider actions, if appropriate, to preclude similar problems occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements and, therefore, no specific action or written response is required. Description of Circumstances: Pilgrim At Pilgrim, on September 29, 1983, the low-pressure section of the high pressure coolant injection (HPCI) suction piping was overpressurized during functional testing of the HPCI system logic. The cause was personnel error while conducting more than one surveillance test at the same time. The prerequisites and initial conditions were not met for all steps. This led to the simultaneous opening of two motor-operated HPCI discharge valves. A testable injection check valve should have isolated the HPCI from the RCS. However, the movable internals of this valve were bound by rust. Apparently, this condition held the valve partially open during normal operation, but did not prevent closing when pressure was applied. As a result, a sudden but brief overpressurization of the HPCI piping occurred. The Pilgrim check valve was repaired and tested. The licensee held a critique with operators and instrumentation and control technicians and initiated administrative actions to ensure strict compliance with surveillance procedure action steps. 8409270525 . IN 84-74 September 28, 1984 Page 2 of 4 Hatch Unit 2 At Hatch Unit 2 in October 1983, it was found that a testable check valve had been held open for about 4 months by an incorrectly assembled actuator. This is a swing-type testable check valve with an air actuator controlled by a four-way pilot solenoid valve. It is installed on a 24-inch low pressure coolant injection (LPCI) line. The second isolation device on this line is a normally closed motor-operated gate valve. The gate valve automatically receives a signal to open upon a LPCI actuation signal but has independent diverse interlocks to prevent opening at high differential pressure. The Hatch event resulted from a series of errors. On June 7, 1983, during maintenance on the valve actuator, the two air supply lines were installed backwards. The air supply line to the right-hand cylinder of the actuator was incorrectly connected to the left-hand cylinder, and vice versa. Failure to use a vendor maintenance manual appears to have contributed to this error. Inadequate post-maintenance functional testing of the valve allowed the initial error to go undetected. The check valve position is indicated in the control room. It is not known with certainty why this did not lead to early detection. However, it appears likely that, after maintenance, the indication was readjusted to show a closed position in the belief that the check valve must actually be closed. A Hatch plant maintenance worker was counseled by utility management on the importance of performing correct maintenance and the importance of using maintenance manuals and performing thorough post maintenance testing before returning components to service, particularly for components that are safety-related. For the longer term, the licensee is considering alternative methods of testing the check valve using shutdown cooling flow. This could allow permanently deactivating the actuator without interfering with check valve operability or position indication. Browns Ferry Unit 1 At Browns Ferry Unit 1, on August 14, 1984, the core spray system was overpressurized. In December 1983 or earlier, during maintenance on the pilot solenoid valve for the testable check valve, a plunger with reversed air ports was apparently installed in the solenoid valve. This resulted in the check valve being held open. Then in August, while performing a semi-annual logic functional test, the operators failed to electrically disarm the motor-operated injection valve. The motor-operated valve opened with the testable check valve open. The core spray system, designed for 500 psi, was pressurized above 500 psi, lifting the small relief valve installed on the line. The maximum core spray system pressure is not known. Operators observed that the control room pressure gauge read off-scale (above 500 psi) and the pressure might have approached primary coolant system pressure (about 1050 psi). The piping was not damaged, probably because of substantial design margins. The pump discharge check valves in combination with open pump suction valves apparently prevented overpressurizing the pump suction piping which is designed for 150 psi. . IN 84-74 September 28, 1984 Page 3 of 4 The Browns Ferry occurrence was caused by errors similar to those in the Hatch event. The solenoid valve had been reassembled incorrectly and without using a maintenance manual. The proximity switch and the air actuator had been readjusted providing an erroneous closed position indication. Post-maintenance testing was inadequate. Finally, during the logic functional test, there was a failure to properly follow the test procedure and to disarm the outboard motor-operated valve. The licensee's final corrective actions are yet to be determined. Discussion: The events described above are considered to be significant because they substantially reduced safety margins for preventing an intersystem LOCA that bypasses containment. When the testable check valve is open, a postulated failure or inadvertent opening of, the motor-operated valve could allow discharge of high-pressure reactor coolant into low-pressure systems. The consequences of such an event are not certain. The flowrate through the motor-operated valve could vary from a small amount of leakage to a massive discharge. If the flow force were moderate, it could close the check valve despite the actuator. This would effectively terminate the event. If, however, the forces were large, the movable internal portions of the check valve could be severely damaged. A substantial failure of the low-pressure system, if it were to occur, would lead to a LOCA that bypasses the containment and could flood the low-pressure ECCS pumps. This would be an accident exceeding current design basis with radioactive material discharged outside the primary containment. Other plants were thought to have a valve configuration similar to that of Hatch. Following the Hatch event, the NRC's Office of Analysis and Evaluation of Operational Data (AEOD) prepared Engineering Evaluation Report E414, "Stuck Open Isolation Check Valve on the Residual Heat Removal System at Hatch Unit 2," on May 31, 1984. This report confirmed that a number of BWRs have a similar residual heat removal (RHR) system configuration (i.e., a testable check valve inside primary containment and a motor-operated injection valve outside primary containment). Additional plants found with this configuration include Duane Arnold, Brunswick 1 and 2, Cooper, Dresden 2 and 3, Hatch 1, FitzPatrick, Monticello, Peach Bottom 2 and 3, Pilgrim, and Quad Cities 1 and 2. In the Pilgrim and Browns Ferry events, the low-pressure section of the HPCI suction piping and one loop of the core spray system, respectively, were actually overpressurized. The potential for an accident was increased by degradation of the barriers. It is suggested that licensees of nuclear reactor facilities consider reviewing their practices and controls in the area of maintenance activities involving air-operated testable check valves, especially where such valves provide isolation barriers for the reactor coolant system. It is also suggested that licensees consider reviewing their practices and controls to ensure that instrument and logic tests do not permit the inadvertent opening of motor-operated valves, especially where these valves also provide isolation barriers for the reactor coolant system. . IN 84-74 September 28, 1984 Page 4 of 4 No specific action or written response is required by this information notice. If you have any questions about this matter, please contact the Regional Administrator of the appropriate NRC Regional Office or this office. Edward L. Jordan, Director Division of Emergency Preparedness and Engineering Response Office of Inspection and Enforcement Technical Contacts: M. S. Wegner, IE (301) 492-4511 S. Newberry, NRR (301) 492-8932 Attachment: List of Recently Issued IE Information Notices
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021