Event Notification Report for May 28, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/24/2002 - 05/28/2002 ** EVENT NUMBERS ** 38634 38809 38935 38941 38942 38943 38945 38946 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38634 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 01/17/2002| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 13:07[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 01/17/2002| +------------------------------------------------+EVENT TIME: 11:45[EST]| | NRC NOTIFIED BY: KELLY KORTH |LAST UPDATE DATE: 05/27/2002| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION INVOLVING RECOVERED SEA TURTLE FROM INTAKE CANAL | | | | At approximately 1130 EST on 01/17/02, a green sea turtle was retrieved from | | the intake canal and a determination was made that it was in need of | | rehabilitation. As required by the Plant's Sea Turtle Permit, the Florida | | Fish and Wildlife Conservation Commission (FFWCC) was notified at 1145 EST. | | | | The licensee notified the NRC Resident Inspector. | | | | See EN #38513 for 2001 occurrences. | | | | * * * UPDATE ON 1/28/02 @ 1243 BY KORTH TO GOULD * * * | | | | At approximately 1115 on 1/28/02 a loggerhead turtle was retrieved from the | | plant's intake canal. The turtle was determined to be in need of | | rehabilitation. Per the licensee's turtle permit, the Florida Fish and | | Wildlife Conservation Commission (FWCC) was notified at 1125. | | | | The NRC Resident Inspector was notified. Notified Reg 2 RDO (Ninh) | | | | * * * UPDATE ON 2/6/02 @ 0853 BY MERRILL TO GOULD * * * | | | | At approximately 0745 on 2/6/02 an injured green sea turtle was rescued from | | the plant's intake canal. The turtle was alive, but in need of | | rehabilitation. The turtle will be transported to a facility in Clearwater | | for treatment. The Florida Department of Environmental Protection has been | | notified of the event. | | | | The NRC Resident Inspector was notified. | | | | Notified Reg 2 RDO(Fredrickson) | | | | * * * UPDATE 1025 3/2/2002 BY R. DIEHL TAKEN BY R. STRANSKY * * * | | | | "At approximately 0830 3/2/02 a Loggerhead turtle was retrieved from the | | plant's intake canal. The turtle was determined to be in need of | | rehabilitation. Per the plant's turtle permit, the Florida Fish and Wildlife | | Conservation Commission (FWCC) was notified at 0845." | | | | The NRC resident inspector has been informed of this report. HOO notified | | R2DO (Julian). | | | | * * * UPDATE 1040EST ON 3/5/02 FROM GEORGE TULLIDGE TO S. SANDIN * * * | | | | "At Approximately 1000 on 3/5/02, a Loggerhead turtle was retrieved from the | | plant intake canal. The turtle was determined to be in need of | | rehabilitation. Per the plant's turtle permit, the Florida Fish and | | Wildlife Conservation Commission (FWCC) was notified." | | | | The NRC resident inspector has been informed of this report. HOO notified | | R2DO (Julian). | | | | * * * UPDATE 1047EST ON 3/6/02 FROM D. EMLING TO M.NORRIS * * * | | | | "At Approximately 1000 on 3/6/02, a Loggerhead turtle was retrieved from the | | plant intake canal. The turtle was determined to be in need of | | rehabilitation. Per the plant's turtle permit, the Florida Fish and | | Wildlife Conservation Commission (FWCC) was notified." | | | | The NRC resident inspector has been informed of this report. HOO notified | | R2DO (Henson). | | | | * * * UPDATE ON 3/10/02 @ 1740 BY KORTH TO GOULD * * * | | | | The Florida Department of Environmental protection was notified of a | | loggerhead sea turtle requiring off-site rehabilitation. The turtle was | | recovered live from the plant's intake canal. | | | | The NRC Resident Inspector was notified. | | | | Notified Reg @ RDO (Henson) | | | | * * * UPDATE ON 5/27/02 AT 1012 BY RUSSELL SCOT TO FANGIE JONES * * * | | | | The Florida Department of Environmental protection was notified of a sick | | underweight loggerhead sea turtle requiring off-site rehabilitation. The | | turtle was recovered live from the plant's intake canal at 0915 EST on | | 5/27/02. | | | | The NRC Resident Inspector will be notified. | | | | Notified R2DO (Thomas Decker). | | | | * * * UPDATE AT 1938EDT ON 5/27/02 FROM ELLIOT SUMNER TO S. SANDIN * * * | | | | "A dead Sea Turtle was recovered from the St. Lucie Plant Intake Canal at | | approx. 1600 [on] 05/27/02. The FL. Dept. of Envir. Protection was notified | | (1615 [on] 05/27/02) as required by the St. Lucie Plant - Sea Turtle Permit. | | This notification to a state government agency requires a four (4) hr | | non-emergency notification to the NRC per 10 CFR 50.72(b)(2)(xi). There | | were no unusual evolutions in progress beyond normal operations which would | | have contributed to this event." | | | | The NRC Resident Inspector will be informed. | | | | Notified R2DO(Decker). