U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/28/2003 - 08/29/2003 ** EVENT NUMBERS ** | General Information or Other | Event Number: 40102 | Rep Org: ARIZONA RADIATION REGULATORY AGENCY Licensee: PHELPS-DODGE, INC. Region: 4 City: BAGHDAD State: AZ County: License #: AZ-13-005 Agreement: Y Docket: NRC Notified By: AUBREY V. GODWIN HQ OPS Officer: JOHN MacKINNON | Notification Date: 08/25/2003 Notification Time: 18:22 [EST] Event Date: 08/25/2003 Event Time: 09:30 [MST] Last Update Date: 08/25/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): MICHAEL RUNYAN (R4) E. WILLIAM BRACH (NMSS) | Event Text 3 CURIE COBALT-60 SOURCE DISCOVERED DISCONNECTED "At approximately 9:30 AM MST August 25, 2003, the Agency was informed by the Licensee that they had discovered a source had disconnected from a rod in the Process Leaching Vessel. The source contains 3 Curies of Cobalt 60 as of October 2001. The licensee has made measurements and determined the radiation levels outside the vessel are not excessive. The device is a ThermoMeasure Tech Model 5031 L SN B43. Even though the source is disconnected, because it is trapped within a sealed source guide tube, it is still secure from inadvertent removal. The estimated date for full repair is October 21, 2003. Repair will be made by the device manufacturer. The Licensee has agreed not to drain the vessel without Agency notice and approval. "The Agency continues to investigate this incident." The Agency is: ARIZONA RADIATION REGULATORY AGENCY. First Notice: 03-13 | Power Reactor | Event Number: 40110 | Facility: GRAND GULF Region: 4 State: MS Unit: [1] [ ] [ ] RX Type: [1] GE-6 NRC Notified By: MIKE BEARD HQ OPS Officer: BILL GOTT | Notification Date: 08/28/2003 Notification Time: 11:27 [EST] Event Date: 08/28/2003 Event Time: 07:50 [CDT] Last Update Date: 08/28/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): MICHAEL RUNYAN (R4) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text LOSS OF POWER TO EMRGENCY OPERATIONS FACILITY "The Emergency Operations Facility (EOF) for Grand Gulf was lost when power was removed from the facility and the EOF diesel generator failed to start. Power had to be removed due to the loss of one phase of the local power supply. Actual plant operations are not affected. The power phase problem and failure of the EOF diesel generator to start are being investigated at this time. The Backup EOF is available if needed." The licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 40111 | Facility: COOPER Region: 4 State: NE Unit: [1] [ ] [ ] RX Type: [1] GE-4 NRC Notified By: NORENA ROBINSON HQ OPS Officer: STEVE SANDIN | Notification Date: 08/28/2003 Notification Time: 12:08 [EST] Event Date: 08/28/2003 Event Time: 07:00 [CDT] Last Update Date: 08/28/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.73 - FITNESS FOR DUTY | Person (Organization): MICHAEL RUNYAN (R4) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text FITNESS FOR DUTY "At 0700 a non-licensed contract supervisor failed a for cause fitness-for-duty test. The individual tested positive for alcohol, and the results of the drug portion of the test have not yet been received. "Immediate Corrective Action: The individual's unescorted site access was denied at 0717 CST on August 28, 2003, and appropriate notifications have been completed in accordance with the station's Fitness-For-Duty Program. "Safety Significance: None. There is no reason to believe there have been any adverse consequences from this event. The employee had been cleared for unescorted access; however, had never obtained his badge for access to the protected area of the site. This event is not considered to have impacted operation of the plant in any way. "The licensee informed the NRC Resident Inspector. "Contact the Headquarters Operations Officer for additional details." | Power Reactor | Event Number: 40113 | Facility: SEQUOYAH Region: 2 State: TN Unit: [1] [ ] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: JEFF EPPERSON HQ OPS Officer: NATHAN SANFILIPPO | Notification Date: 08/28/2003 Notification Time: 17:01 [EST] Event Date: 08/28/2003 Event Time: 16:04 [EDT] Last Update Date: 08/28/2003 | Emergency Class: ALERT 10 CFR Section: 50.72(a) (1) (i) - EMERGENCY DECLARED 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): CAROLYN