Part 21 Report - 1995-074
ACCESSION #: 9412120191 LICENSEE EVENT REPORT (LER) FACILITY NAME: HOPE CREEK GENERATING STATION PAGE: 1 OF 5 DOCKET NUMBER: 05000354 TITLE: Single condition which could have affected the operation of multiple systems - failure of cooling water isolation valves for diesel generators to stroke open EVENT DATE: 11/10/94 LER #: 94-017-00 REPORT DATE: 12/08/94 OTHER FACILITIES INVOLVED: DOCKET NO: 05000 OPERATING MODE: 1 POWER LEVEL: 100 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR SECTION: 50.73(a)(2)(v) LICENSEE CONTACT FOR THIS LER: NAME: Lou Aversa, Senior Staff TELEPHONE: (609) 339-3386 Engineer - Technical COMPONENT FAILURE DESCRIPTION: CAUSE: SYSTEM: COMPONENT: MANUFACTURER: REPORTABLE NPRDS: SUPPLEMENTAL REPORT EXPECTED: NO ABSTRACT: On Saturday, October 22, 1994, during performance of a quarterly In Service Test of the Safety Auxiliary Cooling System (SACS) two room cooler isolation valves failed to stroke open. The valves were associated with the diesel room coolers for the "B" and "D" diesel generators. The valves are air operated and designed to fail open on loss of air to the actuator. The valves were mechanically agitated and subsequently stroked open. The air supply to these two isolation valves was tagged closed and the valves were left in the open position to ensure the safety function to provide cooling in the diesel generator room was satisfied. System Engineering was contacted and informed of the failure as this was a repeat of a similar condition identified in September of 1993. System Engineering immediately initiated a root cause investigation to determine the cause of the stroke failures. On November 10, 1994, the investigation determined that a common mode failure existed and that the condition was reportable. The valve stroke frequency was increased to weekly from quarterly because at this frequency no failures have been noted. The root cause of this event is design deficiency. All valves will be stroked weekly until the packing configuration is corrected. END OF ABSTRACT TEXT PAGE 2 OF 5 PLANT AND SYSTEM IDENTIFICATION General Electric - Boiling Water Reactor (BWR/4) Safety Auxiliary Cooling System (EG) EIIS IDENTIFIER (CC) IDENTIFICATION OF OCCURRENCE TITLE (4): Single condition which could have affected the operation of multiple safety systems - failure of cooling water isolation valves for diesel generators to stroke open. Discovery Date: 11/10/94 Event Dates: 10/22/94 Event Time: 1427 This LER was initiated by Incident Report No. 94-185 CONDITIONS PRIOR TO OCCURRENCE Plant in OPERATIONAL CONDITION 1 (Power Operation) Reactor Power 100% of rated, 1109 MWe DESCRIPTION OF OCCURRENCE On Saturday, October 22, 1994, during performance of a quarterly In Service Test of the Safety Auxiliary Cooling System (SACS) two room cooler isolation valves failed to stroke open. The valves were associated with the diesel room coolers for the "B" and "D" diesel generators. The valves are air operated and designed to fail open on loss of air to the actuator. The valves were mechanically agitated and subsequently stroked open. The air supply to these two isolation valves was tagged closed and the valves were left in the open position to ensure the safety function to provide cooling in the diesel generator room was satisfied. System Engineering was contacted and informed of the failure as this was a repeat of a similar condition identified in September of 1993. System Engineering immediately initiated a root cause investigation to determine the cause of the stroke failures. On November 10, 1994, the investigation determined that a common mode failure existed and that the condition was reportable. The valve stroke frequency was increased to weekly from quarterly because at this frequency no valve stroke failures have been noted. ANALYSIS OF OCCURRENCE The Safety Auxiliaries Cooling System (SACS) provides all station cooling requirements for Emergency Core Cooling Systems (ECCS) and Diesel Generator Systems. The SACS system consists of two independent redundant loops each of which are normally lined up to provide cooling to associated safety related equipment. Selected safety related loads can be manually transferred to an operable loop if one loop is TEXT PAGE 3 OF 5 ANALYSIS OF OCCURRENCE inoperable. Redundant coolers and fans are provided in each ECCS pump room and diesel generator room. The cooling water isolation valves are pneumatically operated, fail open type gate valves. A solenoid valve operates an internal three way pilot which repositions to vent air from the actuator upon receipt of a valid open signal. All valves involving stroke failures are Anchor-Darling flex wedge gate valves utilizing Hiller pneumatic actuators. The failure experienced during this event is similar to that identified in a previous License Event Report (LER 93-006-00). The analysis performed for the previous event attributed the failure to excessive air pressure being supplied to the actuator causing the valve disk to bind in the seat. This condition resulted when the packing style was changed which reduced the packing drag on the valve stem. The design change package did not account for the reduced packing drag and did not lower the air supply pressure to the actuator. The additional seating force and gate travel reduced the ability of the spring in the actuator to drive the valve open. This condition was alleviated by stroking the valves on a weekly basis rather than quarterly stroking frequency specified under the In Service Test program. During the period of the initial investigation all valves were stroked weekly with no failures noted. During the follow-up testing after the air pressure was reduced, half of the valves were stroked weekly while the remaining valves were returned to quarterly stroke frequency. Following two consecutive successful quarterly valve strokings all valves were returned to the quarterly test frequency. During all the initial