Event Notification Report for February 28, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/27/2002 - 02/28/2002 ** EVENT NUMBERS ** 38727 38728 38729 38730 38731 38732 38733 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38727 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: RI DEPT OF RADIOLOGICAL HEALTH |NOTIFICATION DATE: 02/27/2002| |LICENSEE: RHODE ISLAND HOSPITAL |NOTIFICATION TIME: 09:47[EST]| | CITY: PROVIDENCE REGION: 1 |EVENT DATE: 01/28/2002| | COUNTY: PROVIDENCE STATE: RI |EVENT TIME: 15:00[EST]| |LICENSE#: 7D-051-01 AGREEMENT: Y |LAST UPDATE DATE: 02/27/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JAMES LINVILLE R1 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JACK FERRUOLO | | | HQ OPS OFFICER: GERRY WAIG | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING POSSIBLE MISADMINISTRATION | | | | "Event description: Cordis Checkmate IVBT system was used to treat a | | coronary artery on 1/28/02. On 1/31/02 dosimetry and physicist records were | | being reviewed by licensee physics staff and it was discovered that the | | 'diameter' of the vessel was used in the calculation instead of the | | 'radius'. Agency was contacted by phone on 14 February 2002 to inform | | Agency of possible misadministration. At this time the actual increase in | | dose had not been determined. On 14 February 2002 the Agency was notified | | by FAX that, in fact, a misadministration had occurred. Estimated dose | | received by the outer portion of the coronary artery was 14.6 Gy rather than | | the intended 8 Gy. Patient and physician were notified." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38728 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WESTINGHOUSE ELECTRIC CORPORATION |NOTIFICATION DATE: 02/27/2002| | RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 11:59[EST]| | COMMENTS: LEU CONVERSION (UF6 to UO2) |EVENT DATE: 02/26/2002| | COMMERCIAL LWR FUEL |EVENT TIME: 15:00[EST]| | |LAST UPDATE DATE: 02/27/2002| | CITY: COLUMBIA REGION: 2 +-----------------------------+ | COUNTY: RICHLAND STATE: SC |PERSON ORGANIZATION | |LICENSE#: SNM-1107 AGREEMENT: Y |CAUDLE JULIAN R2 | | DOCKET: 07001151 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DAVID WILLIAMS | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01 RESPONSE INVOLVING A C4 DISSOLVER ACID WASH PUMPOUT | | (24-Hour Report) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Facility -- Westinghouse Electric Company, Commercial Fuel Fabrication | | Facility, Columbia SC, low enriched (<=5.0 wt. % U-235) PWR fuel fabricator | | for commercial light water reactors. License: SNM-1107." | | | | "Time and Date of Event -- Approx. 15:00 hours, Tuesday, February 26, | | 2002." | | | | "Reason for Notification -- During an internal procedure review by | | Operations, it was discovered that a current Process Information Form (PIF) | | for flushing and pumping out the lines of the C4 dissolvers did not contain | | all the required criticality controls. The operating procedure for pumpout | | of UN product to non-favorable geometry bulk storage requires sampling for | | grams U-235 per liter, pH, and % free acid. The PIF required only % free | | acid." | | | | "Summary of Process -- During normal processing, uranium is recovered from | | scrap materials in the favorable geometry C4 dissolvers system. The | | resulting uranyl nitrate (UN) is sampled and released. It is then pumped | | through gamma monitors, an active engineered control, to the non-favorable | | geometry UN bulk storage tanks." | | | | "When needed for uranium accountability purposes, the C4 dissolver system | | tanks are filled with water to the 40% level and then with water and acid to | | the 43% level (approximately 102.3 gallons total) to flush the system." | | | | "As-Found Condition -- A summary of the as found conditions is as follows: | | * The condition was found during an internal procedure review - not during | | acid wash pumpout. | | * The PIF was approved for use on February 14, 2002. | | * The PIF required only sampling for free acid. | | * The gamma monitors were functioning properly." | | | | "Double Contingency Protection -- Double contingency protection for this | | situation is based on concentration control, that is (1) preventing | | solutions with >10 grams U-235 per liter from being transferred into the UN | | bulk storage tanks, and (2) detecting any increasing concentration of U-235 | | in the tanks and taking corrective actions. It was determined, however, | | that documented double contingency protection was lost because sampling for | | pH was not required on the PIF. Double contingency protection was | | immediately restored by withdrawing the PIF. Therefore, the incident | | requires notification in accordance with Westinghouse Operating License | | (SNM-1107), paragraph 3.7.3(c.5), in which less than previously documented | | double contingency protection remains in an analyzed system, but less than | | safe mass is involved." | | | | "Summary of Activity -- | | * The PIF was immediately withdrawn. | | * Immediate instructions were given to Operations to ensure that all | | required sampling was performed. | | * A causal analysis will be performed to determine corrective