Morning Report for May 26, 2000
Headquarters Daily Report MAY 26, 2000 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS X REGION I X REGION II X REGION III X REGION IV X PRIORITY ATTENTION REQUIRED MORNING REPORT - HEADQUARTERS MAY 26, 2000 Licensee/Facility: Notification: Part 21 Database MR Number: H-00-0033 Ppg Architectural Finishes Date: 05/26/00 Subject: Part 21 - Changed formulation of coating Discussion: VENDOR: PPG Architectural Finishes NO: mm-13-0 DATE OF DOCUMENT: 04/03/00 ACCESSION NUMBER: SOURCE DOCUMENT: EN 36861 REVIEWER: REXB, V. Hodge On April 3, 2000, the coating vendor PPG Architectural Finishes reported that for small quantities of a silicon stainless steel enamel coating used inside primary containment, the formulation changed from that which was originally supplied. The vendor states that it notified the single affected nuclear power utility. On May 3, 2000, the vendor updated its report (Accession Number ML003712384). Since 1987, the vendor supplied exterior silicone stainless steel enamel coating 8674 to the Catawba, McGuire, and Oconee licensee, Duke Energy Company. The licensee used this coating inside containment on mirror-insulated piping to minimize the potential for paint chip fouling of sump pumps. In a postulated design basis accident, such fouling would interfere with the emergency core cooling systems used for recovery from the accident. The vendor stated that this product was not sold to any other nuclear utility for use in containment. In 1980, the vendor's predecessor, Keeler & Long, Inc., conducted design basis accident qualification testing on the 8674 coating, concluding that the product qualified for Coating Service Level I Exposure because it disintegrated by powdering, leaving no sizeable pieces of coating to interfere with the emergency core cooling systems. Nevertheless, the product was not included in the predecessor's quality assurance program and the formulation was thus not appropriately controlled. Subsequent testing by the licensee indicates that the original formulation and several variations of it exhibit large blisters with paint chips being delaminated from the substrate. These chips could foul sump pumps in a postulated design basis accident. The vendor states that the licensee intends to continue purchasing this product for use in containment as a non-qualified coating. The vendor states that the mirror-insulation on piping currently coated with this product should minimize the potential for paint chip fouling of sump pumps. The NRC will post ensuing reports, if any, on this subject on its website at http://www.nrc.gov/NRC/PUBLIC/PART21/2000. HEADQUARTERS MORNING REPORT PAGE 2 MAY 26, 2000 MR Number: H-00-0033 (cont.) _ REGION IV MORNING REPORT PAGE 2 MAY 26, 2000 Licensee/Facility: Notification: Nebraska Public Power District MR Number: 4-00-0015 Cooper 1 Date: 05/26/00 Brownville,Nebraska From RIs Dockets: 50-298 BWR/GE-4 Subject: EQUIPMENT QUALIFICATION DEFICIENCIES WITH OKONITE TAPED SPLICES - UPDATE Discussion: On April 10, 2000, Cooper Nuclear Station management informed the resident inspectors that drywell temperature profiles during design basis accidents may exceed their equipment qualification test temperatures. Subsequent review by the licensee determined that the overall concern with the environmental qualification of drywell equipment was bounded by existing test results, as long as all electrical splices were in the configuration bounded by the test. To help confirm the actual configuration, on April 14 a licensee electrician and the NRC's resident inspector entered the containment to inspect a sample of splices. The electrician and resident inspector observed that, for most of the Okonite splices observed, the outer tape was unraveling. A special inspection was chartered to review the circumstances surrounding these discrepancies. After comprehensive review and corrective actions, on May 26 at 9:58 a.m., operators at Cooper Nuclear Station began plant restart from the forced outage. The licensee plans to close the main output breaker early on May 27 and restore the facility to normal operation. On May 23, licensee management and technical personnel conducted a teleconference with the Regional Administrator and members of the regional and NRR staffs to discuss the plant's corrective actions and readiness to restart. Licensee personnel have replaced all taped environmentally qualified splice treatments in the drywell and steam tunnel with alternative qualified treatments. During the licensee's evaluations, certain terminal blocks were also replaced. Regional Action: The special inspection is continuing, in accordance with Inspection Procedure 93102. The inspection team reviewed the extent of the condition and the licensee's repair plans and did not identify any outstanding safety issues that affect the restart of the unit. Contact: David Loveless (817)860-8161 Wayne Sifre (817)860-8193 _
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Page Last Reviewed/Updated Wednesday, March 24, 2021