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Event Notification Report for November 27, 2016

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
11/26/2016 - 11/27/2016

EVENT NUMBERS
5239552396
Power Reactor
Event Number: 52395
Facility: FARLEY
Region: 2     State: AL
Unit: [1] [] []
RX Type: [1] W-3-LP,[2] W-3-LP
NRC Notified By: BLAKE MITCHELL
HQ OPS Officer: HOWIE CROUCH
Notification Date: 11/27/2016
Notification Time: 03:08 [ET]
Event Date: 11/27/2016
Event Time: 00:26 [CST]
Last Update Date: 11/27/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
Person (Organization):
JAMIE HEISSERER (R2DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 M/R Y 100 Power Operation 0 Hot Standby
Event Text
MANUAL REACTOR TRIP WITH AUTOMATIC AUXILIARY FEEDWATER SYSTEM ACTUATION DUE TO VOLTAGE OSCILLATIONS

"At 0026 [CST] on November 27, 2016, Farley Unit 1 was manually tripped from 100% reactor power due to voltage swings suspected to be caused by the Auto Voltage Regulator. All control rods fully inserted and Auxiliary Feedwater (AFW) auto-started as expected.

"All systems responded as expected. The plant is currently stable in Mode 3 (Hot Standby). The cause of the main generator voltage oscillations is under investigation.

"The NRC Resident Inspector has been notified."

The trip was uncomplicated. Decay heat is being removed via the steam dumps to condenser. The plant is at normal operating pressure and temperature with auxiliary feedwater supplying the steam generators. The electrical grid is stable and supplying plant loads. All safety equipment is available, if needed. Unit 2 was unaffected by the event and remains at 100% power.


Power Reactor
Event Number: 52396
Facility: MONTICELLO
Region: 3     State: MN
Unit: [1] [] []
RX Type: [1] GE-3
NRC Notified By: ROBERT BALDWIN
HQ OPS Officer: STEVEN VITTO
Notification Date: 11/27/2016
Notification Time: 21:22 [ET]
Event Date: 11/27/2016
Event Time: 14:47 [CST]
Last Update Date: 11/27/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(D) - ACCIDENT MITIGATION
Person (Organization):
AARON McCRAW (R3DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation
Event Text
HIGH PRESSURE COOLANT INJECTION DECLARED INOPERABLE

"At 1447 [CST] on 11/27/2016 while troubleshooting a minor leak on the High Pressure Coolant Injection (HPCI) turbine, it was discovered that the HPCI turbine exhaust drain pot high level bypass switch was not functioning per design to support removal of condensate from the HPCI turbine casing. This resulted in some water accumulation within the HPCI turbine casing. Subsequently, HPCI was declared INOPERABLE and this issue is being reported under 10CFR50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function at the time of discovery. The plant remains at 100 percent power with no challenges to the health and safety of the public. The NRC Resident Inspector has been notified."

Technical Specification limiting condition for operation requires HPCI to be Operable within 14 days. The licensee will be notifying the State of Minnesota regarding the event.