Event Notification Report for May 15, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/14/2002 - 05/15/2002 ** EVENT NUMBERS ** 38915 38919 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38915 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 05/13/2002| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 02:39[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/12/2002| +------------------------------------------------+EVENT TIME: 23:01[EDT]| | NRC NOTIFIED BY: BRADDOCK D. LEWIS |LAST UPDATE DATE: 05/14/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANTON VEGEL R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO AN INSTRUMENTATION RACK POWER SUPPLY FAILURE | | WHICH CAUSED A STEAM GENERATOR FEEDWATER REGULATING VALVE TO FAIL CLOSED | | | | The following text is a portion of a facsimile received from the licensee: | | | | "DC Cook Unit 2 tripped from full power due to an instrumentation rack power | | supply failure on 05/12/02 [at] 2301. All control rods fully inserted. No | | Safety Injection was required. The Unit 2 Reactor is stable and | | subcritical. The Steam Generator Stop Valves were manually closed by the | | Operating Crew to stabilize RCS Temperature in accordance with Plant | | operating procedures. Reactor Coolant Temperature is being maintained | | manually on the Steam Generator Atmospheric relief valves at No-Load T(ave) | | in accordance with plant procedures." | | | | "This instrumentation rack power supply failure caused the #21 Steam | | Generator Feed Regulating Valve to fail CLOSED. The Unit 2 Reactor | | subsequently TRIPPED on Low Level in [the] #21 Steam Generator coincident | | with Low Feedwater Flow. Several control systems were affected by the | | control rack instrumentation failure: Pressurizer Pressure Control - | | transferred control to manual and restored Pressurizer pressure, Pressurizer | | Level Control - transferred control to manual and restored Pressurizer water | | level, Refueling Water Sequence - Manually transferred Charging Pump Suction | | to the RWST. Manual Operator response maintained and restored critical | | plant parameters in MANUAL to normal parameter values." | | | | "Unit 2 entered Technical Specification 3.0.3 for 34 minutes because the | | control system failures and plant system response temporarily caused the | | Boration Flow paths from both the Refueling Water Storage Tank and Boric | | Acid Storage Tanks to become INOPERABLE. Both Boration flow paths were | | subsequently returned to OPERABLE status by manual Operator action." | | | | "The Reactor trip is reportable in accordance with 10 CFR 50.72(b)(2)(iv)(B) | | as an actuation of the Reactor Protection System (RPS) when the Reactor was | | critical. The Reactor TRIP was the result of an instrumentation rack power | | supply failure and was not part of any preplanned test or evolution." | | | | The licensee stated that the unit is currently stable in Mode 3 (Hot | | Standby). The reactor coolant pumps are available for primary system | | transport control. Pressurizer level and pressure control are in manual. | | Normal charging and makeup are available, but the automatic function of the | | refueling water sequence is not available. The auxiliary feedwater pumps | | automatically started as expected and are currently being utilized to supply | | water to the steam generators. Secondary steam is being dumped to | | atmosphere. There is no evidence of steam generator tube leakage, and | | containment parameters are as expected. There were no safety injections and | | none were required, and none of the primary power-operated relief valves | | lifted. | | | | The licensee notified the NRC resident inspector. | | | | ****UPDATE 5/14/02 At 13:20 From B. Bates To R. Laura**** | | | | The initial report stated that the reactor coolant temperature is being | | maintained manually on the steam generator atmospheric relief valves at | | no-load Tave in accordance with plant procedures. Temperature control was | | actually established in automatic on the steam generator atmospheric relief | | valves and remains in automatic. | | | | A statement was made in the original report that Unit 2 entered Technical | | Specification 3.0.3 for 34 minutes. Upon further review, there was no | | requirement to enter Technical Specification 3.0.3. The control system | | failures and plant system response caused the boration flowpaths from both | | the Refueling Water Storage Tank (RWST) and Boric Acid Storage Tanks to | | become inoperable. Therefore, the Unit was actually in Technical | | Specification 3.1.2.2 actions (a)and (b) concurrently. This did not | | constitute an entry into Technical Specification 3.0.3 because entry into | | both actions is not prohibited. | | | | Another statement was made that both boration fiowpaths were subsequently | | returned to operable status by manual operator action. The boration flowpath | | from the boric acid storage tanks was returned to operable. However, after | | further investigation, it was determined that the boration flow path from | | the RWST remained inoperable due to the inability of the refueling water | | sequence to automatically initiate. The NRC Resident Inspector was | | notified. | | | | Notified R3DO R. Gardner. