Event Notification Report for November 18, 2021

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
11/17/2021 - 11/18/2021

EVENT NUMBERS
55571 55583 55584 55586
Agreement State
Event Number: 55571
Rep Org: Texas Dept of State Health Services
Licensee: Chi St. Luke's Baylor College of Medicine Med Ctr
Region: 4
City: Houston   State: TX
County:
License #: 06661
Agreement: Y
Docket:
NRC Notified By: Randall Redd
HQ OPS Officer: Jeffrey Whited
Notification Date: 11/11/2021
Notification Time: 11:55 [ET]
Event Date: 11/09/2021
Event Time: 00:00 [CST]
Last Update Date: 11/11/2021
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
Person (Organization):
Gaddy, Vincent (R4)
NMSS_Events_Notification, (EMAIL)
Event Text
EN Revision Imported Date: 11/18/2021

EN Revision Text: AGREEMENT STATE REPORT - MEDICAL UNDERDOSAGE

The following was received from the Texas Department of State Health Services (the Agency):

"On November 10, 2021, the Agency received notification from [the Radiation Safety Officer] RSO of the licensee reporting that a yttrium-90 TheraSphere administration with an intended activity of 44.8 mCi (120 Gy) to be inserted resulted in only 18.7 mCi inserted into the patient with the remainder still in the delivery system. RSO reported the procedure was completed indicating there was no stoppage due to patient or otherwise intervention. This was 41.6 percent of the prescribed activity inserted into the patient and at present an unknown dose. The target was a tumor in the liver. A survey of the room was done with no contamination found."

Texas Incident: I-9895

A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.


Non-Power Reactor
Event Number: 55583
Facility: Univ Of Missouri-Columbia (MISC)
RX Type: 10000 Kw Tank
Comments:
Region: 0
City: Columbia   State: MO
County: Boone
License #: R-103
Agreement: N
Docket: 05000186
NRC Notified By: Bruce Meffert
HQ OPS Officer: Kerby Scales
Notification Date: 11/16/2021
Notification Time: 15:59 [ET]
Event Date: 11/15/2021
Event Time: 00:00 [CST]
Last Update Date: 11/16/2021
Emergency Class: Non Emergency
10 CFR Section:
Non-Power Reactor Event
Person (Organization):
Geoff Wertz (NRR PM)
Mike Takacs (NRR ENC)
Event Text
EN Revision Imported Date: 11/18/2021

EN Revision Text: ABNORMAL OCCURRENCE

"University Of Missouri Research Reactor (MURR) Technical Specification (TS) 6.6.c(1) requires notification to the NRC Operations Center that an Abnormal Occurrence, as defined by MURR TS 1.1, has occurred. MURR was not in compliance with one (1) of the TS Limiting Conditions of Operations. TS 3.2.g states, 'The reactor safety system and the number (N) of associated instrument channels necessary to provide the following scrams shall be operable whenever the reactor is in operation.' Specifically, the reactor safety scram function that occurs when the differential pressure across the reactor pool reflector (PT-917) instrument channel decreases below 2.52 psi minimum in Mode 1 operation was not operable as required by TS 3.2.g.10.

"On 11/15/21 while the reactor was shut down, Control Room operators shut down the pool coolant system and noticed that the `Reflector Hi-Low Diff Pressure Scram' annunciator alarm did not initiate as pool coolant flow rate decreased to zero. The Control Room operators contacted reactor management, and an investigation was initiated to prove whether or not the safety scram function from the PT-917 instrument channel actuated correctly. Further testing revealed the safety scram signal from the PT-917 instrument channel did not occur due to a failed alarm-meter unit. The alarm-meter unit was replaced with an exact spare, the PT-917 instrument channel was calibrated, and the reactor safety scram functions of the PT-917 instrument channel were retested satisfactorily.

"In accordance with TS 6.6.c(4), the Reactor Facility Director was briefed and gave permission to restart the reactor prior to the reactor returning to operation later on 11/15/21. Currently, MURR is operating at 10 MW. A detailed event report will follow within 14 days as required by MURR TS 6.6.c(3)."

The NRC Project manager was notified.


