The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for October 15, 2002



                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           10/11/2002 - 10/15/2002

                              ** EVENT NUMBERS **

39250  39261  39269  39270  39271  39272  39274  39275  39276  39277  39278  39279 
39280  39281  39282  39283  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39250       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: VERMONT YANKEE           REGION:  1  |NOTIFICATION DATE: 10/06/2002|
|    UNIT:  [1] [] []                 STATE:  VT |NOTIFICATION TIME: 18:00[EDT]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        10/06/2002|
+------------------------------------------------+EVENT TIME:        11:30[EDT]|
| NRC NOTIFIED BY:  MITCH McCLUSKIE              |LAST UPDATE DATE:  10/11/2002|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |PETE ESELGROTH       R1      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| RCIC SYSTEM DECLARED INOPERABLE                                              |
|                                                                              |
| Following reactor core isolation cooling system injection check valve        |
| surveillance, the check valve apparently did not fully close.  This resulted |
| in high pump suction pressure trip which would have prevented further system |
| operation.  The licensee conservatively declared the RCIC system inoperable  |
| and entered Tech Spec LCO 3.5.G.2, a 14 day action statement.  Shortly       |
| afterwards the plant pressure was dropped to less than 150 psig as part of   |
| normal plant shutdown to refueling, this takes the plant out of the Tech     |
| Spec action statement as it no longer applies.  The licensee is conducting   |
| an investigation of the problem with RCIC injection check valve.  Repairs    |
| will be completed prior to plant restart.                                    |
|                                                                              |
| The licensee notified the NRC Resident Inspector and the State of Vermont.   |
|                                                                              |
| * * * RETRACTION FROM Andy Wisniewski on 10/11/02 at 1428 EDT to Gerry Waig  |
| * * *                                                                        |
|                                                                              |
| "BASIS FOR RETRACTION:                                                       |
|                                                                              |
| NRC Event Notification 39250 was made with the concern that this condition   |
| may have rendered the Reactor Core Isolation Cooling (RCIC) system           |
| inoperable due to a 'high pump suction pressure trip'. The RCIC pump does    |
| not have this aforementioned trip device. Therefore, the predicament that    |
| Operations has been confronted with for declaring the RCIC system inoperable |
| may be more aptly stated as; 'Could the leakage that occurred past the       |
| discharge check valve, after the RCIC system run, have over-pressurized the  |
| RCIC system suction piping and caused the system to be unavailable for       |
| service if called upon for a 'Loss of All AC Event'. A team of engineers was |
| assembled to determine the extent of this condition that resulted in the     |
| completion of an Operability Determination on 10/08/02 by the RCIC System    |
| Engineer, concluding that the RCIC system remained operable based upon the   |
| following two facts:                                                         |
|                                                                              |
| 1. The RCIC suction line relief valve lifts at 150 psi.                      |
| 2. The outer pump discharge valve, combined with a pressure switch, provides |
| an additional barrier of defense. The pressure switch actuates at 74 psi and |
| causes the RCIC PUMP SUCT PRESS HI alarm in the control room. The alarm      |
| response procedure directs operators to close the isolation valve that is    |
| downstream of the discharge check valve.                                     |
|                                                                              |
| "Additionally, the leakage has been determined to be 'slight' and well       |
| within the capacity of the relief valve, based upon system performance and   |
| observation of the event as it occurred. The RCIC system would have          |
| performed it's specified safety function during this condition if required.  |
|                                                                              |
| "Therefore, ENS Event Number 39250, made on 10/06/02, is being retracted."   |
|                                                                              |
| The licensee notified the NRC Resident Inspector of this retraction. The     |
| R1DO (John White) was notified by the NRC Headquarters Operations Officer.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   39261       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  ILLINOIS DEPT OF NUCLEAR SAFETY      |NOTIFICATION DATE: 10/09/2002|