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38919 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ABB, INC. |NOTIFICATION DATE: 05/14/2002| |LICENSEE: ABB, INC. |NOTIFICATION TIME: 08:05[EDT]| | CITY: FLORENCE REGION: 2 |EVENT DATE: 05/14/2002| | COUNTY: STATE: SC |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 05/14/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DANIEL HOLODY R1 | | |ROBERT HAAG R2 | +------------------------------------------------+RONALD GARDNER R3 | | NRC NOTIFIED BY: PATRICK O'NEAL (fax) |DAVE LOVELESS R4 | | HQ OPS OFFICER: LEIGH TROCINE |VERN HODGE NRR | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOTIFICATION OF A POTENTIAL DEFECT REGARDING K-LINE MECHANISM FAILURES TO | | CHARGE AND CLOSE | | | | The following text is a portion of a facsimile received from ABB, Inc.: | | | | "In August of 2001, Southern California Edison, San Onofre Nuclear | | Generating Station, reported and submitted an operating mechanism for | | evaluation to the ABB, Inc., Florence, SC Breaker Manufacturing Facility due | | to suspected shipping damage causing 'failure to charge' symptoms. The | | mechanism was a special configuration of the base 709774 Model '05' | | mechanism manufactured in 10/1997. This mechanism was in a Nuclear | | Safety-Related application. The mechanism was received by the factory in | | September of 2001, and the reported failure mode was not duplicated in | | Florence. However, under the auspices of a 'refurbishment,' ABB, Inc., | | personnel performed an evaluation of critical characteristics for parts that | | could be contributory to the failure mode described herein." | | | | "On 7 February 2002, Ameren - Union Electric's Sioux Generating Plant | | reported a failure to charge and close of a Model '05' K-Line K-600S circuit | | breaker (Serial Number 935461B--010496) manufactured 04/96. This breaker | | was purchased for a Non-1E application. The cause of the breaker failure | | was determined to be a culmination of energy utilization deficits. | | Specifically, the condition of lubricant (Anderol 757), the surface and | | finish of parts critical to the charging operation, and the interaction of | | critical latching surfaces serve to impede the ability of the mechanism to | | fully charge through the end of the charge cycle." | | | | "In March 2002, Dominion Virginia Power's Surry Nuclear Station reported the | | failure to charge and close of a 1993 K-800M (Serial Number | | 865613B033--010793). In this case the breaker was refurbished in the hopes | | of alleviating the symptoms, only to find they returned a short time after | | return to service. ABB, Inc., had already initiated Part 21 reporting | | proceedings as this latest failure was announced, and the Florence Breaker | | Manufacturing Facility is awaiting a customer report to verify the failure | | mode." | | | | "In all cases, the end user is observing a failure to charge and/or close in | | electrically operated mechanisms. These failures are due to one of the | | following two scenarios:" | | | | "1. A failure to charge and close, either mechanically or electrically, | | until the needed energy is supplied to rotate the charging cam over the | | center-point into a fully charged position -- either by mechanical vibration | | or operator rotation of the charging cam." | | | | "2. A failure to close where the above scenario does not exist but the | | fully charged mechanism does not close due to the fact that the primary | | close latch does not fully clear in response the secondary close latch | | actuation." | | | | "With the introduction of the Model '07' mechanism in December 1998, while | | maintaining backward compatibility with pre-existing models, ABB has | | facilitated improvements to be incorporated into every mechanism that is | | built at the Florence Breaker Manufacturing Facility. ABB recognizes that | | this failure mode may exist in any K-Line circuit breaker manufactured or | | having undergone mechanism repair, refurbishment, or replacement between | | January 1, 1988 and December 31, 1998 and, therefore, recommends that | | utilities address this issue at the next available maintenance interval. | | This includes any 'spare' K-Line mechanisms manufactured during the afore | | determined time frame that may be in stock." | | | | "Three equally viable options are available to rectify this situation. They | | are, listed in order of ABB preference, most desirable first:" | | | | "1. Replacement of suspect K-Line operating mechanism (ABB part number | | 709774T##) with a Model '07' mechanism (ABB part number 716785T##). This | | option will require the purchase of an Engineering Qualification Report | | Addendum so that 1E dedication traceability is maintained." | | | | "2. Upgrade of suspect K-Line operating mechanism to a Model '07' mechanism | | utilizing one of ABB upgrade kits, numbers 716659T03 through T10. This | | option will require the purchase of an Engineering Qualification Report | | Addendum so that 1E dedication traceability is maintained." | | | | "3. Improvement of suspect K-Line operating mechanism within the original | | model class utilizing ABB repair kit number 716659T01 or T02." | | | | "Work required by the options listed above should only be performed by | | personnel trained and/or authorized by ABB, Inc. ABB is available to | | perform the work in the Florence, South Carolina, factory or perform | | in-factory training if non-ABB personnel are to be used or contracted." | | | | "Note: If work associated with options 2 or 3 above is performed by | | personnel outside of the Florence, SC factory, one minor configuration | | change must be noted. During mechanism re-assembly, technicians must | | relocate the washer (ABB part number 650351A57) from its original location | | on the control device side on the Primary Close Latch Pivot Pin (ABB part | | number 702883D00) to the charging motor side." | | | | "ABB [plans to] notify all Nuclear Utility Companies." | | | | Call the NRC operations officer for ABB, Inc., contact information. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021