Event Notification Report for December 18, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/17/2001 - 12/18/2001 ** EVENT NUMBERS ** 38575 38577 38578 38579 . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38575 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/16/2001| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 00:30[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/15/2001| +------------------------------------------------+EVENT TIME: 22:28[EST]| | NRC NOTIFIED BY: ALAN RABENOLD |LAST UPDATE DATE: 12/17/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 | |10 CFR SECTION: | | |ACCS 50.72(b)(2)(iv)(A) ECCS INJECTION | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE REACTOR RECIRCULATION PUMPS DOWN SHIFTED TO SLOW SPEED FOR UNKNOWN | | REASONS RESULTING IN AN AUTOMATIC REACTOR SCRAM, BALANCE-OF-PLANT | | ISOLATIONS, AND EMERGENCY CORE COOLING SYSTEM ACTUATIONS. | | | | At 2228 EST on 12/15/01, the reactor recirculation pumps down shifted to | | slow speed for unknown reasons. This caused reactor pressure vessel (RPV) | | water level to swell, and an automatic reactor scram from 100% power | | occurred when Level 8 was reached. All control rods fully inserted. | | Following the scram, RPV water level started to decrease because the | | feedwater pumps also tripped (as designed) when Level 8 was reached. When | | RPV water level dropped to Level 2 (130 inches), balance-of-plant isolations | | occurred, and all of the applicable valves properly isolated. In addition, | | the high pressure core spray (HPCS) and reactor core isolation cooling | | (RCIC) systems automatically actuated when Level 2 was reached. The HPCS | | and RCIC systems were utilized to restore RPV water level to the normal | | range. | | | | The unit is currently stable in Mode 3 with RPV pressure at 900 psi and RPV | | water level at 210 inches. Normal feedwater is being utilized to maintain | | RPV water level within the proper band, and the HPCS and RCIC systems have | | been secured. The main steam isolation valves remained open, and the | | condenser is being utilized as the heat sink. Containment parameters are | | currently normal, the electrical grid is stable, and the emergency diesel | | generators are available. | | | | The licensee stated that all systems functioned as required and that there | | was nothing unusual or misunderstood other than the cause of the initiating | | event (the recirculation pumps down shifting to slow speed). The licensee's | | investigation is underway. | | | | The licensee notified the NRC resident inspector. | | | | * * * UPDATE AT 1844 EST ON 12/17/01 FROM DAVID GUDGER TO S. SANDIN * * * | | | | "This notification is a follow-up to the notification provided on | | 12/16/01." | | | | "The following is a description of the sequence of plant events that | | occurred as determined by the failure analysis." | | | | "Initial conditions: Feedwater level control was on Master Level controller | | selected to the 'B' narrow range channel and the plant was operating at 100% | | power. Due to the level summer card 1C34K657 failure, the level signal from | | the selected channel rapidly decreased to less than 178 inches, Level 3 (L3) | | signal, which caused the reactor recirculation pumps to receive a | | fast-to-slow speed downshift. Simultaneously, feedwater flow rapidly | | increased in response to the low level on the 'B' channel. The feedwater | | pumps tripped at 219 inches, Level 8 (L8), which occurred due to swell from | | the recirculation pumps downshift and increased feedwater flow. The [motor | | feed pump (MFP)] did not automatically start due to the L8 signal (as | | designed) and level decreased to 130 inches, Level 2 (L2). The | | recirculation pumps tripped, and [the] HPCS and RCIC systems [automatically] | | started and restored level. The MFP L8 signals were reset, and level was | | controlled on the startup controller." | | | | "The Reactor Water Cleanup Inboard Containment Isolation Valve failed to | | close as designed upon [the] L2 isolation signal. The valve was manually | | closed during containment valve isolation verification following the scram. | | The cause of the failure to close was determined to be relay failure. Two | | relays were subsequently replaced and retested satisfactorily." | | | | The licensee informed the NRC resident inspector. The NRC operations | | officer notified the R3DO (Phillips). | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38577 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 12/17/2001| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 09:58[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 11/20/2001| +------------------------------------------------+EVENT TIME: 03:25[EST]| | NRC NOTIFIED BY: JIM TURKETT |LAST UPDATE DATE: 12/17/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHARLES R. OGLE R2 | |10 CFR SECTION: | | |AINV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INADVERTENT START OF A MOTOR-DRIVEN EMERGENCY FEEDWATER PUMP (60-Day | | Report) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "During the performance of a surveillance test, the 'B' Motor-Driven | | Emergency Feedwater (EFW) pump was inadvertently started from the Main | | Control Board when the intended action was to place the control switch in | | the pull-to-lock position. The plant was preparing to test the function of | | the solid state output relay K633 as it pertains to sending an open signal | | to the EFW flow control valves IFV03531, IFV03541, and IFV03551. To prevent | | actually injecting EFW into the [steam generators (S/G)], the pump for the | | train whose relay