|LICENSEE:  HARRY W. KUHN, INC.                  |NOTIFICATION TIME: 11:33[EDT]|
|    CITY:  CHICAGO                  REGION:  3  |EVENT DATE:        10/08/2002|
|  COUNTY:                            STATE:  IL |EVENT TIME:        07:30[CDT]|
|LICENSE#:  IL-01870-01           AGREEMENT:  Y  |LAST UPDATE DATE:  10/09/2002|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHRIS MILLER         R3      |
|                                                |DOUG BROADDUS        NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  TOM SEIF                     |                             |
|  HQ OPS OFFICER:  MIKE RIPLEY                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT INVOLVING LOST TROXLER GAUGE                          |
|                                                                              |
| At 1133 EDT, the Illinois Dept. of Nuclear Safety (IDNS) reported that a     |
| materials licensee reported that a Troxler Gauge (Model 3440, S/N 24468 with |
| 8 millicuries Cesium-137 and 40 millicuries Americium-241) was lost from the |
| back of a pickup truck while being transported between 7:30 am and 8:00 am   |
| on 10/8/02.  The licensee reported that the worker picked up the gauge at    |
| the licensee's facility, then drove to his residence, and then returned to   |
| the licensee's office where he found the gauge missing from the back of the  |
| pickup truck.  The worker reported to the RSO that the chain and lock for    |
| the gauge was lost the previous day (10/7/02).  The licensee stated the      |
| cause for the loss to be a failure to secure the gauge in the truck.  The    |
| licensee and IDNS personnel re-traced the route twice and did not find the   |
| gauge.  The licensee notified the police departments for the cities of West  |
| Chicago, Naperville, and Warrenville, IL, NRC Region 3,  Troxler, Inc and    |
| the Illinois Department of Transportation.                                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39269       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 10/11/2002|
|    UNIT:  [1] [] []                 STATE:  FL |NOTIFICATION TIME: 11:03[EDT]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        10/11/2002|
+------------------------------------------------+EVENT TIME:        09:25[EDT]|
| NRC NOTIFIED BY:  JOE HASSLING                 |LAST UPDATE DATE:  10/11/2002|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |GEORGE MacDONALD             |
|10 CFR SECTION:                                 |                             |
|NINF                     INFORMATION ONLY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| CHLORINE RELEASE IN TURBINE GENERATOR BUILDING                               |
|                                                                              |
| "At 0925 EDT, a release of chlorine gas was noted from the hypochlorite      |
| area, and smell of chlorine gas was noted in the Turbine Generator Building. |
| All personnel were evacuated from the Turbine Generator Building as a        |
| precautionary measure, and personnel were dispatched to determine the        |
| concentration of chlorine gas.                                               |
|                                                                              |
| "All the site of the source, chlorine gas concentration was 3ppm. Per the    |
| MSDS, the IDLH limit is 30 ppm. No Emergency Action Levels were entered.     |
| Additional samples are being taken in the Turbine Generator building prior   |
| to allowing unrestricted access into the area.  Both Unit's Control Rooms    |
| were placed in the recirculation mode as a precautionary measure as well.    |
|                                                                              |
| "There were no injuries from this event.                                     |
|                                                                              |
| "The leak has been stopped."                                                 |
|                                                                              |
| The chlorine gas was generated while acid cleaning the hypochlorite lines    |
| with muriatic acid. The acid caused the chlorine to come out as a gas. The   |
| lines are cleaned periodically to remove the calcium buildup on the lines.   |
| The licensee is investigating why chlorine gas was released this time when   |
| it was not released when the lines were cleaned in the past.  The licensee   |
| surmised that they may  have used a stronger concentration of muriatic acid  |
| this time.                                                                   |
|                                                                              |
| The NRC Resident Inspector was notified of this information call by the      |
| licensee.                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   39270       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  US DEPT OF AGRICULTURE               |NOTIFICATION DATE: 10/11/2002|
