Part 21 Report - 1995-049
. PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION IV FEBRUARY 13, 1995 Licensee/Facility: Notification: Nebraska Public Power District MR Number: 4-95-0014 Cooper 1 Date: 02/13/95 Brownville,Nebraska Senior Resident Inspector Dockets: 50-298 BWR/GE-4 Subject: UNPLANNED SHUTDOWN Reportable Event Number: N/A Discussion: At 10:40 a.m. (CST) on February 10, 1995, Nebraska Public Power District declared a Notification of Unusual Event (NOUE) after declaring three relief valves in the automatic depressurization system (ADS) inoperable. The Cooper Nuclear Station (CNS) was being restarted after an extended shutdown that began on May 25, 1994. With reactor power at approximately 5 percent and RCS pressure at 350 psig, a functional test of the ADS failed when three of six relief valves would not manually open. The NOUE was declared and a shutdown to cold conditions was initiated. The unit achieved cold shutdown and the NOUE was exited at 10:13 p.m. (CST) on February 10. The unit has eight safety relief valves. Of the eight, six are associated with the ADS function and two with the low-low set relief logic. All eight valves were replaced during the recent outage. Licensee testing confirmed the valves were inoperable due to the malfunction of the solenoid control valves in the safety relief assemblies. One of the three solenoid control valves was disassembled and it was identified that internal corrosion had caused binding of the solenoid operating mechanism. The other two control valves were not disassembled in order to preserve them for future analysis. In consultation with the control valve vendor, Target Rock Corporation, it was identified that the valves may not have been appropriately dried, following hydrostatic testing with water, at the vendor's facility. The licensee and the vendor were able to conclude that the affected defective components were isolated to the three failed relief valves. However, there may have been other defective units supplied to other licensees. The licensee will begin a significant hazards analysis process to determine reportability pursuant to 10 CFR Part 21. The Vendor Branch has been briefed on this issue for further followup. The licensee has replaced the defective solenoid control valves in the safety relief assemblies. A functional test of all valves will be reperformed when the RCS reaches 300 psig. In addition, on February 11, 1995, operations personnel were in the process of swapping trains of RHR and a motor-operated valve (MOV) failed to shut on demand. The licensee's investigation identified that the stem cap on the valve operator had threaded itself, due to vibration when the valve was operated, into the MOV casing, thus preventing the valve stem from moving. During followup of this issue, it was identified that: (1) the licensee had replaced some stem caps and the replacement caps were . REGION IV MORNING REPORT PAGE 2 FEBRUARY 13, 1995 MR Number: 4-95-0014 (cont.) not constructed to the same tolerances as were the original caps (e.g., the tolerance on the cap threads was less for the replacement caps than was used for the original caps), and (2) no actions (such as staking) had been taken by the licensee to prevent self-threading of the stem cap into the valve operator housing. The licensee has inspected the valves in the drywell and found three valves with similar problems. No inspections have been performed in other areas of the plant. The licensee is currently evaluating whether or not these inspections must be performed prior to restart of the unit. Finally, on February 11, while removing the ADS solenoid valves, the licensee noted by visual observation that one of the vacuum breakers was not fully shut. The licensee's investigation determined that the disc for this vacuum breaker was not constructed correctly in that the disc had a right angle face instead of a tapered face to allow it to seal in the valve seat properly. The licensee also noted that the disc was slightly too large, which prevented the movement of the disc inside the pipe when the temperature of the disc increased (caused by steam being relieved in the pipe). The increase in temperature caused the size of the disc to increase because of thermal expansion and caused the disc to not freely move inside the pipe. The licensee is in the process of correcting these problems. Regional Action: Region IV and NRR have been providing 24-hour per day coverage of licensee restart activities. Contact: P. H. Harrell (817)860-8250
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021