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38809 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 03/28/2002| | UNIT: [] [2] [3] STATE: IL |NOTIFICATION TIME: 01:24[EST]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 03/27/2002| +------------------------------------------------+EVENT TIME: 22:30[CST]| | NRC NOTIFIED BY: BROCK |LAST UPDATE DATE: 05/24/2002| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRUCE BURGESS R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 95 Power Operation |95 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SPURIOUS OPERATION OF THE REACTOR HEAD VENT VALVES IN THE SAFE SHUTDOWN | | REPORT(SSR) IS NOT CONSISTENT WITH THE NRC SAFETY EVALUATION REPORT. | | | | Specifically the Section 3.4.3 of the SER states that spurious operation of | | the Reactor Head Vent (RHV) valves {SO-2(3)-0220-46 ann SO-2(3)-0220-47} | | which would result in Reactor Coolant inventory loss, will be prevented by a | | pre-fire action to ensure closure by removing power from these valves. | | However, the current SSR dispositions this postulated concern based upon the | | assumption that spurious operation of greater than one normally closed valve | | in a series combination is not considered a credible failure mode except for | | high/low pressure systems. As a result, there is no pre-fire action to | | ensure closure by removing power to RHV valves. The documentation (FPR | | revision and 50.59) that supports the change in the licensing position of | | these valves from that described in the SER to the current SSR has not been | | located. | | | | A review was performed on the Fire Protection Report (FPR) which includes | | the Fire Hazard Analysis & Safe Shutdown Analysis, to evaluate the options | | for additional sources of water to address the loss of reactor inventory | | from the spurious actions of the reactor head vent valves. This review | | indicated that no specific circuit analysis was performed to determine what | | other available sources of water could be used for makeup of reactor | | inventory via the reactor head vent valves spurious operation. Therefore, | | in the event of a fire in the various assumed Appendix R fire zones, a | | qualified makeup source would not be available to mitigate the inventory | | loss introduced by the spurious operation of both RHV valves. | | | | Fuses have been pulled to remove power to and close a RHV valve on both Unit | | 2 and Unit 3 to comply with the SER. The action puts the plant in the | | configuration required if the RHV valves are considered a high-low pressure | | boundary. Completion of this action restores the plants compliance with the | | referenced SER. | | | | Dresden Engineering will perform an evaluation that documents the RHV valves | | as a high-low pressure boundary and that the actions taken above are | | adequate to mitigate the multiple spurious failures which must be postulated | | when these valves are considered a high/low pressure boundary. A revision | | to the FPR will be made to document the results of this evaluation. | | | | The NRC Resident Inspector will be notified. | | | | ***** RETRACTION AT 1815 EDT ON 05/24/02 FROM WARREN DEAGLE TO LEIGH TROCINE | | ***** | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On March 27, 2002 at 2230 CST, Dresden Station made an ENS Notification (EN | | 38809) regarding fuses that had not been removed from reactor head vent | | (RHV) valves. It was reported that the station's methodology for addressing | | fire induced spurious operation of the RHV valves in the safe shutdown | | report was not consistent with the NRC safety evaluation report. During | | preliminary reviews, it was postulated that a fire could result in spurious | | operation of these valves that in turn would result in reactor inventory | | loss. The postulated water source in the scenario was the opposite unit's | | Control Rod Drive system, which may not provide the makeup capability to | | maintain reactor water level above the top of active fuel (TAF)." | | | | "The condition was reported in accordance with 10 CFR 50.72(b)(3)(ii)(B), as | | an Unanalyzed condition that significantly degraded plant safety." | | | | "Upon further evaluation, it has been determined that a credible fire that | | would cause spurious operation of the RHV valves would not result in a loss | | in the High Pressure Coolant Injection (HPCI) system. Therefore, the HPCI | | system would have been available and capable to provide inventory makeup to | | the reactor vessel. Vessel water level would have been maintained above | | TAF. Based on the subsequent evaluation, the safety function (inventory | | control) would have been maintained at all times during post-fire safe | | shutdown of the unit." | | | | "Therefore, based on the above conclusion, this notification is being | | retracted." