Event Notification Report for April 14, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/11/2003 - 04/14/2003 ** EVENT NUMBERS ** 39749 39750 39751 39752 39753 39754 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39749 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 04/11/2003| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 06:23[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 04/11/2003| +------------------------------------------------+EVENT TIME: 01:45[CDT]| | NRC NOTIFIED BY: PAT RYAN |LAST UPDATE DATE: 04/11/2003| | HQ OPS OFFICER: ARLON COSTA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MICHAEL PARKER R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 30 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO VIBRATIONS ON THE MAIN TURBINE | | | | "A manual scram was initiated at 0145 on April 11, 2003, due to vibrations | | on the Main Turbine trending up to the trip setpoint. A scheduled plant | | shutdown was in progress for a maintenance outage [of the 'B' recirculation | | flow control valve sensor]. All plant systems operated normally on the | | scram. The plant is shutdown at 0% power in Mode 3. The turbine vibrations | | returned to normal values after the turbine tripped." | | | | All rods inserted normally. All safety and electrical systems operated as | | designed during and after the reactor trip. The plant is stable and using | | normal feedwater. There was nothing unusual or not understood. | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39750 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DAVIS BESSE REGION: 3 |NOTIFICATION DATE: 04/11/2003| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 17:17[EDT]| | RXTYPE: [1] B&W-R-LP |EVENT DATE: 04/11/2003| +------------------------------------------------+EVENT TIME: 17:00[EDT]| | NRC NOTIFIED BY: LARRY MYERS |LAST UPDATE DATE: 04/11/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MICHAEL PARKER R3 | |10 CFR SECTION: |GENE IMBRO NRR | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANALYZED CONDITION COULD CAUSE HIGH PRESSURE INJECTION PUMP DAMAGE | | | | "As a result of an in-depth design and performance capability review, a | | non-conforming condition was identified whereby, utilizing only safety grade | | equipment, long term cyclic repressurizations of the reactor coolant system | | (RCS) may occur following a subset of postulated very small Loss of Coolant | | Accidents (LOCAs) with effective break sizes in a range between 0.0021 ft2 | | to 0.0045 ft2. The repressurization cycles were not previously analyzed, | | but are predicted by a new application of the license basis 10 CFR 50.46 | | Evaluation Model. Although non-safety grade equipment would be available to | | prevent repressurizatons, if only safety grade LOCA mitigating equipment is | | credited, these repressurizazion cycles could be postulated to damage both | | High Pressure Injection (HPI) pumps. This could occur due to pump | | deadheading after HPI recirculation flow back to the borated water storage | | tank is procedurally isolated upon tank low level and pump suction has been | | manually transferred to the containment emergency sump at minimum of | | approximately 20 hours into the postulated event. Minimum recirculation | | flow back to the borated water storage tank initially provided protection | | against deadheading the pump and previously assumed reactor coolant system | | pressures would have allowed continued HPI pump flow. During part of the | | newly predicted repressurization cycle, RCS pressure would exceed the | | shutoff head of the HPI pumps. Without minimum flow, the pumps would be | | damaged. | | | | "This issue is currently evaluated by Condition Report 02-06702. | | Davis-Besse has determined this condition is reportable under � | | 50.72(b)(3)(ii)(B) 'Any event or condition that results in ..'The nuclear | | power plant being in an unanalyzed condition that significantly degrades | | plant safety.' Although the plant is currently in cold shutdown and the HPI | | pumps are not required to be operable per the Technical Specifications, this | | issue represents a historical condition that existed within the last three | | years." | | | | The licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 39751 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WESTINGHOUSE ELECTRIC CORPORATION |NOTIFICATION DATE: 04/12/2003| | RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 17:02[EDT]| | COMMENTS: LEU CONVERSION (UF6 to UO2) |EVENT DATE: 04/11/2003| | COMMERCIAL LWR FUEL |EVENT TIME: 18:30[EDT]| | |LAST UPDATE DATE: 04/12/2003| | CITY: COLUMBIA REGION: 2 +-----------------------------+ | COUNTY: RICHLAND STATE: SC |PERSON ORGANIZATION | |LICENSE#: SNM-1107 AGREEMENT: Y |BRIAN BONSER R2 | | DOCKET: 07001151 |JANET SCHLUETER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CARL SNYDER | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF DOUBLE CONTINGENCY PROTECTION | | | | NRC BULLETIN 91-01 24 HOUR NOTIFICATION | | | | Westinghouse Electric Company, Commercial Fuel Fabrication Facility, | | Columbia SC, low enriched (less than or equal to 5.0 wt. % U-235) PWR fuel | | fabricator for commercial light water reactors. License: SNM-1107. | | | | Time and Date of Event: 18:30 hours, April 11, 2003. | | | | Reason for Notification: | | | | On March 19, 2003, six UF6 cylinders were placed on hold because | | Westinghouse questioned if the cylinders were properly tested following | | repair. The ANSI N14.1 nameplate had been removed from supporting "feet" | | and-welded directly onto the pressure vessel dome. The "U" Stamp had been | | replaced with an "R" Stamp and documentation from the shipper indicated that | | the fillet weld on the dome had undergone dye-penetrant testing. The UF6 | | cylinder pressure vessel, however, had not undergone hydrostatic testing. | | | | The "hold" consisted of a flag in the UF6 cylinder tracking computer | | database, which was inserted as a manual edit. The hold flag should have | | prevented the cylinders from being transferred into work in process (WIP) to | | allow processing. On March 31, 2003 one of the six cylinders was allowed | | by the tracking database to be processed. A second cylinder with the hold | | flag was allowed to be processed on April 1, 2003. | | | | Unaware of the failure of the hold flags, the safety analysis proceeded. On | | April 10, 2003 NCS and process engineering completed the safety review begun | | on March 19, 2003 of the nameplate welding using applicable pressure vessel | | standards including an on-site interview with a certified boiler code | | inspector. The conclusion of the safety review was that the "R" Stamp | | cylinders met the ANSI N 14.1 requirements and were acceptable for | | processing. | | | | On April 11, 2003, NCS began a review of the sequence of events leading to | | the processing of the two hold tagged cylinders. At approximately 18:30 | | hours April 11, 2003 NCS completed its final interview. Shortly thereafter, | | it was determined that there had been a loss of previously documented | | double contingency protection. NCS immediately informed the EH&S manager of | | the event. | | | | Double Contingency Protection: | | | | The parameters that directly affect neutron multiplication for the | | vaporizers are mass (density) and geometry (level control). A criticality | | could be possible in a vaporizer under the following conditions: | | | | Sufficient material is discharged from the cylinder into the vaporizer in | | order to form a critical UO2F2 H2O density (optimum moderation), and water | | slab height increases to a critical height. | | | | Cylinder integrity maintains mass control. The U235 mass control depends | | upon maintaining the structural integrity of the cylinder to ensure that no | | material is released due to a sudden uncontrollable rupture. | | | | The geometry control consists of ensuring that condensate drains properly | | from the vaporizer, and detecting water accumulation should it occur. | | | | It has been determined that less than previously documented double | | contingency protection remained for the system and that greater than a safe | | mass was involved. Double Contingency protection was restored within 4 | | hours. In accordance with Westinghouse Operating License (SNM-1107), | | paragraph 3.7.3 (c.5b), this event satisfies the criterion for a 24-hour | | notification. | | | | As Found Condition: | | | | See "Reason for Notification." As detailed above, the Investigation found | | that the cylinders were safe to process. In fact, there never was an actual | | safety issue. The event did point out a weakness in our control of UF6 | | cylinders that will be addressed. | | | | Summary of Activity: | | | | 1) The four remaining cylinders were physically tagged out. | | 2) A complete inventory and inspection of all cylinders on-site was | | performed. | | 3) It was verified that no movement of UF6 cylinders onto the site or into | | processing will occur for the next week. | | | | Conclusions: | | | | 1) Loss of double contingency protection occurred. Greater than a safe mass | | was involved. | | 2) At no time was the health or safety to any employee or member of the | | public in jeopardy. No exposure to hazardous material was involved. | | 3)The Incident Review Committee (IRC) determined that this is a safety | | significant incident in accordance with governing procedures. | | 4) Notification was the result of an event, not a deficient NCS analysis. | | 5) A causal analysis will be