Morning Report for September 23, 1999
Headquarters Daily Report SEPTEMBER 23, 1999 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS X REGION I X REGION II X REGION III X REGION IV X PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION I SEP. 23, 1999 Licensee/Facility: Notification: Baltimore Gas & Elec Co. MR Number: 1-99-0036 Calvert Cliffs 1 Date: 09/23/99 Lusby,Maryland RI PC Dockets: 50-317 PWR/CE Subject: REACTOR TRIP Discussion: On September 22, at 9:08 a.m., Calvert Cliffs Unit 1 (CCNPP 1) was manually tripped from 100 percent power upon a loss of main feedwater. All control rods fully inserted and an auxiliary feedwater actuation signal (AFAS) occurred due to low steam generator water level. The preliminary cause was determined to be personnel error (plant electrician) during the performance of maintenance which resulted in the loss of non-vital motor control center (MCC)- 106 and MCC-116. The de-energization of these MCCs resulted in a loss of control oil to both turbine driven steam generator feed pumps (SGFP). In addition, the condenser air removal (CAR) pumps powered from MCC-106 and MCC-116 were lost, resulting in a loss of main condenser vacuum and the ability to dump steam to the main condenser. All plant equipment operated as designed during and following the shutdown. The main steam isolation valves were closed by the operators following the trip and remained closed during the event. Plant cooldown was performed by using the atmospheric dump valves and the auxiliary feedwater system. As of 8:00 a.m. this morning, the unit was in Mode 3 Hot Standby, with plans to restart this afternoon. The resident inspectors were on site and responded to the shutdown and have been monitoring licensee activities. Contact: William Cook (610)337-5074 Fred Bower (410)586-2626 _ REGION I MORNING REPORT PAGE 2 SEPTEMBER 23, 1999 Licensee/Facility: Notification: Northeast Utilities MR Number: 1-99-0038 Millstone 3 Date: 09/23/99 Waterford,Connecticut SRI/PC Dockets: 50-423 PWR/W-4-LP Subject: INOPERABLE SUMP PUMPS Discussion: During surveillance testing of two air driven safety-related pumps located in the recirculation spray system (RSS) cubicle sumps on September 22, the "A" pump failed to start. The licensee entered a technical specification (TS) action statement to shut the plant down in 3 days because a support system for the RSS was inoperable. The pump was replaced with a spare pump and tested satisfactorily. When the "A" pump was disassembled, the licensee discovered growth of the plastic rotating air blades that caused the pump to mechanically bind. Even though the "B" pump passed its surveillance test, the licensee is currently removing it for an inspection of its air blades to determine if this condition is a generic problem. The licensee exited the action statement, based upon the successful completion of surveillance testing of the replacement pumps. The function of the pumps is to remove ground water that drains from under the primary containment basemat to sumps located in the engineered safeguards features (ESF) building. However, the resultant operability concerns are not significant from an overall plant risk perspective. Factors that reduce the risk significance include the amount of time available to take compensatory measures in the event both sump pumps failed. There would be more than 65 days before the water level around the containment would rise to a level where hydrostatic forces on the containment liner would be a concern. Also, although not environmentally qualified, two non-safety-related sump pumps could be powered and provide ground water removal capability, further extending the time available to provide compensatory measures in the event the safety-related pumps failed. Additionally, since the ground water communicates in common with both sumps, it would be expected that one sump pump in operation, either the air driven or electric driven pump, would be capable of keeping both RSS cubicles dry. Regional Action: The resident inspectors and an NRC engineering team that is onsite are following licensee actions. Contact: A. Cerne (860)447-3170 James Linville (610)337-5129 _ REGION II MORNING REPORT PAGE 3 SEPTEMBER 23, 1999 Licensee/Facility: Notification: Carolina Power & Light Co. MR Number: 2-99-0014 Brunswick 1 2 Date: 09/23/99 Southport,North Carolina Dockets: 50-325,50-324 BWR/GE-4,BWR/GE-4 Subject: MANAGEMENT CHANGES Discussion: Carolina Power & Light (CP&L) announced on September 22, 1999, that Neil Gannon will become the new plant general manager at Brunswick effective September 22, 1999. This position had previously been occupied by Jeff Lyash, also the Brunswick director of site operations (DSO). Mr. Lyash will retain the position of DSO and Mr. Gannon will report to him. Mr. Gannon had been serving as operations manager at Brunswick. Regional Action: For information only. Contact: Geoffrey West (404)562-4660 _
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021