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R3DO (Christine Lipa). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38935 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 05/22/2002| |LICENSEE: HVJ ASSOCIATES |NOTIFICATION TIME: 17:49[EDT]| | CITY: AUSTIN REGION: 4 |EVENT DATE: 05/21/2002| | COUNTY: STATE: TX |EVENT TIME: 10:00[CDT]| |LICENSE#: L03813-003 AGREEMENT: Y |LAST UPDATE DATE: 05/22/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA SMITH R4 | | |THOMAS ESSIG NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HELEN WATKINS | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN HUMBOLDT GAUGE CONTAINING CESIUM-137 AND AMERICIUM-241 THAT WAS LATER | | RECOVERED | | | | | | On May 21, 2002, a Humboldt 5001EZ gauge was stolen between the hours of | | 1000 hours and 1200 hours from a truck parked behind the Licensee's office, | | HVJ Associates, Inc. located in Austin. The gauge was discovered missing at | | 1230 hours and was later found at 1400 hours. The gauge was found by | | security at a local shopping plaza. The gauge was secure inside the yellow | | container on the ground near a dumpster. The shielding remained intact and | | no one was exposed to the excessive radiation levels. The local police had | | been notified of the gauge being stolen. The serial number for the Humboldt | | gauge is 3776. No media attention. | | | | Texas Incident No. I-7896 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38941 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 05/24/2002| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 09:26[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 05/23/2002| +------------------------------------------------+EVENT TIME: 14:00[EDT]| | NRC NOTIFIED BY: JOE WIDAY |LAST UPDATE DATE: 05/24/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM RULAND R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY REPORT | | | | A non-licensed contract supervisor was determined to have provided a tainted | | sample during a random drug test. The employee's access to the plant has | | been terminated. | | | | Refer to the Headquarters Operations Officer for additional details. | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38942 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 05/24/2002| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 12:33[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 05/23/2002| +------------------------------------------------+EVENT TIME: 19:34[EDT]| | NRC NOTIFIED BY: PATRICK RYAN |LAST UPDATE DATE: 05/24/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RONALD BELLAMY R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A CONTRACT SUPERVISOR TESTED POSITIVE FOR ALCOHOL DURING A RANDOM | | FITNESS-FOR-DUTY TEST (24-Hour Report) | | | | A contract supervisor failed a random drug and alcohol fitness-for-duty | | test. The individual tested positive for alcohol, and the results of the | | drug portion of the test have not yet been received. The individual's | | unescorted site access was terminated at 1937 on 05/23/02, and the licensee | | plans to perform a review of the individual's work for the last 30 calendar | | days or for the duration of the individual's employment (which ever is | | shorter). (Call the NRC operations officer for additional details.) | | | | The licensee notified the NRC resident inspector and plans to notify the NRC | | Region 1 office (Greg Smith). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38943 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: US ARMY |NOTIFICATION DATE: 05/24/2002| |LICENSEE: US ARMY |NOTIFICATION TIME: 14:39[EDT]| | CITY: ABERDEEN REGION: 1 |EVENT DATE: 05/24/2002| | COUNTY: STATE: MD |EVENT TIME: 11:30[EDT]| |LICENSE#: 19-00294-19 AGREEMENT: Y |LAST UPDATE DATE: 05/24/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |RONALD BELLAMY R1 | | |FRED BROWN NMSS | +------------------------------------------------+NADER MAMISH IRO | | NRC NOTIFIED BY: JOHN BECKMAN | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF CONTAMINATION/TRITIUM LEAKAGE ON AN M-1 TANK MUZZLE REFERENCE | | SENSOR AT THE US ARMY ABERDEEN TEST SITE TANK RANGE | | | | While preparing a tank for shipment, the licensee discovered