Agreement State
Event Number: 55584
Rep Org: Illinois Emergency Mgmt. Agency
Licensee: British Petroleum
Region: 3
City: Lemont   State: IL
County:
License #: 9152422
Agreement: Y
Docket:
NRC Notified By: Gary Forsee
HQ OPS Officer: Kerby Scales
Notification Date: 11/16/2021
Notification Time: 16:09 [ET]
Event Date: 11/10/2021
Event Time: 00:00 [CST]
Last Update Date: 11/16/2021
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
Person (Organization):
Orth, Steve (R3)
NMSS_Events_Notification, (EMAIL)
Event Text
EN Revision Imported Date: 11/18/2021

EN Revision Text: AGREEMENT STATE REPORT - STUCK SHUTTER

The following was received from the state of Illinois (the Agency) via email:

"The Agency was notified by British Petroleum [BP] (registered as a general licensee under the name CHICAP Pipe Line Company (9152422)), that they had discovered a stuck shutter on a generally licensed fixed gauge at their Lemont, IL location. The shutter, which is normally open, has apparently been broken for many years and was only discovered during removal last week. No personnel exposures resulted and the gauge has been secured pending disposal.

"A specifically licensed service provider was removing a generally licensed fixed gauge on 11/10/21 for planned disposal through a waste broker when it was discovered to have an inoperable shutter. The gauge was a Ronan Engineering Company model SA-1, containing 50 milliCi of Cs-137 (s/n 8333GG). While the shutter was reportedly routinely tested, the arm that moves the shutter was severely corroded. It was only during removal that the registrant discovered the shutter itself was broken. The gauge has been in service for 24 years and was installed at a 12' height with the beam projecting into the process equipment. As the shutter remains in the open position and personnel are not in the beam path, personnel exposure is not a concern. No reported exposures during removal. The gauge has been double locked with the beam facing down into the concrete floor. The shutter is being repaired so it may be properly transported and disposed of through Bionomics (waste broker). A written report detailing remedial action is required within 30 days under 32 Ill. Adm. Code 330.220(a)(3)(E).

"This incident is reportable under 32 Ill. Adm. Code 340.1220. At this time, it does not appear a response to the site by Agency staff will be required. BP's consultant indicated that the gauge manufacturer reports 3-4 of these gauges per year are returned. The issue is reportedly a seal that leaks and gives rise to corrosion - despite being used within the environmental conditions specified in the SSDR [Seal Source Device Registry]. This information is anecdotal but included for NRC's evaluation and trending analysis. This matter will remain open until confirmation of shipping for disposal is received."

Illinois Item Number: IL210037


Power Reactor
Event Number: 55586
Facility: Beaver Valley
Region: 1     State: PA
Unit: [2] [] []
RX Type: [1] W-3-LP,[2] W-3-LP
NRC Notified By: Ronald Ferrie
HQ OPS Officer: Karen Cotton
Notification Date: 11/17/2021
Notification Time: 16:24 [ET]
Event Date: 11/17/2021
Event Time: 13:13 [EST]
Last Update Date: 11/17/2021
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical
50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Deboer, Joseph (R1)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 N Y 100 Power Operation 0 Hot Standby
Event Text
MANUAL REACTOR TRIP AND AUTOMATIC AUXILIARY FEEDWATER ACTUATION

"At 1313 hours on November 17, 2021, with Unit 2 in Mode 1 at 100 percent power, the reactor was manually tripped due to a loss of the 21B Main Feedwater Pump [due to low suction pressure]. The Auxiliary Feedwater System automatically started as designed in response to the full power reactor trip. Additionally, the Main Steam Isolation Valves were manually closed to prevent excessive reactor coolant system cooldown. The trip was not complex, with all systems responding normally post-trip. There was no equipment inoperable prior to the event that contributed to the reactor trip or adversely impacted plant response. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the atmosphere using the Atmospheric Dump Valves.
"Beaver Valley Power Station Unit 1 is unaffected and remains at 100 percent power in Mode 1.

"Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, the automatic actuation of the Auxiliary Feedwater System is being reported as an eight-hour, non-emergency Specific System Actuation per 10 CFR 50.72(b)(3)(vi)(A).

"There was no impact on the health and safety of the public or plant personnel. The NRC Resident has been notified."