|LICENSEE:  US DEPT OF AGRICULTURE               |NOTIFICATION TIME: 14:15[EDT]|
|    CITY:  BELTSVILLE               REGION:  1  |EVENT DATE:        10/02/2002|
|  COUNTY:                            STATE:  MD |EVENT TIME:             [EDT]|
|LICENSE#:  1900915-03            AGREEMENT:  Y  |LAST UPDATE DATE:  10/11/2002|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JOHN WHITE           R1      |
|                                                |FRED BROWN           NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  DANIEL SHARP                 |                             |
|  HQ OPS OFFICER:  MIKE RIPLEY                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|BLO1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TROXLER GAUGE MISSING WHILE IN SHIPMENT                                      |
|                                                                              |
| On 10/10/2002, the licensee received notification from FedEx that their      |
| Troxler Gauge (Model No. 3321, Serial No. 446 with 10 millicuries Americium  |
| 241) could not be located.  The gauge was being shipped via FedEx from       |
| Colorado on 10/2/2002 for arrival in California on 10/4/2002.  FedEx stated  |
| that the last confirmed location was in FedEx's Denver facility, but did not |
| know exactly when it was lost.  FedEx stated that the shipping container     |
| handle with attached shipping papers had come loose from the container and   |
| was found on their conveyor belt, but not the container itself.  FedEx is    |
| continuing to locate the gauge.  The licensee has not made any other         |
| notifications.                                                               |
|                                                                              |
| Contacted R1 DO (John White) and NMSS (Fred Brown)                           |
|                                                                              |
| * * * UPDATE ON 10/11/02 AT 1608 EDT FROM DANIEL SHARP TO MIKE RIPLEY * * *  |
|                                                                              |
| Mr. Sharp reported that the missing Troxler gauge was located by the         |
| shipper, Fed Ex , in Memphis, TN. Fed Ex will resend the gauge to the        |
| intended recipient.                                                          |
|                                                                              |
| Notified R1DO (John White) and NMSS (John Hickey)                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   39271       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  QUEENS MEDICAL CENTER                |NOTIFICATION DATE: 10/11/2002|
|LICENSEE:  QUEENS MEDICAL CENTER                |NOTIFICATION TIME: 16:32[EDT]|
|    CITY:  HONOLULU                 REGION:  4  |EVENT DATE:        10/09/2002|
|  COUNTY:  HONOLULU                  STATE:  HI |EVENT TIME:        13:00[HST]|
|LICENSE#:  53-16533-02           AGREEMENT:  N  |LAST UPDATE DATE:  10/11/2002|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |KRISS KENNEDY        R4      |
|                                                |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  SCOTT DUBE                   |                             |
|  HQ OPS OFFICER:  GERRY WAIG                   |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|LADM 35.33               MED MISADMINISTRATION  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MEDICAL MISADMINISTRATION: BRACHYTHERAPY UNDERDOSE TO TREATMENT SITE         |
|                                                                              |
| A patient undergoing brachytherapy treatment for cardiac restenosis received |
| an underdose when it was determined that the strontium 90 source did not     |
| reach the intended treatment site. The source contained 16 source beads in   |
| the source train. The cause of the under dose is suspected to have been      |
| caused by blockage along the catheter but this has not yet been confirmed.   |
| An investigation will be conducted to determine the cause of the underdose.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   39272       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  C&D TECHNOLOGIES, INC.               |NOTIFICATION DATE: 10/11/2002|
|LICENSEE:  C&D TECHNOLOGIES, INC.               |NOTIFICATION TIME: 17:15[EDT]|
|    CITY:  BLUE BELL                REGION:  1  |EVENT DATE:        10/11/2002|
|  COUNTY:                            STATE:  PA |EVENT TIME:             [EDT]|
|LICENSE#:                        AGREEMENT:  N  |LAST UPDATE DATE:  10/11/2002|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JOHN MADERA          R3      |
|                                                |WILLIAM BECKNER      NRR     |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  TERRY KANDEN                 |                             |
