Information Notice No. 82-26: RCIC and HPCI Turbine Exhaust Check Valve Failures
SSINS No.: 6835 IN 82-26 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C. 20555 July 22, 1982 Information Notice No. 82-26: RCIC AND HPCI TURBINE EXHAUST CHECK VALVE FAILURES Addressees: All boiling water nuclear power reactor facilities holding an operating license or construction permit. Purpose: This information notice is provided as an early notification of a potentially significant problem pertaining to reactor core isolation cooing (RCIC) and high pressure coolant injection (HPCI) turbine exhaust check valve failures. It is expected that recipients will review the information for applicability to their facilities. No specific action or response is required at this time. Description of Circumstances: A number of RCIC turbine exhaust check valve failures that have occurred during the past 20 months are outlined below. 1. On December 10, 1980, Carolina Power and Light Company reported (LER 80-101/03L) a RCIC system turbine trip at Brunswick Steam Electric Plant, Unit 2, while conducting a RCIC system test. The turbine tripped on high turbine exhaust pressure due to the turbine exhaust swing check valve failing in the closed position. Inspection revealed the check valve disc stem had broken off where it connects to the valve hinge assembly. This allowed the disc to fall into the discharge part of the valve and isolate flow. An examination of the check valve disc and hinge assembly indicated the disc had been rotating inside of the hinge bore area and caused excessive wear of both components. In addition, indications that the valve disc had been striking the upper part of the valve body while in the open position were noted. To return the check valve to normal operability, the valve seat was lapped, the valve disc replaced, and the valve was tested satisfactorily. This LER also referred to a similar failure (LER 79-074/03L) at Brunswick Steam Electric Plant, Unit 1. This time, disassembly of the RCIC steam exhaust check valve showed that the stud and nut on the back of the disc had broken and the disc had separated from the hinge and had lodged in the valve inlet. A new valve was ordered and installed upon arrival. The valve failure prevented the RCIC turbine, which had been used intermittently throughout the day for vessel level control, from starting following a reactor scram. 8204210398 . IN 82-26 July 22, 1982 Page 2 of 4 2. On May 29, 1981, Pennsylvania Power and Light Company reported (ERs 100450/100508) the failure of the RCIC turbine exhaust swing check valve at Susquehanna Steam Electric Station, Unit 1, while conducting a RCIC system test. The stud (integrally cast with the disc) which attached the disc, to the valve hinge broke off. In a subsequent report on February 5, 1982, they indicated that turbine exhaust steam flow conditions experienced during testing caused the valve disc to cycle violently open and close. Since the check valve was sized for full flow, operational testing of the system at low flow caused the disc function to be erratic. As a result, the end of the disc stud gradually wore a hole in the valve bonnet (cover) which served as the stop. This additional travel allowed the disc edge to impact against the valve body due to a lack of clearance. The loads and stresses experienced by the disc resulted in a disc stud fracture. The failure was a brittle fracture. A second disc, taken from Unit 2, was put in service to replace the fractured disc. This disc also failed at approximately the same section as the first. Therefore, they concluded that with both the valve and system as presently designed, a swing check valve disc will fail for this service application. This was further evidenced by three more replacement discs that eventually broke in a similar fashion in spite of the provision of a specially designed "anvil" nut to replace the original nut. They are planning on either replacing the existing valve with a lift type check valve design having an inherent damping action in the opening position or modifying the existing valve and/or piping system so that the valve will function properly under both, low and high flow conditions. (See Information Notice No. 82-20.) 3. On December 10, 1981, Georgia Power Company reported (LER 81-112/03L),a RCIC isolation at Edwin I. Hatch Nuclear Plant, Unit 2, while conducting a RCIC rated flow test. An investigation revealed that the turbine exhaust check valve had internal damage creating a block in the line causing the rupture diaphragm to fail. The valve was repaired and the diaphragm replaced. A design change has been approved to replace the check valve with a better design. The new valve has been ordered and will be installed as soon as possible. A generic review, by the licensee, revealed that the HPCI system has the same valve type in a similiar configuration and that a design change has been approved to replace the valve. 4. On March 9, 1982, Long Island Lighting Company reported a deficiency concerning two check valves located in the RCIC turbine exhaust line at Shoreham Nuclear Power Station. The deficiency was identified while t testing the turbine and pump using auxiliary steam at low flow conditions. Examination of the valves disclosed that the slamming and cyclic action of the valve resulted in wear to the swing check bushings, the anti-rotation pins, and the swing checks. The valve bodies showed rubbing marks from the interaction with the swing check. A systems review of the valve failures, by the licensee, indicated that damage to these components could have an . IN 82-26 July 22, 1982 Page 3 of 4 impact on the turbine exhaust back pressure thereby causing the turbine to trip. All damaged components of the RCIC exhaust check valves will be replaced and the valves will be rebuilt to assure properly conditioned and working valves are installed. Discussion: All of the above failures deal only with the RCIC turbine exhaust check valve. However, as noted by Georgia Power Company, the HPCI exhaust system has the same type valve in a similiar system configuration. Thus it is reasonable to expect similiar problems with the HPCI turbine exhaust check valve also. In fact, both services have been identified in the generic correspondence by General Electric pertaining to this topic. The first of the generic correspondence is Services Information Letter (SIL) No. 30, "HPCI/RCIC Turbine Exhaust Line Vacuum Breakers," dated October 31, 1973. In this SIL, General Electric identified the problem of possible damage to the exhaust line check valve and recommended the installation of vacuum breakers based on tests conducted at Browns Ferry and Peach Bottom. The second of the generic correspondence is Application Information Document (AID) No. 56, "High Pressure Core Injection and Reactor Core Isolation Cooling Turbine Exhaust Check Valve Cycling," dated December 18, 1981. In this AID, General Electric identified the possible causes of failure as improper system operation, improper check valve sizing, inadequate check valve design, or inadequate exhaust line design. To minimize the possibility of future problems, they recommend that: 1. Manual starts and monthly system surveillance testing should be performed in accordance with the Operating and Maintenance Instructions (specifically, gradually increasing the turbine speed until the rated pump discharge flow is achieved is not recommended). 2. The exhaust check valve, the exhaust line vacuum breaker, and the exhaust line sparger should be designed in accordance with the requirements/ recommendations given in the GE system design specification. 3. System operation below the recommended turbine rated speed should be minimized. 4. The exhaust check valve should be located as close as possible to the containment. 5. The turbine exhaust check valve internals should be visually inspected on a routine schedule such as at every refueling outage. . IN 82-26 July 22, 1982 Page 4 of 4 If you have any questions regarding this matter, please contact the Regional Administrator of the appropriate NRC Regional Office, or this office. Edward L. Jordan, Director Division of Engineering and Quality Assurance Office of Inspection and Enforcement Technical Contact: Richard J. Kiessel 301-492-8119 Attachment: List of Recently Issued IE Information Notices
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021