Information Notice No. 84-39: Inadvertent Isolation of Containment Spray Systems
SSINS No.: 6835 IN 84-39 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C. 20555 May 25, 1984 Information Notice No. 84-39: INADVERTENT ISOLATION OF CONTAINMENT SPRAY SYSTEMS Addressees: All pressurized water power reactor facilities holding an operating license (OL) or construction permit (CP). Purpose: This information notice is provided to alert licensees and applicants of the potential for significant degradation of safety associated with the inadvertent isolation of containment spray. Recipients are expected to review the information for applicability to their facilities and consider actions, if appropriate, to preclude similar problems occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements and, therefore, no specific action or written response is required. Description of Circumstances: Farley Unit 2 Farley Unit 2 was taken to cold shutdown on October 24, 1982, to begin a refueling and maintenance outage. On October 28, 1982, while aligning valves for certain scheduled inservice inspections, the licensee found the containment spray header isolation valve on each of the two supply headers locked in the closed position. These valves, located inside the Unit 2 containment building, supply separate, redundant, containment spray rings. After investigation and record searches of valve movement documentation, the licensee concluded that the valves had been closed since before the plant achieved initial criticality on May 8, 1981. Thus the redundant, containment spray systems were inoperable during this period and consequently would have been unable to fulfill their safety function. The event was caused by the valves not being in conformance with design draw-ings and by the inadequacy of the procedure used by an operator to determine the position of the valves. A unique condition developed in these valves when the vendor, Westinghouse, made a design change that lengthened the valve stem to increase the valve's adaptability to a motor-operated valve (however, the motors to operate the valves were never installed and the valves remained manually operated). The design change resulted in a valve stem that makes the valve appear to be open when it is actually closed. That is, the extra long valve stem shows 6 inches of threaded stem extending out of the bonnet when the valve is in the closed position. 8405230319 . IN 84-39 May 25, 1984 Page 2 of 5 Therefore, operators, who were instructed and trained to observe valve stem position to verify the valve positions, erroneously interpreted these valves as being open when they were, in fact, closed. Indian Point Unit 2 On November 29, 1983, while the licensee was performing a bimonthly (every two months) containment spray pump surveillance test during normal operation, two motor-operated spray header isolation valves were found in the locked closed, de-energized position instead of the required locked open, de-energized position. This condition would have prevented automatic actuation of the containment spray system during the safety injection phase of an accident. A review of conditions leading up to this event revealed that on October 12, 1983, during a cold shutdown, these valves were closed and tagged out of service so that work could be performed on the reactor coolant system. On October 18, 1983, while still in the cold shutdown condition, the tagout was cleared even though these valves were specified to remain closed to block the containment spray paths while personnel continued to work in the containment. Before plant startup, operators were assigned to complete a Safety Injection System Check-Off List (COL-12), which should have returned the valves to their proper positions before heating the reactor coolant system above 350 degrees. COL-12 was performed on October 23 and 24, 1983. It required one operator to ensure the correct valve position and a second operator to verify the posi- tion. COL-12 directs the operators to the motor control centers to perform two verifications for each valve: (1) verify that the position of the valve is open and (2) verify that the breaker is de-energized. In the de-energized condition, position indication for the valve is lost at the motor control centers. Verifying position at the motor control center, therefore, requires energizing the breaker. The first operator assumed that the valve was posi- tioned by another operator. The second operator assumed the valve was open because the breaker was locked in the de-energized position. San Onofre Unit 3 On March 17, 1984, during routine surveillance at approximately 100% power, manual isolation valves in both of the containment spray headers were found closed, rendering both trains of the containment spray system (CSS) inoper- able. Misalignment of the isolation valves was caused by improper use of the valve alignment checklist for the CSS when leaving the shutdown cooling mode. Unit 3 entered Mode 4 (hot shutdown) following an extended surveillance and maintenance outage on February 27, 1984. The valve alignment checklist was completed and verified by two operators for the CSS on February 28, which confirmed the spray header isolation valves to be open as required for CSS operability in Modes 1-3. . IN 84-39 May 25, 1984 Page 3 of 5 Because of the inoperability of a safety injection system (SIS) valve, Unit 3 re-entered Mode 5 (cold shutdown) on February 23. Valve alignments were completed for operation of the shutdown cooling system, including closure of the containment spray header isolation valves. Valve repairs were completed for the SIS valve and Unit 3 