|  HQ OPS OFFICER:  GERRY WAIG                   |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|CCCC 21.21               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PART 21 DEFECT/NONCOMPLIANCE IDENTIFIED IN NOT-YET-INSTALLED BATTERY RACKS   |
| AT PRAIRIE ISLAND                                                            |
|                                                                              |
| "In accordance with NSP's purchase order requirements and 10CFR21, I am      |
| notifying you that C&D Technologies, Inc. has identified what it believes to |
| be a reportable event.                                                       |
|                                                                              |
| "On purchase order #534, line item 4, an order was placed for two (2) Single |
| Tier racks Part No RD00-900-16EP3. Subsequent to the fabrication of these    |
| racks it was observed that a series of welds which join the horizontal cross |
| beam to the vertical member of the frame were not welded correctly. This may |
| affect the seismic qualification of the rack. Our understanding is that      |
| these racks have not been installed. C&D is making arrangements to replace   |
| the nonconforming frames prior to the facility's scheduled outage.           |
|                                                                              |
| "Copies of each of the following referenced drawings were supplied to [the   |
| licensee] on 10/10/02; the single tier racks (RD00900- 16 EP3) are covered   |
| by the following drawings;                                                   |
|                                                                              |
| "M121 14 (1) and (2) are page one and two of the same drawing. These are the |
| outline drawings for the rack. Page 1 covers the Bill of Material and shows  |
| the RD02008E frame is used in rack assembly.                                 |
|                                                                              |
| "Ml 104 is the frame drawing for part number RD02008E. The critical part of  |
| the drawing in our discussion is the gusset support labeled Part No. RE-263  |
| 1 (Dwg K-7406).                                                              |
|                                                                              |
| "Drawing M6228 (1) and (2) reflect the welding details for the racks.        |
|                                                                              |
| "Detail A on page 1 shows the flare bevel groove weld that is carried across |
| the length of the horizontal cross bar as it is welded to the vertical       |
| member of the frame. This should be carried the full distance of the         |
| intersection.                                                                |
|                                                                              |
| "Detail J on page 2 shows the addition of the gusset to reinforce the joint. |
| This is placed over the flare bevel groove weld above and then fillet welded |
| in place.                                                                    |
|                                                                              |
| "We have been advised that when our sub-tier supplier, Kim Manufacturing,    |
| manufactured the frames, they preassembled and clamped the vertical member,  |
| horizontal cross member and gusset in place. They performed a flare bevel    |
| groove weld on the exposed portion of the horizontal cross member, and       |
| fillet welded the remaining sections of the cross member and the gusset. The |
| portion of the cross member which was hidden behind the gusset was not       |
| welded with the flare bevel groove weld as it should have been.              |
|                                                                              |
| "These racks represented the first two racks manufactured by Kim             |
| Manufacturing after transfer of this manufacturing function to Kim from      |
| C&D's Conshohocken facility. To ensure that the problem did not predate      |
| C&D's relationship with Kim we have interviewed the welder responsible for   |
| this function within Conshohocken and determined that he was aware of the    |
| requirement for a full flare bevel groove weld prior to the assembly of the  |
| gusset plate. The welder reports that this was standard practice in          |
| Conshohocken. No other racks will be affected by this defect.                |
|                                                                              |
| "Kim Manufacturing first notified C&D of the defect in the welds on the      |
| afternoon of 10/8/02. After analysis by C&D's engineering department on      |
| Wednesday (10/9/02) we determined that we no longer had design traceability  |
| to the original seismic qualification of this rack and that this event       |
| should be reported. Initial contact was made with NMC Quality Assurance      |
| through [a licensee representative] on (10/10/02)."                          |