and follow-up testing no stroke failures were noted. Following the failure identified on Saturday, October 22, 1994, System Engineering initiated a root cause investigation starting with an inspection of the air supply regulators. The air supply regulators were found to be set correctly and were eliminated as the root cause of the failures. The valves were then scheduled for testing and disassembly to inspect for stem galling or mechanical failure. As a precaution all valves were returned to the weekly stroke frequency which has resulted in 100% success rate. The disassembly of the valves did not indicate any abnormalities in the disk and seating area other than some minor scratches that would be expected for a flex wedge designed valve. The stuffing boxes were unpacked and inspected for packing order, number of packing rings, presence of lubricant and foreign material, and location of the lantern ring. No abnormal conditions were noted. The stems were inspected and deemed to be in good condition. The valve stem diameter, stuffing box dimensions, and lantern ring were measured with no abnormalities noted. The valves stroke length and actuator stroke length were measured and determined to be correct to assure proper actuator spring compression. TEXT PAGE 4 OF 5 ANALYSIS OF OCCURRENCE In conjunction with the above activities the manufacturers for the actuator (Hiller) and the valve (Anchor Darling) were contacted to determine if the actuator/valve combination were adequately designed. A conference call was conducted with representatives of Anchor Darling and Hiller to review their findings and it appears that the current design is adequate for all the valves ( 3", 4" and 6"), although the 3" design margin is smaller than the 4" and 6" valves. Anchor-Darling believes that the current packing configuration is the most probable cause for the valve stroke failures. The original valves were supplied with Crane 187I packing. The packing was replaced with Chesterton Graphfoil packing. This replacement was done on a one for one bases (nine rings of Crane were replaced with nine rings of Chesterton). The current industry standard for Graphite type packing is to use four or five ring configuration, regardless of the original number of packing rings, with a carbon bushing to make up any spacing difference. The standard packing gland torque calculations are based on a standard five ring configuration, therefore using these calculations for a large number of packing rings may give non-- conservative results. Calculations indicate that reducing the number of packing rings to four or five, can reduce the dynamic packing load by up to 50% thereby reducing the total force needed by the actuator. There has been industry experience with graphite type packing that indicates if a valve is left stationary for long periods of time (this time is not well defined), that the packing may tend to stick causing static packing loads to increase substantially. This increase in static loads may cause the total load to exceed the capability of the actuator. Additionally, industry experience has shown that a higher degree of stem finish is necessarily when using graphite packing. A contributing factor to the valve stroke failures may be attributed to the disk friction coefficient used in the original actuator sizing calculations. Testing of motor operated valves (MOV) under GL 89-10 has indicated that the valve friction coefficient used by many valve manufacturers is generally non-conservative. For an air operated valve that relies solely on spring pressure to open, a non-conservative valve factor could have a significant impact on the actuators ability to open the valve. SAFETY SIGNIFICANCE This event posed minimal safety significance. Redundant components were operable to maintain sufficient ECCS equipment operable. PREVIOUS OCCURRENCES There has been one previous event reported for this particular condition. See LER 93-006-00. TEXT PAGE 5 OF 5 APPARENT CAUSE OF OCCURRENCE Based on the initial analysis the most probable cause of the binding is packing configuration combined with the long period of time between valve stroking. Contributing factors may include a non-conservative valve friction coefficient used in calculating the actuator size, and the style of packing versus stem finish. CORRECTIVE ACTIONS Based on the available information the following corrective action are being implemented. As the root cause investigation continues further corrective actions will be implemented as appropriate: All valves in the affected population will be stroked on a weekly basis until the root cause investigation is completed and all corrective actions to assure proper valve performance are complete. The packing manufacturer will be contacted to develop a four or five ring packing configuration with appropriate gland torque values. Engineering will evaluate the need to improve the finish of the valve stems to minimize the packing drag. The actuator manufacturer will be contacted to determine whether a larger spring is required to increase capability margin. Diagnostic testing will be utilized to determine actual seating thrusts and adjust the air supply as necessary to ensure the desired seating thrust is obtained. Sincerely, R.J. Hovey General Manager - Hope Creek Operations SORC Mtg. 94-082 Recommended approval: Yes C Distribution ATTACHMENT TO 9412120191 PAGE 1 OF 1 PSE&G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Hope Creek Generating Station December 8, 1994 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Dear Sir: HOPE CREEK GENERATING STATION DOCKET NO. 50-354 UNIT NO. 1 LICENSEE EVENT REPORT 94-017-00 This Licensee Event Report is being submitted pursuant to the requirements of 10CFR 50.73(a)(2)(v). Sincerely, R.J. Hovey General Manager - Hope Creek Operations LAA/ Attachment SORC Mtg. 94-082 C Distribution The Energy People *** END OF DOCUMENT ***
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