Event Notification Report for June 26, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/25/2003 - 06/26/2003 ** EVENT NUMBERS ** 39631 39951 39953 39957 39959 39960 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39631 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 03/02/2003| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 16:00[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 03/02/2003| +------------------------------------------------+EVENT TIME: 14:30[EST]| | NRC NOTIFIED BY: CHARLES PIKE |LAST UPDATE DATE: 06/26/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WALTER RODGERS R2 | |10 CFR SECTION: |DAVID AYRES R2 | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO STATE AGENCY OF EXPIRED GREEN SEA TURTLE FOUND AT | | BARRIER NET | | | | "NRC notification [is] being made due to state notification to [the] Florida | | Wildlife Commission regarding a Green Sea Turtle found dead at barrier net | | pursuant to 10 CFR 50.72(b)(2)(xi)." | | | | The turtle was found on the surface at the barrier net with no injuries or | | abnormalities except for fresh cuts common for turtles coming through pipes. | | The cause of death is unknown at this time. A necropsy is planned. | | | | The NRC Resident Inspector will be notified by the licensee. | | | | * * * UPDATE ON 3/15/03 @ 1033 EST FROM TEREZAKIS TO CROUCH * * * | | | | "On 3-15-03, a green sea turtle was retrieved from the plant's intake canal. | | The turtle was determined to be in need of rehabilitation. The injuries to | | the turtle are not causal to plant operation. Per the plant's turtle permit, | | the Florida Fish and Wildlife Conservation Commission (FWCC) was notified at | | 0920 EST. This non-emergency notification is being made pursuant to 10 CFR | | 50.72(b)(2)(xi) due to the notification of FWCC." | | | | The NRC Resident Inspector will be notified by the licensee. | | | | * * * UPDATE ON 3/19/03 AT 1222 EST FROM E. SUMNER TO RIPLEY * * * | | | | "On 03/19/03 @ 1105 hrs., one loggerhead turtle was retrieved from the | | plant's intake canal. The turtle was determined to be in need of | | rehabilitation. The injury to the turtle is not causal to plant operation. | | Per the plant's turtle permit, the Florida Fish and Wildlife Conservation | | Commission (FWCC) was notified at 1115 EST." | | | | The NRC Resident Inspector was notified. | | | | * * * UPDATED ON 3/31/03 AT 1159 EST FROM W.L. PARK TO A. COSTA * * * | | | | "On 3-31-03 [1105 EST], a loggerhead sea turtle was retrieved from the | | plant's intake canal. The turtle was determined to be in need of | | rehabilitation. The injuries to the turtle are not causal to plant | | operation. Per the plant's turtle permit, the Florida Fish and Wildlife | | Conservation Commission (FWCC) was notified at 1105 EST. This non-emergency | | notification is being made pursuant to 10 CFR 50.72(b)(2)(xi) due to the | | notification of FWCC." | | | | The NRC Resident Inspector will be notified. | | | | * * * UPDATE 1235EST ON 4/9/03 FROM ANDY TEREZAKIS TO S.SANDIN * * * | | | | "On 4-9-03, a loggerhead sea turtle was retrieved from the plant's Intake | | canal. The turtle was determined to be in need of rehabilitation. The | | injuries to the turtle are not causal to plant operation. Per the plant's | | turtle permit, the Florida Fish and Wildlife Conservation Commission (FWCC) | | was notified at 1100 EST. This non-emergency notification is being made | | pursuant to 10CFR50.72(b)(2)(xi) due to the notification of FWCC." | | | | The licensee informed the NRC resident inspector. Notified R2DO(Landis). | | | | *** UPDATE ON 5/2/03 AT 1826 FROM S. OEHRLE TO A. COSTA *** | | | | "On 5/2/03, a green sea turtle was retrieved from the intake canal. The | | turtle required rehabilitation. The injuries were not causal to plant | | operation. Per the plant's turtle permit, the Florida Fish and Wildlife | | Conservation Commission was notified at 1445 EDT. This non-emergency | | notification is being made pursuant to 10 CFR 50.72 (b)(2)(xi) due to | | offsite notification." | | | | The Licensee will notify the NRC Resident Inspector. Notified R2DO | | (Munday). | | | | **** update on 05/24/03 at 1417 EDT FROM JOE HESSLING TO JOHN MACKINNON | | **** | | | | "On 5-24-03, a loggerhead sea turtle was retrieved from the plant's intake | | canal. The turtle was determined to be in need of rehabilitation. The | | turtle was very underweight and lethargic, no injuries or anomalies noted. | | Turtle's condition is not causal to plant operation. Per the plant's turtle | | permit the Florida Fish and Wildlife Conservation Commission (FWCC) was | | notified at 1345 EDT. This non-emergency notification is being made | | pursuant to 10 CFR 50.72(b)(2)(xi) due to the notification of FWCC. NRC R2DO | | (TOM DECKER) notified. | | | | The NRC Resident Inspector was by notified of this event by the licensee. | | | | ****UPDATE ON 5/27/03 AT 10:49 FROM HESSLING TO LAURA**** | | | | "On 5-27-03, a loggerhead sea turtle was retrieved from the plant's intake | | canal. The turtle was determined to be in need of rehabilitation. The turtle | | was underweight, and missing lower posterior marginals on left side. | | Turtle's injuries are