EVANS (R2) JAMES LYONS (NRR) NADER MAMISH (IRO) LUIS REYES (R2) TERRY REIS (NRR) BILL BORCHARDT (NRR) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | A | Y | 100 | Power Operation | 0 | Hot Standby | Event Text ALERT DECLARED DUE TO REACTOR PROTECTION SYSTEM FAILURE At 1618 EDT on 08/28/03, an Alert was declared at Sequoyah Unit 1 due to a failure of the Reactor Protection System (RPS) to auto-trip the reactor following a turbine trip. Turbine oil trip testing was in progress when at 1604, the main turbine tripped. The reactor trip breakers were opened by manual operator action approximately 20 seconds after the valid reactor trip signal. Following the trip, all systems operated as required. The main steam isolation valves were manually closed based on indication of steam flow and a throttled steam dump valve. No primary system or steam generator safety valves opened. The unit is currently stable with temperature controlled using atmospheric relief valves. The Auxiliary Feedwater System received an auto-start signal and successfully operated. All control rods were fully inserted into the core. There was no release of radioactive material. The licensee has initiated an investigation into the cause of the incident. The NRC Resident Inspector and the State of Tennessee were notified by the licensee. The NRC notified FEMA (Steiner), DOE (Morroni), USDA (Beers-Block), HHS (Williams), DHS (Glick), and DOT/EPA/NRC (Threatt). The NRC entered monitoring phase of normal mode with Region 2 in the lead at 1735 EDT. * * * UPDATE ON 08/28/03 AT 2044 EDT, KEVIN WILKES TO NATHAN SANFILIPPO * * * At 2030 EDT on 08/28/03, the licensee terminated the Alert at Sequoyah Unit 1. The reactor is stable and in Mode 3, Hot Standby. This termination is based upon containment integrity, Emergency Core Cooling System and Engineered Safety Features operability, availability of heat sink, onsite and offsite electrical system and Emergency Diesel Generator operability, radiation monitor operability, availability of technical support personnel, and activation of a forced outage recovery team. Reactor coolant samples were taken, which showed no increase in activity. The NRC notified FEMA (Austin), DOE (Morroni), USDA (Beers-Block), HHS (Hogan), DHS (Van Buskirk), and DOT/EPA/NRC (White). The NRC exited monitoring phase of normal mode at 2045 EDT. | Power Reactor | Event Number: 40114 | Facility: CATAWBA Region: 2 State: SC Unit: [1] [ ] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: MIKE LEE HQ OPS Officer: GERRY WAIG | Notification Date: 08/29/2003 Notification Time: 05:40 [EST] Event Date: 08/29/2003 Event Time: [EDT] Last Update Date: 08/29/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): CAROLYN EVANS (R2) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | A/R | Y | 95 | Power Operation | 0 | Hot Standby | Event Text CATAWBA UNIT 1 AUTOMATIC REACTOR TRIP DUE TO REACTOR PROTECTION SYSTEM ACTUATION Unit 1 tripped on Over Temperature Delta T (OTDT) protection. Channel 1 Over Temperature Delta T was in trip due to a reactor coolant hot leg temperature problem. Per Technical Specifications, this required Channel 1 OTDT to be placed in the tripped condition. Channel 2 Pressurizer pressure failed low at 0203 EDT. This input caused channel 2 Over Temperature Delta T to enter a trip condition. With 2 of 4 Over Temperature Delta T channels in the trip condition, a reactor trip signal was generated by the reactor protection system resulting in an automatic reactor trip. After the reactor trip occurred, RCS (Reactor Coolant System) letdown was lost on the chemical and volume control system due to low Pressurizer level (~17%). 1NV-1A (Reactor Coolant Letdown Isolation Valve) did not close as required. This necessitated the alignment of the excess letdown flowpath to maintain the desired Pressurizer level. ESF functions operated as designed. Auxiliary feedwater auto started and main feedwater isolated as designed. All control rods fully inserted on the reactor trip. Station service electrical systems, emergency diesel generators, and ESF equipment are available. Catawba Unit 2 was unaffected by the trip of Unit 1. The licensee has notified the NRC Resident Inspector and will be notifying state and local officials. | |