is being tested (in this case 'B') must be placed in | | pull-to-lock since the same relay which opens the IFVs also starts the | | pump." | | | | "When the BOP operator attempted to place the pump in P-T-L the pump | | started. This was immediately recognized as an unexpected response, and the | | pump was shut off within a second. Due to the start of the EFW pump, S/G | | blowdown isolated as per design and had to be subsequently realigned. [Data | | from the] plant computer and alarm printers [was] reviewed by the Shift | | Supervisor and [Shift Engineer] to determine if any cold EFW actually | | entered the S/Gs. The alarm printer showed 1 second between pump start and | | pump stop, which is consistent with the prompt error recognition observed by | | the crew. The plant computer data showed no increase in EFW flow during the | | time period in question. It is believed from this investigation that the | | pump never came up to speed to the point where sufficient pressure was | | developed to swing open the discharge check valves, thus no EFW injection | | occurred. The cause of this event is attributed to human performance | | error." | | | | "This event does not require a telephone notification under | | 10CFR50.72(b)(3)(iv)(A) because this is being reported as an invalid ECCS | | actuation of an Emergency Feedwater Pump. However, the plant is making this | | call under the criteria of 10CFR50.73(a)(1) in lieu of submitting an LER | | under 10CFR50.73(a)(2)(iv)." | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38578 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 12/17/2001| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 10:39[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/17/2001| +------------------------------------------------+EVENT TIME: 08:00[CST]| | NRC NOTIFIED BY: GREG BAKER |LAST UPDATE DATE: 12/17/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 95 Power Operation |95 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SIGNIFICANT FITNESS-FOR-DUTY EVENT UNDER BRAIDWOOD PROGRAM SEC-1.10 | | | | A non-licensed supervisor tested positive based on a for-cause test due to | | the odor of alcohol. The individual was immediately escorted out of the | | Protected Area, and the individual's access has been suspended. (Call the | | NRC operations officer for additional details and for the Security Manager's | | telephone number.) | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38579 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 12/17/2001| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 16:17[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 12/17/2001| +------------------------------------------------+EVENT TIME: 15:30[EST]| | NRC NOTIFIED BY: DARON ZAKARIAN |LAST UPDATE DATE: 12/17/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |10 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR REPORT DUE TO POTENTIAL OPERATION IN EXCESS OF OPERATING LICENSE | | CONDITION 2.C(1) | | | | "After restart of Hope Creek from RF10, analysis of plant parameters | | indicated that changes occurred in the final feedwater temperature since the | | previous operating cycle. The temperatures as indicated by temperature | | loops 1AETE-N041A/B/C/D, were approximately 3 degrees lower than when | | operating at 100 percent power prior to the outage. This indicates that | | actual power may have been below 100 percent of last cycle operation. Other | | parameters, such as First Stage pressure, main turbine control valve | | position, #6 Feedwater Heater shell pressure, feed pump discharge flow, | | condensate pump flow, were also lower, substantiating that power was lower | | than previous cycle. Performance Engineering notified Design Engineering of | | this condition. Design Engineering then initiated a complete review of | | related documentation. | | | | "During Hope Creek RF9 (May 2000), the main feedwater temperature loops | | required recalibration to support power up-rate. The traditional method to | | determine the RTD curve introduced a +1 degree F bias. This was | | non-conservative, in that power level was higher than calculated by the | | plant computer. In January of 2001, crossflow was implemented to correct | | for fouling of the venturis. In October 2001, a non-conservative moisture | | carryover fraction was used in the core thermal power calculation as | | reported in Hope Creek Special Report 354/2001-003-00. As a result of these | | conditions, Hope Creek Generating Station has potentially operated at power | | levels in excess of Operating License Condition 2.C(1), which requires that | | the facility be operated at reactor core power levels not in excess of 3339 | | MWt. The upper limit may have been exceeded by significantly less than | | 0.1%. This potential overpower condition existed between the time of | | crossflow implementation and RF10. | | | | "This notification is being made in accordance with Hope Creek Operating | | License Condition 2.F, as a potential violation of Hope Creek Operating | | License Condition 2.C(1). | | | | "The moisture carryover fraction was corrected during RF10. During the | | recent forced outage, the 4 RTDs were checked and all four loops were | | calibrated, therefore, eliminating the potential for operating above 100% | | power." | | | | The period of time during which the unit may have operated in this condition | | occurred between August 1, 2001, and October 10, 2001. The corrective | | action involving calibration of the 4 RTDs was completed last week. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ .
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021