|                                                                              |
| The affected facility is the NMC Prairie Island Station.                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39274       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CALLAWAY                 REGION:  4  |NOTIFICATION DATE: 10/11/2002|
|    UNIT:  [1] [] []                 STATE:  MO |NOTIFICATION TIME: 19:29[EDT]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        10/11/2002|
+------------------------------------------------+EVENT TIME:        14:45[CDT]|
| NRC NOTIFIED BY:  JOHN DAMPF                   |LAST UPDATE DATE:  10/11/2002|
|  HQ OPS OFFICER:  GERRY WAIG                   +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |KRISS KENNEDY        R4      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NOTIFICATION TO OFFSITE AGENCIES DUE TO SULFURIC ACID RELEASE IN EXCESS OF   |
| LIMITS                                                                       |
|                                                                              |
| "This notification is being made under 10CFR50.72 (b)(2)(xi) for an event    |
| reportable to another government agency. The EPA National Response Center    |
| was notified at 1635, the Missouri Department of Natural Resources at 1645   |
| and the Local Emergency Planning Commission at 1650 on 10/11/2002 of a       |
| release of sulfuric acid in excess of the 40CFR302.6 and 40CFR355.40         |
| reportable quantities outside the plant boundary. At 0045 on 10/11/2002 a    |
| failure of the sulfuric acid feed system to the cooling tower basin was      |
| detected. The failure resulted in the release of 19,000 pounds (1300         |
| gallons) of sulfuric acid outside the plant boundary. At 0050 on 10/11/2002  |
| cooling tower blowdown was isolated and the release terminated, The total    |
| duration of the release was 7 hours, 27 minutes."                            |
|                                                                              |
| The licensee notified the NRC Resident Inspector of the event.               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39275       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DRESDEN                  REGION:  3  |NOTIFICATION DATE: 10/12/2002|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 07:55[EDT]|
|   RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3           |EVENT DATE:        10/11/2002|
+------------------------------------------------+EVENT TIME:        17:30[CDT]|
| NRC NOTIFIED BY:  VALHERIA GENGLER             |LAST UPDATE DATE:  10/12/2002|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |JOHN MADERA          R3      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       97       Power Operation  |97       Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FOR-CAUSE TEST FOR ALCOHOL                                                   |
|                                                                              |
| Contract supervisor while entering the site was given an initial for cause   |
| test for alcohol followed by a confirmatory test. Person tested positive for |
| alcohol on the confirmatory test. The person's access  was revoked.          |
|                                                                              |
| Call the Headquarters Operation Officer for further details.                 |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39276       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DIABLO CANYON            REGION:  4  |NOTIFICATION DATE: 10/12/2002|
|    UNIT:  [1] [2] []                STATE:  CA |NOTIFICATION TIME: 08:02[EDT]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        10/12/2002|
+------------------------------------------------+EVENT TIME:        01:30[PDT]|
| NRC NOTIFIED BY:  J. BROWN                     |LAST UPDATE DATE:  10/12/2002|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |KRISS KENNEDY        R4      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71(b)(1)         SAFEGUARDS REPORTS     |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       54       Power Operation  |54       Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| ALLEGED FITNESS-FOR-DUTY QUESTIONED DUE TO SLEEPING ON WATCH.                |
|                                                                              |
| IMMEDIATE COMPENSATORY MEASURES TAKEN UPON DISCOVERY.                        |
|                                                                              |
| THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR .                           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39277       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: OYSTER CREEK             REGION:  1  |NOTIFICATION DATE: 10/12/2002|
|    UNIT:  [1] [] []                 STATE:  NJ |NOTIFICATION TIME: 17:15[EDT]|
|   RXTYPE: [1] GE-2                             |EVENT DATE:        10/12/2002|
+------------------------------------------------+EVENT TIME:        16:00[EDT]|
