Event Notification Report for May 2, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/01/2002 - 05/02/2002 ** EVENT NUMBERS ** 38888 38891 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38888 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 04/30/2002| | UNIT: [] [2] [] STATE: AR |NOTIFICATION TIME: 19:13[EDT]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 04/30/2002| +------------------------------------------------+EVENT TIME: 18:01[CDT]| | NRC NOTIFIED BY: JAMES PORTER |LAST UPDATE DATE: 05/01/2002| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |BLAIR SPITZBERG R4 | |10 CFR SECTION: |SUSIE BLACK NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |TIM MCGINTY IRO | | |RENE ZAPATA FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Hot Standby |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT AT ANO2 DUE TO BORON RESIDUE AT PRESSURIZER HEATER SLEEVE N-2 | | | | "On 4/30/02, while performing a planned Reactor Coolant System Integrity | | Inspection following the 2R15 refueling outage, with the Reactor Coolant | | System at normal operating temperature and pressure (Mode 3), an inspector | | discovered small traces of boric acid on pressurizer heater sleeve N-2. | | Based on the subsequent evaluation, pressurizer heater sleeve N-2 has been | | determined to have had pressure boundary leakage. No current leakage is | | detectable. The Unit 2 Tech Spec 3.4.6.2 does not allow operation in Modes | | 1-4 with any pressure boundary leakage. Therefore a plant cooldown is being | | initiated to place Unit 2 in Mode 5. Based on this criteria, the condition | | is reportable upon declaring a Notification of Unusual Event (EAL 2.1) and | | Degraded Condition which is reportable per 1OCFR50.72(b)(3)(ii)(A)". | | | | The NRC Resident Inspector was notified. | | | | | | * * * UPDATE ON 5/1/02 @ 0331 BY AHO TO GOULD * * * | | | | NOUE terminated at 0221CDT. Plant in mode 5 (cold shutdown) | | | | The NRC Resident Inspector will be notified. | | | | Notified FEMA(Zapata), REG 1 RDO(Spitzberg), EO(Black) and IRO(McGinty) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38891 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/01/2002| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 15:45[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/01/2002| +------------------------------------------------+EVENT TIME: 15:00[EDT]| | NRC NOTIFIED BY: RANDOLPH HAISLET |LAST UPDATE DATE: 05/01/2002| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF OFFSITE EP SIRENS | | | | The licensee reported an unexpected loss of the prompt alert notification | | system (i.e., sirens) due to unknown reasons. Compensatory measures are in | | place and an investigation was started to determine the cause of the | | problem. | | | | The NRC Resident Inspector has been notified. Also, the licensee informed | | the State and local agencies. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021