Event Notification Report for December 11, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/10/2001 - 12/11/2001 ** EVENT NUMBERS ** 38029 38553 38554 38555 38556 . !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38029 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 05/24/2001| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 21:50[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/24/2001| +------------------------------------------------+EVENT TIME: 18:09[CDT]| | NRC NOTIFIED BY: MIKE HAUNER |LAST UPDATE DATE: 12/10/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |SONIA BURGESS R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 1 Startup |1 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI DECLARED INOPERABLE | | | | "During a reactor startup following a refueling outage, HPCI was declared | | inoperable and is reportable under 50.72(b)(3)(v)(D) and 50.72(b)(3)(vi) as | | a single failure. | | | | "Upon completion of HPCI system operability testing, it was discovered that | | the HPCI system flow controller indicated approximately 500 GPM verses an | | expected 0 GPM. Since the plant is in MODE 2 and reactor pressure is greater | | than 150 PSIG, HPCI was declared inoperable and a 14-day LCO was entered per | | TS 3.5.1, condition F. | | | | "The preliminary investigation results are that air in the HPCI system flow | | transmitter sensing lines is causing the erroneous flow indication. | | Troubleshooting efforts are in progress." | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | ***** RETRACTION FROM JOHN KARRICK TO LEIGH TROCINE AT 1536 EDT ON 12/10/01 | | ***** | | | | The following text is a portion of a facsimile received from the licensee: | | | | "This is a retraction of event number 38029 from May 24, 2001. The initial | | report involved an erroneous reading on the flow-indicating controller | | (FIC-2309) for the HPCI system. At the time of the discovery, the | | consequence of FIC-2309 reading high was believed to be a non-conservative | | speed demand signal to the HPCI turbine such that the actual HPCI injection | | flow would fall short of that required (assuming an auto start with no | | operator action). As a result, HPCI was declared inoperable and a report | | was made. A calculation has since concluded that actual HPCI operability | | would not have been lost given the as-found condition. Also, the quarterly | | surveillance test to prove HPCI operability had just been successfully | | completed. During the time HPCI was considered inoperable, it remained | | available for use (as documented in Operator logs). Therefore, there was no | | actual loss of HPCI as a single train safety system and there was no event | | or condition that could have prevented safety function fulfillment. This | | event is being retracted. A formal cancellation letter to withdraw the LER | | (331/2001-002) is also being mailed." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R3DO (Anne Marie Stone). | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38553 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 12/10/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 11:53[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 12/10/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 03:48[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 12/10/2001| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |ANNE MARIE STONE R3 | | DOCKET: 0707001 |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MATT MAURER | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |OCBA 76.120(c)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INADVERTENT LOSS OF POWER TO THE C-315 TAILS WITHDRAWAL BUILDING DURING AN | | IMPROPERLY PERFORMED POWER SWITCHING EVOLUTION (24-Hour Report) | | | | The following text is a portion of a facsimile received from the Paducah: | | | | "At 0348 CST on 12-10-01, 480-volt power was inadvertently lost to the C-315 | | tails withdrawal building during an improperly performed power switching | | evolution. As a result of the power loss, the high voltage UF6 release | | detection system for the UF6 condensers, accumulators, and heated housings | | was rendered inoperable for approximately 10 minutes. The high voltage UF6 | | release detection system is required to be operable per TSR 2.3.4.4. The | | function of the high voltage UF6 release detection system is to detect UF6 | | releases and to sound an alarm in the local control room. The power loss | | also caused the withdrawal systems to shut down and automatically isolate as | | designed. No UF6 releases occurred as a result of this evolution. Power | | was restored and the building was returned to normal operation." | | | | "This event is reportable under 10 CFR 76.120(c)(2) as an event in which | | equipment required by the TSR is disabled or fails to function as | | designed." | | | | Paducah personnel notified the NRC resident inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38554 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 12/10/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 11:58[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 10/29/2001| +------------------------------------------------+EVENT TIME: 01:21[EST]| | NRC NOTIFIED BY: ANDY HALLIDAY |LAST UPDATE DATE: 12/10/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CLIFFORD ANDERSON R1 | |10 CFR SECTION: | | |AINV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 66 Power Operation |66 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INVALID PRIMARY AND SECONDARY CONTAINMENT ISOLATION DUE TO LOSS OF POWER TO | | A REACTOR PROTECTION SYSTEM POWER DISTRIBUTION BUS (60-Day Report in | | Accordance with 10CFR50.73(a)(1)) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Event Description" | | | | "At 0121 hours on October 29, 2001, with the plant operating at 66 percent | | of rated thermal power, power was lost to Reactor Protection System (RPS) | | power distribution bus B as a result of an Electrical Protective Assembly | | (EPA) logic card failure." | | | | "The power sources for the RPS provide power to both the RPS and the Primary | | Containment Isolation System (PCIS) logic circuits. Loss of power to RPS | | power distribution bus B resulted in invalid actuation of RPS trip system B | | and [PCIS] trip system B. The RPS trip was a partial actuation (a 'half | | scram'), and the PCIS trip was also a partial actuation (a 'half | | isolation')." | | | | "The portions of PCIS logic that are designed with separate 'inboard' and | | 'outboard' logic had the 'outboard' logic de-energized due to the power | | loss. This resulted in the automatic closure of the outboard primary | | containment isolation valves [...] for the: drywell