not causal to plant operation. Per the plant's turtle | | permit, the Florida Fish and Wildlife Conservation Commission (FWCC) was | | notified at 0850 EDT. This non-emergency notification is being made pursuant | | to 10 CFR 50.72(b)(2)(xi) due to the notification of FWCC." | | | | Notified R2DO (T. Decker) | | | | * * * UPDATE ON 06/17/03 AT 12:45 EDT FROM CALVIN WARD TO ARLON COSTA * * * | | | | "At approximately 12:45 p.m. on 6/17/03 a loggerhead turtle was rescued from | | the St. Lucie Plant intake canal. The turtle was injured and will be | | transported to the State authorized sea turtle rehabilitation facility. The | | Florida Dept. of Environmental Protection (FDEP) was notified at 1:09 p.m. | | as required by the St. Lucie Plant Sea Turtle Permit - see the attached sea | | turtle stranding report (1 page). | | | | "Notification to the state government agency requires a four (4) Hr. | | Non-Emergency Notification to the NRC per 10 CFR 50.72(b)(2)(xi). There were | | no unusual plant evolutions in progress which may have contributed to this | | event." | | | | The licensee notified the NRC Resident Inspector. | | | | Notified R2DO (L. Wert). | | | | * * * UPDATE 0605 EDT ON 6/26/03 FROM STEVE MERRILL TO S. SANDIN * * * | | | | The licensee was informed by the FWCC that the green sea turtle requiring | | rehabilitation which was retrieved from the plant's intake canal on 3/15/03 | | had expired within 10 days of removal. Consequently, the licensee is | | updating their 3/15/03 report to include this additional information. The | | licensee will inform the NRC Resident Inspector. Notified R2DO(C. Ogle). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39951 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SC DIV OF HEALTH & ENV CONTROL |NOTIFICATION DATE: 06/20/2003| |LICENSEE: GEO-SYSTEMS DESIGN & TESTING, INC. |NOTIFICATION TIME: 13:42[EDT]| | CITY: NEWBERRY REGION: 2 |EVENT DATE: 06/20/2003| | COUNTY: STATE: SC |EVENT TIME: [EDT]| |LICENSE#: 412 AGREEMENT: Y |LAST UPDATE DATE: 06/20/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LEONARD WERT R2 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM PETERSON | | | HQ OPS OFFICER: HOWIE CROUCH | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT | | | | The following information was received from South Carolina Department of | | Health and Environmental Control via facsimile: | | | | "The SC Department of Health and Environmental Control was notified on June | | 20, 2003, by a representative from Geo-Systems Design and Testing, that a | | portable gauging device had been run over by a construction vehicle at a | | construction work site. The gauge is a Campbell Pacific Nuclear model 131 | | containing 10 [milliCuries] of cesium-137 and 50 [milliCuries] of Am-241:Be. | | The licensee is maintaining constant surveillance of the damaged gauge. The | | extent of damage at this time is unknown but the licensee has indicated the | | gauge is crushed. State inspectors are responding at this time and are | | traveling to the scene. Updates to this event will be made through the | | national NMED system." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39953 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NEW MEXICO RAD CONTROL PROGRAM |NOTIFICATION DATE: 06/20/2003| |LICENSEE: TERACON |NOTIFICATION TIME: 17:50[EDT]| | CITY: LENEXA REGION: 4 |EVENT DATE: 06/20/2003| | COUNTY: STATE: KS |EVENT TIME: 11:00[CDT]| |LICENSE#: DM346 AGREEMENT: Y |LAST UPDATE DATE: 06/20/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DALE POWERS R4 | | |C.W. (BILL) REAMER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: BILL FLOYD | | | HQ OPS OFFICER: HOWIE CROUCH | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - STOLEN MOISTURE DENSITY GAUGE | | | | The following information was obtained from the New Mexico Radiation Control | | Bureau: | | | | At 1750 EDT on 06/20/03, the Program Manager of New Mexico's Radiation | | Control Bureau reported a stolen Troxler Moisture Density Gauge (10 | | milli-curies CS-137 and 44 milli-curies Am-241). The licensee's employee | | reported that the gauge was in a box and chained to his truck at 2100 CDT | | last night, 06/19/03. Today, 06/20/03, at 1100 CDT when the employee | | reached the worksite in Ruidoso, NM, the gauge was missing. Apparently the | | chain had been moved enough to open the box. The licensee is Teracon, | | Lenexa, KS. The licensee was advised to report the incident to local law | | enforcement. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39957 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ILLINOIS DEPT OF NUCLEAR SAFETY |NOTIFICATION DATE: 06/23/2003| |LICENSEE: GOOD SHEPHERD HOSPITAL |NOTIFICATION TIME: 17:26[EDT]| | CITY: BARRINGTON REGION: 3 |EVENT DATE: 06/17/2003| | COUNTY: STATE: IL |EVENT TIME: [CDT]| |LICENSE#: IL-01620-01 AGREEMENT: Y |LAST UPDATE DATE: 06/23/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PATRICK LOUDEN R3 | | |C.W. (BILL) REAMER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DAREN PERRERO | | | HQ OPS OFFICER: ARLON COSTA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT- WRONG PATIENT SELECTED | | | | "Today, June 23, 2003, a consultant to Good Shepherd Hospital (IL-01620-01) | | in Barrington, IL called concerning a reportable medical event [discovery | | date 06/20/2003]. On June 17th the licensee was scheduled to provide a | | therapeutic dose of 15 milliCi [milliCuries] of I-131 to a patient by | | capsule. Instead, the patient received a capsule with an assayed dose of | | 10.8 milliCi. Apparently, two treatments were scheduled for the day and a | | second patient was prescribed a dose of 11 milliCi and the technician failed | | to administer the correct dose to the patient. The second patient did not | | receive any treatment that day and was rescheduled for last Friday. (A | | separate call to the pharmacy confirmed two doses were delivered on Tuesday, | | one of 15 milliCi and a second [dose] of 11 milliCi and another dose of 10 | | milliCi was provided on Friday.) | | | | "At this time, the radiation oncologist does not believe there will be any | | appreciable effect to the patient, but will continue to follow through with | | the evaluation to determine if an additional dose is necessary to achieve | | the optimal results. The licensee has advised the referring physician | | verbally and in writing. They have determined it would not be appropriate | | to notify the patient[s] given their condition and medical situation. | | | | "The licensee has spoken with the responsible technician about ensuring the | | correct dose is administered to the correct patient. The licensee is in the | | process of changes procedures at the site so that two individuals must | | independently confirm the correct patient identification and dosage | | information immediately prior to administration. | | | | "The licensee was advised as the need for timely reporting or these events | | and that a formal report must be filed within 15 days as per 32 Ill. Adm. | | Code 335.1080." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39959 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HADDAM NECK REGION: 1 |NOTIFICATION DATE: 06/25/2003| | UNIT: [1] [] [] STATE: CT |NOTIFICATION TIME: 14:27[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 06/25/2003| +------------------------------------------------+EVENT TIME: 13:24[EDT]| | NRC NOTIFIED BY: JOHN BOWER |LAST UPDATE DATE: 06/25/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KENNETH JENISON R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SMALL OIL SPILL AT HADDAM NECK PROMPTS OFFSITE NOTIFICATION | | | | The licensee reported an offsite notification to the Connecticut Department | | of Environmental Protection concerning a 1 pint oil spill. Apparently, a | | hydraulic hose on a forklift failed and spilled oil onto the dirt. The | | licensee indicated they will clean-up the oil spill. | | | | Notified R1DO (K. Jenison) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39960 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: THREE MILE ISLAND REGION: 1 |NOTIFICATION DATE: 06/25/2003| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 19:45[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP |EVENT DATE: 06/25/2003| +------------------------------------------------+EVENT TIME: 14:30[EDT]| | NRC NOTIFIED BY: JOHN SCHORK |LAST UPDATE DATE: 06/25/2003| | HQ OPS OFFICER: JAMES DODSON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KENNETH JENISON R1 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANALYZED CONDITION DUE TO DISLODGED ACCESS PANEL IN THE CONTROL BUILDING | | VENTILATION SYSTEM | | | | "An access panel cover for the Control Building Ventilation System supply | | duct was found to be dislodged on June 24, 2003. The access panel was | | immediately realigned upon discovery of the condition and secured. The | | probable cause of the event is that vibration of the ductwork caused the | | panel closure camlocks to vibrate from a closed position to an open | | position. A walkdown is being performed to ensure that other access panels | | are secure. The corrective action to this event will address additional | | actions to ensure these closure camlocks and other similar camlocks are | | positively secured to prevent an event recurrence. | | | | "The review of the potential impact of this system configuration determined | | on June 25, 2003 that conditions may have existed as defined in 10 CFR | | 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D) and that the event requires | | reporting. On Tuesday, June 25, 2003, further Engineering evaluation | | determined that the dislodged panel access cover for the Control Building | | Ventilation System may have reduced the systems capability to maintain a | | positive pressure in the Control Building Habitability Envelope. This | | condition could have lead to increased unfiltered in-leakage of airborne | | radioactive material beyond the previously analyzed condition in the event | | of a design basis accident. Further analysis may determine that the system | | would have been able to perform its design basis function. | | | | "The NRC Resident Inspector has been notified. No other state, local or | | other government agencies have been notified. There has been no media press | | release issued." | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021