performed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39752 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 04/12/2003| | UNIT: [2] [] [] STATE: PA |NOTIFICATION TIME: 20:55[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 04/12/2003| +------------------------------------------------+EVENT TIME: 18:47[EDT]| | NRC NOTIFIED BY: STEVEN SULLIVAN |LAST UPDATE DATE: 04/12/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAMES TRAPP R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM- ALL RODS FULLY INSERTED | | | | At 1847 hours on 04/12/03 the Peach Bottom Atomic Power Station Unit 2 | | experienced an automatic reactor scram and shutdown following an air line | | failure which resulted in the closure of the "D" outboard main steam line | | isolation valve. The closure of this valve resulted in a Reactor High | | Pressure Automatic Scram Signal. This caused a actuation of the Alternate | | Rod Insertion system on reactor high pressure of 1106 psi. All rods fully | | inserted. Additionally reactor vessel water level lowered to approximately | | negative 10 inches which resulted in a RPS and PCIS Group 2 & 3 | | isolations. All systems activated as required. The outage control center is | | currently staffed and repair/planning and restart preparation activities are | | in progress. Peach Bottom Atomic Power Station Unit 2 plant conditions are | | currently stable. | | | | A copper air line going to the solenoid valve which operated the "D" | | outboard main steam isolation valve failed. Cause of the line failure is | | unknown at this time. The offsite electrical grid is stable and all | | emergency core cooling systems are fully operable if needed. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39753 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 04/12/2003| | UNIT: [] [2] [] STATE: TN |NOTIFICATION TIME: 23:50[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/12/2003| +------------------------------------------------+EVENT TIME: 22:21[EDT]| | NRC NOTIFIED BY: MITCHEL TAGGART |LAST UPDATE DATE: 04/13/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRIAN BONSER R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TURBINE TRIP CAUSES REACTOR TRIP AT SEQOUYAH UNIT 2 | | | | "While resetting a turbine trip supervisory module, the unit 2 turbine | | tripped from "Turbine High Vibration Turbine Trip" at 22:21. The reactor | | tripped as a result of the turbine trip. Investigation is pending concerning | | the turbine vibration equipment. | | | | "Auxiliary feed water system initiated as designed. All secondary plant | | equipment performed as expected. | | | | "The plant is being maintained in Mode 3 at NOT/NOP, 547 degrees F and 2235 | | psig, with auxiliary feed water supplying the Steam Generators and steam | | dumps removing the decay heat." | | | | All control rods inserted into the core with no problems. The NRC Resident | | Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39754 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 04/13/2003| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 19:06[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/13/2003| +------------------------------------------------+EVENT TIME: 16:56[CDT]| | NRC NOTIFIED BY: RON GIBBS |LAST UPDATE DATE: 04/13/2003| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVID LOVELESS R4 | |10 CFR SECTION: | | |ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR VESSEL BOTTOM HEAD DEGRADED CONDITION | | | | "On 4/12/2003, during the Unit 1 11th (1RE11) refueling outage, an | | inspection was performed of the vessel bottom head. This bare metal | | inspection identified a potential leak indication at the head to penetration | | interface for Bottom Mounted Instrumentation (BMI) penetrations 1 and 46. | | There was a small amount of residue around the outer circumference of the | | BMI penetrations. No wastage was observed. Samples of the residue were taken | | and the area was cleaned with demineralized water. Chemical sample results | | available as of 1300 on 4/13/2003 are not conclusive; however, they have | | confirmed that the residue found at the Penetration 46 contains boron, | | indicating that this could be an RCS leak. The residue removed from | | Penetration 1 was characterized as 'gummy' and its composition is still | | under investigation. Additional exams are planned to confirm the likely | | origin of the residue and to determine the scope of any repairs. There has | | been no indication of RCS leakage observed at the BMI penetrations during | | previous operational cycles. This notification is being made in accordance | | with 10 CFR 50.72(b)(3)(ii)(A)." | | | | Unit 1 will remain in mode 5 until appropriate corrective actions are | | identified. The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021