| NRC NOTIFIED BY:  DAVID PIETRUSKI              |LAST UPDATE DATE:  10/12/2002|
|  HQ OPS OFFICER:  GERRY WAIG                   +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |JOHN WHITE           R1      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SPURIOUS ACTUATION OF ONE (1) OFFSITE EMERGENCY NOTIFICATION SIREN           |
|                                                                              |
| The licensee was notified by local police, Lacey Township, NJ, that one (1)  |
| of the emergency notification sirens was sounding. The licensee confirmed    |
| the actuation and notified the Ocean County Sheriffs Office, who control the |
| siren, and had them turn off the siren. The licensee has dispatched          |
| communications technicians to investigate the cause of the spurious          |
| actuation.                                                                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector of the event.               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   39278       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 10/12/2002|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 21:41[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        10/12/2002|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        04:45[EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  10/12/2002|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |JOHN MADERA          R3      |
|  DOCKET:  0707002                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  RICK LARSON                  |                             |
|  HQ OPS OFFICER:  GERRY WAIG                   |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NONR                     OTHER UNSPEC REQMNT    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| VALID (MANUAL) ACTUATION OF A SAFETY SYSTEM                                  |
|                                                                              |
| "October 12, 2002, at 0445 hours while performing UF6 sampling (Mode III),   |
| X-344 Feed and Transfer Building                                             |
| Operations personnel manually activated the X-344A Pigtail Line Isolation    |
| System (a Safety System) this was in                                         |
| response to an observed out-gassing from Autoclave #2 Sample Manifold.       |
| Operations were secured, and personnel                                       |
| evacuated the building per procedure. Emergency response personnel monitored |
| the area for surface and airborne                                            |
| contamination with all samples less than detectable. Autoclave #2 was        |
| declared inoperable. This event is being                                     |
| reported as a valid actuation of a Safety System per [procedure]             |
| UE2-RA-RE1030, Appendix D, Section J.2."                                     |
|                                                                              |
| The licensee notified the NRC Resident Inspector of the event via voice mail |
| and the DOE.                                                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39279       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PEACH BOTTOM             REGION:  1  |NOTIFICATION DATE: 10/12/2002|
|    UNIT:  [2] [3] []                STATE:  PA |NOTIFICATION TIME: 23:24[EDT]|
|   RXTYPE: [2] GE-4,[3] GE-4                    |EVENT DATE:        10/12/2002|
+------------------------------------------------+EVENT TIME:        21:14[EDT]|
| NRC NOTIFIED BY:  ROBERT BIRMINGHAM            |LAST UPDATE DATE:  10/12/2002|
|  HQ OPS OFFICER:  GERRY WAIG                   +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |JOHN WHITE           R1      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     N          Y       99       Power Operation  |99       Power Operation  |
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NOTIFICATION OF OFFSITE AUTHORITIES OF FIRE IN 500 KV SWITCHYARD             |
|                                                                              |
| The licensee notified offsite state and county authorities of a fire in the  |
| south 500 KV substation. The fire occurred at 2030 on the #205 circuit       |
| breaker current transformer during electrical switching. The state and       |
| county were notified of an event of public interest due to multiple          |
| emergency vehicles responding to the substation. The fire was extinguished   |
| at 2120. The #205 circuit breaker remains out of service. The circuit        |
| breaker is on one of two ring buses, on the output side of the main          |
| generators, and are located about one-half mile from the plant outside the   |
| protected area. Plant electrical systems, including safety systems, were     |
| unaffected by the fire in the switchyard.                                    |
|                                                                              |