that an M-1 | | Tank Muzzle Reference Sensor (MRS) containing 10 curies of tritium was | | leaking and discharged to the atmosphere. The exact time that the leak | | occurred is not currently known. Apparently, 200 rounds were fired from | | this tank, and then the MRS was checked prior to shipment of the tank to | | Michigan. Three swipe counts were performed, and the contamination levels | | ranged between 150,000 and 170,000 dpm/100 cm�. | | | | The licensee stated that there were no personnel contaminations as a result | | of this event. A swipe count was performed on the hands of the individual | | who installed the MRS, and it was negative. Urinalysis is also being | | performed as a precautionary measure, and the results are pending. | | Apparently, no other personnel came into contact with the leaking MRS. | | | | The leaking MRS was removed, double bagged, and placed in storage. The | | licensee plans to dispose of it as radioactive waste. | | | | There was minimal contamination on the tank gun tube, and it was cleaned to | | acceptable levels (below limits). The licensee plans to ship the tank | | without the MRS. | | | | (Call the NRC operations officer for a contact telephone number for the | | licensee's Radiation Safety Officer.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38945 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 05/24/2002| | UNIT: [1] [2] [] STATE: SC |NOTIFICATION TIME: 17:06[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/24/2002| +------------------------------------------------+EVENT TIME: 14:20[EDT]| | NRC NOTIFIED BY: JEFFREY BRADLEY |LAST UPDATE DATE: 05/24/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |THOMAS DECKER R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING THE DISCOVERY OF AN OLD SPENT BLASTING CAP IN | | THE YARD OUTSIDE THE PROTECTED AREA | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Offsite agency assistance [was] requested to assess a spent blasting cap | | found outside the Protected Area in the yard. A City of Rock Hill | | explosives expert was requested by security to assess/take possession of the | | spent blasting cap." | | | | "The explosives expert determined that the blasting cap was spent[. The | | explosives expert also] determined its age as 10-20 years at least and [that | | it] was leftover from the construction of the site. The officer took | | possession of the spent blasting cap and removed it from the site at 1507 | | EDT." | | | | The licensee notified the NRC resident inspector and City of Rock Hill | | Police Department in South Carolina. The licensee also plans to notify the | | States of North Carolina and South Carolina as well as York, Gaston, and | | Mecklenburg Counties. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38946 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 05/26/2002| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 15:24[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/26/2002| +------------------------------------------------+EVENT TIME: 08:35[EDT]| | NRC NOTIFIED BY: BRADLEY |LAST UPDATE DATE: 05/26/2002| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |THOMAS DECKER R2 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PERSONNEL ACCESS DOOR BETWEEN UPPER AND LOWER CONTAINMENT COMPARTMENTS FOUND | | OPEN | | | | Maintenance technicians discovered a personnel access door (submarine hatch) | | open between the upper and lower containment compartments. The seals and | | sealing surfaces were inspected and the door was closed immediately in | | compliance with LCO 3.6.14. While the door was open, containment divider | | integrity was not intact per LCO 3.6.14. This LCO establishes the minimum | | equipment requirements to ensure that the divider barrier performs its | | safety function of ensuring that bypass leakage, in the event of a DBA, does | | not exceed the bypass leakage assumed in the accident analysis. The divider | | barrier functions with the ice condenser to limit the pressure and | | temperature that could be expected following a DBA. | | | | An analysis performed to support a 6 hour completion time in LCO 3.6.14 | | condition B indicates that an open hatch(7.5 sq. ft bypass area) during a | | DBA does not impact the design pressure or temperature of the containment. | | The submarine hatch is 2 ft in diameter(3.19 sq. ft), thus the safety | | significance is considered minimal at this time. | | | | The NRC Resident Inspector will be notified along with the states of N | | Carolina and S Carolina. | | | | Also the nearby counties were notified. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021