actions | | needed to prevent recurrence." | | | | "Conclusions -- | | * Loss of documented double contingency protection did occur, but was | | immediately restored. | | * At no time was criticality possible because the gamma monitors ensure | | that the concentration remains <5 grams U-235 per liter. | | * At no time was there any risk to the health or safety of any employee or | | member of the public. No exposure to hazardous material was involved. | | * It has been determined that this is a safety significant incident in | | accordance with governing procedures. A root cause analysis will be | | performed." | | | | The licensee notified the NRC Region 2 office (David Ayres) and NMSS (Dennis | | Morey). | | | | (Call the NRC operations officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38729 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIV OF MICHIGAN |NOTIFICATION DATE: 02/27/2002| |LICENSEE: UNIV OF MICHIGAN |NOTIFICATION TIME: 12:00[EST]| | CITY: ANN ARBOR REGION: 3 |EVENT DATE: 02/27/2002| | COUNTY: WASHTENAW STATE: MI |EVENT TIME: 08:30[EST]| |LICENSE#: 21-00215-04 AGREEMENT: N |LAST UPDATE DATE: 02/27/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHRISTINE LIPA R3 | | |ALEXANDER ADAMS/PM NRR | +------------------------------------------------+DON COOL NMSS | | NRC NOTIFIED BY: MARK DRISCOLL |JOSEPH HOLONICH IRO | | HQ OPS OFFICER: LEIGH TROCINE |IMOB Office via fax NMSS | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10 CFR PART 21 NOTIFICATION REGARDING FAILURE OF A J.L. SHEPHERD & | | ASSOCIATES, MARK-1, MODEL-25, IRRADIATOR, DOOR INTERLOCK | | | | During the performance of a pre-operations inspection, an operator | | discovered that an irradiator door interlock could be defeated and that the | | door could be raised and expose the source. The irradiator involved is a | | J.L. Shepherd & Associates, Mark 1, Model 25, irradiator which contains 780 | | curies of cesium-137, and it is used for irradiating biological specimens. | | | | The university has been contacted. The licensee notified the NRC Region 3 | | office (Darryl Weideman), and the licensee plans to notify the vendor. | | | | (Call the NRC operations officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38730 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 02/27/2002| | UNIT: [] [] [3] STATE: CA |NOTIFICATION TIME: 14:54[EST]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 02/27/2002| +------------------------------------------------+EVENT TIME: 10:43[PST]| | NRC NOTIFIED BY: DOUG KNUDSON |LAST UPDATE DATE: 02/27/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVID GRAVES R4 | |10 CFR SECTION: |TOM KOSHY NRR | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|JOSEPH HOLONICH IRO | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 A/R Y 100 Power Operation |0 Hot Standby | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC TURBINE TRIP/REACTOR TRIP DUE TO A LOSS OF OFFSITE POWER ON UNIT 3 | | DURING THE PERFORMANCE OF SWITCHYARD MAINTENANCE | | | | | | Prior to this transient, the 220-kV, switchyard, section-B, west bus was | | de-energized to facilitate the performance of maintenance activities. | | During the performance of local breaker failure backup testing on the | | switchyard, section-B, west bus; the switchyard section-B east bus tripped | | at 1043 PST resulting in a loss of offsite power on Unit 3. The loss of | | offsite power in turn caused a turbine trip/reactor trip signal to be | | generated. All rods fully inserted. An emergency feedwater actuation | | signal (EFAS) initiated as expected on steam generator shrinkage, and a | | containment cooling actuation signal (CCAS) was manually initiated. The | | loss of offsite power also resulted in a loss of all non-1E power. The | | reactor coolant pumps remained running because their power supply | | automatically transferred to Unit 2, and the Unit 3, 1E, 4-kV buses remained | | energized from Unit 2. The emergency diesel generators automatically | | started but did not load due to the automatic power supply transfers to Unit | | 2. Preliminary indications revealed that the primary safety valves remained | | closed. The licensee stated that all systems functioned as required and | | that there was no impact on Unit 2. | | | | Unit 3 is currently stable in Hot Standby with emergency feedwater supplying | | water to the steam generators and secondary steam being dumped to atmosphere | | via the atmospheric dump valves (due to a loss of condenser vacuum). The | | licensee reported that there was no steam generator tube leakage. | | Containment parameters remain normal. | | | | The Unit 3 east and west switchyard buses have been re-energized, and all | | non-1E power was restored to the 4-kV buses at 1120 PST. The emergency | | diesel generators have been secured. The licensee currently plans to | | perform secondary equipment inspections, and the event evaluation is | | ongoing. | | | | The licensee notified the NRC resident inspector and may make a press | | release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38731 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CANBERRA INDUSTRIES, INC. |NOTIFICATION DATE: 02/27/2002| |LICENSEE: CANBERRA INDUSTRIES, INC. |NOTIFICATION