| The licensee notified the NRC Resident Inspector of the event.               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39280       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 10/13/2002|
|    UNIT:  [1] [] []                 STATE:  FL |NOTIFICATION TIME: 12:56[EDT]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        10/13/2002|
+------------------------------------------------+EVENT TIME:        11:10[EDT]|
| NRC NOTIFIED BY:  KELLY KORTH                  |LAST UPDATE DATE:  10/13/2002|
|  HQ OPS OFFICER:  GERRY WAIG                   +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |GEORGE MacDONALD             |
|10 CFR SECTION:                                 |WILLIAM BECKNER      NRR     |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION  DUE TO THE DISCOVERY OF CONTAMINATED CLOTHING IN       |
| UNRESTRICTED AREA                                                            |
|                                                                              |
| "At 1130 EDT on October 13, 2002, Florida Power and Light made an            |
| informational notification to the State of Florida (Department of Health,    |
| Bureau of Radiation Control) regarding the discovery of contaminated         |
| clothing in an unrestricted area.                                            |
|                                                                              |
| "On October 12, 2002 at 1915 EDT, Health Physics personnel identified low    |
| level fixed contamination on an individual's undergarment in his hotel room. |
| The undergarment was confiscated. Measured activity was 20,000               |
| disintegrations per minute consisting primarily of Cobalt 58, Cobalt 60 and  |
| Chromium 51. This resulted in a shallow dose equivalent of 0.0014 rem per    |
| hour averaged over a 10-centimeter square. Conservatively assuming 16 hours  |
| of exposure results in 0.022 rem, a very small fraction of the 50-rem annual |
| shallow dose regulatory limit. No detectable activity was found on any other |
| item during a complete survey of the hotel room and its contents.            |
|                                                                              |
| "This notification is being made pursuant to 10CFR50.72(b)(2)(xi) in that    |
| other government agencies have been notified of an event related to the      |
| health and safety of the public or on-site personnel."                       |
|                                                                              |
| The licensee notified the NRC Resident Inspector of this event.              |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   39281       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  IDAHO DEPT OF ENVIRONMENTAL QUALITY  |NOTIFICATION DATE: 10/13/2002|
|LICENSEE:                                       |NOTIFICATION TIME: 14:40[EDT]|
|    CITY:  LAVA HOT SPRINGS         REGION:  4  |EVENT DATE:        10/13/2002|
|  COUNTY:  BANNOCK                   STATE:  ID |EVENT TIME:        10:30[MDT]|
|LICENSE#:                        AGREEMENT:  N  |LAST UPDATE DATE:  10/13/2002|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |KRISS KENNEDY        R4      |
|                                                |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  DOUG WALKER                  |                             |
|  HQ OPS OFFICER:  GERRY WAIG                   |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|BLO1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TWO MOISTURE DENSITY GAUGES FOUND IN IDAHO RIVER                             |
|                                                                              |
| Two local citizens found two Troxler moisture density gauges in the          |
| Portneous River located near Lava Hot Springs, Idaho, in Bannock County. The |
| citizens, seeing the trifoil radiation symbol on one of the gauges,          |
| immediately contacted the Bannock County Sheriffs Office. The  Sheriff's     |
| Office called the State of Idaho and  two hazardous material qualified State |
| Police Officers were dispatched to the scene. On-scene inspection of the two |
| gauges by the Idaho Dept. of Environmental Quality Radiation Safety Officer  |
| revealed that one of the gauges is Model 2401, serial #2813. The Model       |
| number on the second gauge is not readable but both appeared to be same      |
| model. The serial number of the second gauge is 2744. Additional information |
| found on the gauges indicated that they are 8.2 millicurie Cs-137, 50        |
| millicurie Am-241:Be sources. A survey of the gauges indicated a 13          |
| millirem/hour contact reading and less than 2 times background smear survey. |
| The sources will be transported to a secure location for storage until the   |
| owner(s) can be located and the gauges returned. Local law enforcement will  |
| continue to investigate the circumstances of the recovered gauges.           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Transportation                                   |Event Number:   39282       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  MICHIGAN DEPARTMENT OF ENVIR. QUAL   |NOTIFICATION DATE: 10/14/2002|
