Event Notification Report for May 2, 2002
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
05/01/2002 - 05/02/2002
** EVENT NUMBERS **
38888 38891
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|Power Reactor |Event Number: 38888 |
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| FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 04/30/2002|
| UNIT: [] [2] [] STATE: AR |NOTIFICATION TIME: 19:13[EDT]|
| RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 04/30/2002|
+------------------------------------------------+EVENT TIME: 18:01[CDT]|
| NRC NOTIFIED BY: JAMES PORTER |LAST UPDATE DATE: 05/01/2002|
| HQ OPS OFFICER: RICH LAURA +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: UNUSUAL EVENT |BLAIR SPITZBERG R4 |
|10 CFR SECTION: |SUSIE BLACK NRR |
|AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |TIM MCGINTY IRO |
| |RENE ZAPATA FEMA |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N N 0 Hot Standby |0 Hot Standby |
| | |
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EVENT TEXT
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| UNUSUAL EVENT AT ANO2 DUE TO BORON RESIDUE AT PRESSURIZER HEATER
SLEEVE N-2 |
| |
| "On 4/30/02, while performing a planned Reactor Coolant System Integrity |
| Inspection following the 2R15 refueling outage, with the Reactor Coolant |
| System at normal operating temperature and pressure (Mode 3), an inspector |
| discovered small traces of boric acid on pressurizer heater sleeve N-2. |
| Based on the subsequent evaluation, pressurizer heater sleeve N-2 has been |
| determined to have had pressure boundary leakage. No current leakage is |
| detectable. The Unit 2 Tech Spec 3.4.6.2 does not allow operation in Modes |
| 1-4 with any pressure boundary leakage. Therefore a plant cooldown is being |
| initiated to place Unit 2 in Mode 5. Based on this criteria, the condition |
| is reportable upon declaring a Notification of Unusual Event (EAL 2.1) and |
| Degraded Condition which is reportable per 1OCFR50.72(b)(3)(ii)(A)". |
| |
| The NRC Resident Inspector was notified. |
| |
| |
| * * * UPDATE ON 5/1/02 @ 0331 BY AHO TO GOULD * * * |
| |
| NOUE terminated at 0221CDT. Plant in mode 5 (cold shutdown) |
| |
| The NRC Resident Inspector will be notified. |
| |
| Notified FEMA(Zapata), REG 1 RDO(Spitzberg), EO(Black) and IRO(McGinty) |
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|Power Reactor |Event Number: 38891 |
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| FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/01/2002|
| UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 15:45[EDT]|
| RXTYPE: [1] GE-3 |EVENT DATE: 05/01/2002|
+------------------------------------------------+EVENT TIME: 15:00[EDT]|
| NRC NOTIFIED BY: RANDOLPH HAISLET |LAST UPDATE DATE: 05/01/2002|
| HQ OPS OFFICER: RICH LAURA +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |JOHN KINNEMAN R1 |
|10 CFR SECTION: | |
|ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
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EVENT TEXT
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| LOSS OF OFFSITE EP SIRENS |
| |
| The licensee reported an unexpected loss of the prompt alert notification |
| system (i.e., sirens) due to unknown reasons. Compensatory measures are in |
| place and an investigation was started to determine the cause of the |
| problem. |
| |
| The NRC Resident Inspector has been notified. Also, the licensee informed |
| the State and local agencies. |
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