again entered Mode 4 and left shutdown cooling on March 2, 1984. Instead of reperforming the entire CSS valve alignment checklist completed on February 28, the cognizant control room supervisor, a senior reactor operator (SRO), designated valves on the completed February 28 checklist to be repositioned and double-verified. At San Onofre an SRO was permitted to designate a portion of a checklist to be performed when changes in system status do not require the entire checklist to be performed. Double-verifications were conducted in this instance for which of the valves designated, as required. This repositioning was completed before entry into Mode 3 on March 4, 1984. However, because of an oversight by the SRO, the containment spray header isolation valves were not designated to-be repositioned, and they remained closed until March 17, 1984. Other Events The staff has observed other events where procedural or personnel errors would have prevented operation of the containment spray systems. While most of these events only resulted in system inoperability for a few minutes or hours, the potential was there for extended plant operation with these safety systems inoperable. In addition to the containment spray system, the following events include examples of inadvertent valving out of the chemical addition tank. The following is a partial list of both types of events: Davis-Besse On January 12, 1978, both containment spray pumps were found with the circuit breakers de-energized. Personnel error resulted in 24 hours of plant operation (Mode 4) with the system inoperable. D.C. Cook Unit 2 On May 2, 1978, during change from Mode 5 to Mode 4, containment spray pumps remained inoperable when control switches were left in the locked out posi- tion. Procedural and personnel error left the system inoperable for 4 hours. Davis Besse On December 28, 1978, 2 hours after entering Mode 4, containment spray pump motor breakers were found in the locked out position. This was caused by an operator failing to follow procedures. . IN 84-39 May 25, 1984 Page 4 of 5 Indian Point Unit 2 On September 24, 1980, both containment spray,pump control switches were found in the pull-to-lock position by the resident inspector while the plant was at full power. Plant procedures called for disabling the containment spray during containment entry. The licensee was informed of noncompliance, with Technical Specifications which require the operability of containment spray when the plant is at power, and the procedures were subsequently revised. Point Beach Unit 1 On June 21, 1981, while performing periodic surveillance, the spray additive tank isolation valve was found in the closed position, thus preventing in- jection of NaOH to the containment spray system. Operator error left the valve misaligned for 4 days. Farley Unit 2 On December 26, 1981, while performing surveillance testing, the isolation valve on the NaOH spray additive tank was found in the closed position. This was caused by operator error during position alignment checks. Farley Unit 1 On May 10, 1982, while performing Penetration Room Exhaust and Air Filtration System Train Operability and Valve Inservice Test, an operator inadvertently closed the containment spray suction valves from the refueling water storage tank (RWST). The valves were closed for 7 hours while the reactor was at power. Surry Unit 1 On October 16, 1982, isolation valves leading from the chemical addition tank were found in the closed position. The cause was attributed to personnel failure to perform valve alignment checks. Ginna On June 13, 1983, while changing modes (cold shutdown to hot shutdown), the containment spray pumps were found in the pull-to-lock position. Turkey Point Unit 4 On October 4, 1983, a nonlicensed operator assigned to close the spray header isolation valves on Unit 3 (cold shutdown) inadvertently closed the identical valves on Unit 4. Unit 4 operated at power with these valves closed for approximately 50 hours. . IN 84-39 May 25, 1984 Page 5 of 5 Discussion: The intent of this information notice is to heighten awareness of industry to the potential for significant problems involving the inadvertent isolation of containment spray systems (CSSs). During shutdown conditions when containment entries are being made, PWR operators find it desirable to close the manual isolation valves in each spray header and/or put the spray pump control switches in the pull-to-lock position. These actions prevent inadvertent containment spray actuation during maintenance and testing activities. However, when valve l alignment check-off lists are completed before restart, procedural inadequacies or personnel errors have resulted in plants going back to power with the isolation valves closed or the pumps in the pull-to-lock position, thus preventing automatic operation if needed. The NRC recommends that recipients of this notice review their existing pro- cedures for locking out and returning containment spray systems to operation and determine whether any changes to the existing procedures would be desir- able in light of the information contained herein. No written response to this information notice is required. If you need additional information about this matter, please contact the Regional Administrator of the appropriate NRC regional office or this office. Edward L. Jordan, Director Division of Emergency Preparedness and Engineering Response Office of Inspection and Enforcement Technical Contacts: Douglas Pickett, NRR (301) 492-7876 Eric Weiss, IE (301) 492-4973 Attachment: List of Recently Issued IE Information Notices
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021