TIME: 15:13[EST]| | CITY: WARRINGTON REGION: 1 |EVENT DATE: 01/28/2002| | COUNTY: STATE: PA |EVENT TIME: 13:00[EST]| |LICENSE#: 37-02401-01 AGREEMENT: N |LAST UPDATE DATE: 02/27/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JAMES LINVILLE R1 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: TERRY SCHWAGER | | | HQ OPS OFFICER: MIKE NORRIS | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF LICENSED NUCLEAR MATERIAL | | | | On 1/28/02 at 1300, it was discovered that 13 Cl-36 sources were missing. | | The sources were 10 microcuries each and were manufactured on Nov 1995. The | | sources were 1 inch diameter, flat disc with mylar window, and assembled | | with an ion chamber instrument. Each source was individually packaged in a | | 2ft x 1ft x 1ft cardboard box. The assemblies were packaged for shipment on | | 1/28/02 and stored on a shelf prior to shipment. A clean up had been | | performed recently and it is believed by the Licensee, that these materials | | had been thrown into a waste dumpster for disposal. | | | | There was no detectable radiation levels on the shipping container, and it | | is believed by the Licensee that there is no threat to the general | | population. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38732 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DAVIS BESSE REGION: 3 |NOTIFICATION DATE: 02/27/2002| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 15:42[EST]| | RXTYPE: [1] B&W-R-LP |EVENT DATE: 02/27/2002| +------------------------------------------------+EVENT TIME: 13:30[EST]| | NRC NOTIFIED BY: DALE MILLER |LAST UPDATE DATE: 02/27/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHRISTINE LIPA R3 | |10 CFR SECTION: |TOM KOSHY NRR | |ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION |JOSEPH HOLONICH IRO | |NBNL RESPONSE-BULLETIN | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | IDENTIFICATION OF AXIAL THROUGH-WELD INDICATIONS (REACTOR COOLANT SYSTEM | | PRESSURE BOUNDARY LEAKAGE) ON ONE CONTROL ROD DRIVE MECHANISM NOZZLE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On February 26, 2002, following shutdown for a scheduled refueling outage, | | the Davis-Besse Nuclear Power Station performed a qualified visual | | examination of the Reactor Vessel head per NRC Bulletin 2001-01. This | | examination revealed evidence of boric acid build up around Control Rod | | Drive Mechanism (CRDM) nozzles but was inconclusive due to the previous | | known boric acid deposits. At approximately 1330 hours on February 27, | | 2002, Ultrasonic Testing (UT) data identified axial through weld indications | | on one CRDM. Engineering evaluation of this data confirmed Reactor Coolant | | System pressure boundary leakage exists. Technical Specification 3.4.6.2.a | | states that Reactor Coolant System leakage shall be limited to no pressure | | boundary leakage. As a result this is being reported as a non-emergency, | | 8-hour report in accordance with 10CFR50.72(b)(3)(ii)(a), a condition that | | resulted in the nuclear power plant, including its principal safety barriers | | being seriously degraded." | | | | The licensee stated that UT inspections are continuing on other nozzles. | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38733 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ARIZONA RADIATION REGULATORY AGENCY |NOTIFICATION DATE: 02/27/2002| |LICENSEE: ACS ENGINEERING GROUP, CONSTRUCTION |NOTIFICATION TIME: 16:01[EST]| | CITY: TEMPE REGION: 4 |EVENT DATE: 02/26/2002| | COUNTY: STATE: AZ |EVENT TIME: [MST]| |LICENSE#: 07-422 AGREEMENT: Y |LAST UPDATE DATE: 02/27/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID GRAVES R4 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: NRC REGION 4 | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT REGARDING THE LOSS OF CONTROL AND RECOVERY OF AN ACS | | ENGINEERING GROUP, CONSTRUCTION, MOISTURE/DENSITY GAUGE IN TEMPE, ARIZONA | | | | The following text is a portion of Preliminary Notification PNO-IV-02-013 | | received from NRC Region 4: | | | | "On February 26, 2002, the Arizona Radiation Regulatory Agency (ARRA) | | notified NRC Region IV by facsimile of the loss of control and recovery of a | | portable gauge. The ARRA was informed by the Gilbert, Arizona fire | | department on February 26, 2002, that a Troxler moisture/density gauge, | | Model 2401 (Serial No. MD91 005368) containing a 370 megabecquerel (10 | | millicurie) source of americium-241/beryllium and a 1.48 gigabecquerel (40 | | millicurie) cesium-137 source had been recovered by a motorist that saw the | | device fall off of a truck. The motorist picked up the gauge and turned it | | into the local police department. ARRA determined that the truck was | | operated by two employees of ACS Engineering Group, Construction, an Arizona | | licensee. The gauge was not damaged. The licensee reclaimed the device on | | February 26, 2002. ARRA will be investigating the event. Media interest | | included reports by three local television stations." | | | | "Region IV received notification of this occurrence by facsimile from ARRA | | at 2:35 p.m. (CT) on February 26, 2002. Region IV has informed OEDO, NMSS, | | STP, and OPA." | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021