pressure sensing line, | | pressure suppression chamber pressure sensing line, Reactor Water Cleanup | | system pump suction line, Reactor Water Cleanup system return line, and | | reactor water sample line." | | | | "The de-energized PCIS logic circuits also initiated automatic closure of | | Reactor Building (Secondary Containment) ventilation system outboard supply | | and exhaust isolation valves and automatically started Standby Gas Treatment | | (SGT) subsystem B, as designed, to maintain the reactor building atmosphere | | at a slightly negative pressure." | | | | "Operating personnel restored power to RPS power distribution bus B by | | transferring to the alternate power source. The invalid PCIS and RPS trip | | signals that were caused by the loss of power were reset, systems that | | isolated were restored to service, reactor building ventilation was restored | | to normal, and SGT subsystem B was restored to a normal standby status." | | | | "Actions Taken" | | | | "1. RPS power distribution bus B was energized from the alternate power | | source." | | | | "2. RPS and PCIS logic systems were reset." | | | | "3. The affected systems were restored to normal." | | | | "4. Troubleshooting of a logic card associated with the tripped EPA circuit | | breaker revealed a failed capacitor. The failed logic card was replaced | | with a refurbished logic card from stock." | | | | "5. Power to RPS power distribution bus B was transferred back to the | | normal (motor generator) source." | | | | "6. New capacitors will be installed on the logic cards, or refurbished | | logic cards will be installed, in the subject EPAs during the next available | | maintenance window." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38555 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 12/10/2001| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 18:40[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 12/10/2001| +------------------------------------------------+EVENT TIME: 12:00[CST]| | NRC NOTIFIED BY: TOM OSELAND |LAST UPDATE DATE: 12/10/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT STANDBY LIQUID CONTROL SYSTEM RELIEF VALVES MAY | | INTERMITTENTLY LIFT DURING THE MOST LIMITING ATWS TRANSIENTS (Refer to | | event #38556 for a similar notification received from Dresden Unit 3.) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "While performing calculations associated with the power uprate project, | | Quad Cities Nuclear Power Station determined that the Standby Liquid Control | | (SLC) system relief valves on Unit 1 and Unit 2 may intermittently lift | | during the most limiting ATWS [transients. (The] specific scenario | | evaluated is a Main Steam Line isolation at rated power with failure of the | | normal, backup, and alternate rod insertion (ARI) scram functions.) This | | issue also applies to the current rated power level during two-pump SLC | | operation. Title 10 of the Code of Federal Regulations, subpart 50.62, | | requires the SLC system to inject the equivalent of 86 gpm of 13-weight | | percent sodium pentaborate solution. While the relief valve was lifted, the | | system flow rate would not meet the required equivalent flow rate into the | | vessel. Therefore, this condition is not in direct compliance with 10 CFR | | 50.62. The NRC communicated a similar industry issue in Information Notice | | 2001-13." | | | | "Further plant specific analysis has demonstrated that an adequate volume of | | boron would be injected to shut down the reactor and meet the appropriate | | acceptance criteria including reactor pressure, peak cladding temperature, | | peak suppression pool temperature, and peak containment pressure. For these | | reasons, the safety significance of this event is minimal." | | | | "This phone call is being made as an informational call. Written | | communications, as appropriate, will be submitted to provide additional | | detail. The station will continue to communicate additional information | | with the NRC resident inspectors and with Region Ill as it is identified." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38556 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 12/10/2001| | UNIT: [] [] [3] STATE: IL |NOTIFICATION TIME: 18:49[EST]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 12/10/2001| +------------------------------------------------+EVENT TIME: 12:00[CST]| | NRC NOTIFIED BY: BOB SCOTT |LAST UPDATE DATE: 12/10/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT STANDBY LIQUID CONTROL SYSTEM RELIEF VALVES ON UNIT 3 MAY | | INTERMITTENTLY LIFT DURING THE MOST LIMITING ATWS TRANSIENTS (Refer to | | event #38555 for a similar notification received from Quad Cities.) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "While performing calculations associated with the power uprate project, | | Dresden Nuclear Power Station determined that the Standby Liquid Control | | (SLC) system relief valves on Unit 3 may intermittently lift during the most | | limiting ATWS [transients. (The] specific scenario evaluated is a Main | | Steam Line isolation at rated power with failure of the normal, backup, and | | alternate rod insertion (ARI) scram functions.) This issue also applies to | | the current rated power level during two pump SLC operation. Title 10 of | | the Code of Federal Regulations, subpart 50.62, requires the SLC system to | | inject the equivalent of 86 gpm of 13-weight percent sodium pentaborate | | solution. While the relief valve was lifted, the system flow rate would not | | meet the required equivalent flow rate into the vessel. Therefore, this | | condition is not in direct compliance with 10 CFR 50.62. The NRC | | communicated a similar industry issue in Information Notice 2001-13" | | | | "Further plant specific analysis has demonstrated that an adequate volume of | | boron would be injected to shut down the reactor and meet the appropriate | | acceptance criteria including reactor pressure, peak cladding temperature, | | peak suppression pool temperature, and peak containment pressure. For these | | reasons, the safety significance of this event is minimal." | | | | "This phone call is being made as an informational call. Written | | communications, as appropriate, will be submitted to provide additional | | detail. The station will continue to communicate additional information | | with the NRC resident inspectors and with [NRC] Region Ill as it is | | identified." | | | | The licensee stated that although Dresden Units 2 and 3 are similar vintage | | boiling water reactors, this issue does not apply to Dresden Unit 2 because | | the piping runs are different. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ .
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021