|LICENSEE:  SYNCOR                               |NOTIFICATION TIME: 09:58[EDT]|
|    CITY:  HESPERIA                 REGION:  3  |EVENT DATE:        10/14/2002|
|  COUNTY:  OCEANA                    STATE:  MI |EVENT TIME:        07:00[EDT]|
|LICENSE#:  04-26507-01MD         AGREEMENT:  N  |LAST UPDATE DATE:  10/14/2002|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JOHN MADERA          R3      |
|                                                |JOHN HICKEY          NMSS    |
+------------------------------------------------+NOWAK                DOT     |
| NRC NOTIFIED BY:  D. MINNAAR                   |STUART BAILEY        DOE     |
|  HQ OPS OFFICER:  JOHN MacKINNON               |NADER MAMISH         IRO     |
+------------------------------------------------+                             |
|EMERGENCY CLASS:                                |                             |
|10 CFR SECTION:                                 |                             |
|NINF                     INFORMATION ONLY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SYNCOR VEHICLE CARRYING  RADIOPHARMACEUTICALS OVERTURNED                     |
|                                                                              |
| A Syncor transportation vehicle, 2000 Ford Ranger Pickup truck, turned over  |
| near State Highway M-20 and 162 avenue which is located in Oceana County, MI |
| west of Hesperia, MI, around 0700 ET on October 14, 2002. The driver was not |
| injured.  Three packages were damaged or potentially damaged. The first      |
| package was empty and was being returned to Syncor was totally smashed. The  |
| second package had a White Label 1 containing 16.13 GBq of Tc-99m. The third |
| package was Yellow Label 2 contain 6.9GBq of Tc-99m and 0.001 GBq of I-123.  |
| The last two packages were being delivered to Gerber Memorial Health Center  |
| located in Fremont, MI.  When the local Fire Department/Police showed up at  |
| the scene of the accident they called Gerber Memorial Health Center and      |
| informed them that they needed someone to take radiation surveys at the      |
| scene of the accident.  Gerber Memorial Health Center sent a person to the   |
| scene of the accident. All radiological surveys taken at the scene of the    |
| accident indicated that  the contents of packages 2 & 3 were not damaged.    |
| The inner containers inside packages 2 & 3 were intact and undamaged.  The   |
| first package level was at normal background level.   The person from Gerber |
| Memorial Health Center placed the packages in the trunk of his car and took  |
| them to Gerber Memorial Health Center. Syncor went out to Gerber Memorial    |
| Health Center and picked up the packages and took them to their facility     |
| located in Jenison, MI.  Also Syncor took radiation surveys at the scene of  |
| the accident and all radiation readings were normal.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39283       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: OYSTER CREEK             REGION:  1  |NOTIFICATION DATE: 10/14/2002|
|    UNIT:  [1] [] []                 STATE:  NJ |NOTIFICATION TIME: 14:40[EDT]|
|   RXTYPE: [1] GE-2                             |EVENT DATE:        10/14/2002|
+------------------------------------------------+EVENT TIME:        14:15[EDT]|
| NRC NOTIFIED BY:  DAVE PIETRUSKI               |LAST UPDATE DATE:  10/14/2002|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |JOHN WHITE           R1      |
|10 CFR SECTION:                                 |                             |
|AUNA 50.72(b)(3)(ii)(B)  UNANALYZED CONDITION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DISCOVERY THAT APPENDIX R CRITERIA NOT SATISFIED FOR ELECTRICAL CABLING      |
|                                                                              |
| "An open void was discovered (approx. 5 feet deep) that exists in the area   |
| between the Reactor and Turbine Building walls beneath the 23' floor elev.   |
| affecting Appendix R fire separation. It appears that sand has been moved /  |
| eroded away over time, thus opening a void beneath the A and B 480 V switch  |
| gear room floors. Adequate separation of the conduits between A and B trains |
| no longer meets Appendix R separation criteria beneath the floor.            |
|                                                                              |
| "At the present time plant safety is not affected, as a compensatory measure |
| a firewatch has been established in the affected area."                      |
|                                                                              |
| The licensee has corrective action under review and has informed the NRC     |
| resident inspector.                                                          |
+------------------------------------------------------------------------------+





Page Last Reviewed/Updated Thursday, March 25, 2021