Event Notification Report for October 1, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/28/2001 - 10/01/2001 ** EVENT NUMBERS ** 38183 38326 38328 38329 38330 38332 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38183 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 08/02/2001| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 19:17[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 08/02/2001| +------------------------------------------------+EVENT TIME: 15:00[EDT]| | NRC NOTIFIED BY: TIM RIEGER |LAST UPDATE DATE: 09/28/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CLIFFORD ANDERSON R1 | |10 CFR SECTION: |HERB BERKOW NRR | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANALYZED CONDITION INVOLVING SEISMIC EVENT DISCOVERED DURING ENGINEERING | | REVIEW | | | | "On August 2, 2001, at approximately 1500 hours, Engineering notified | | operations that the Service Water (SW) System may not meet analyzed flow | | requirements after a seismic event as a result of a system re-alignment | | change implemented June 4, 2001. The SWS re-alignment change placed an 8 | | inch non-seismic SW line on the essential SW header. The SWS was originally | | analyzed for a seismic event with the break of a 10 inch non-seismic SW | | line. The change evaluation concluded that this configuration was bounding | | for the alignment. The assessment of the alignment change did not adequately | | consider the effects of the seismic event. After a review of the change, | | Engineering judged that the SWS would not meet system design flow | | requirement after a seismic event with two out of three pumps due to the | | failure of both non-seismic lines that were aligned as a result of the | | change. Operations initiated realignment of the 8 inch SW line back to the | | non-essential header which was completed at 1640 hours. Engineering is | | performing evaluations but judged that the SWS would have met flow | | requirements for plant shutdown with three SW pumps operable after a seismic | | event with no random single failure (three pumps operable)." | | | | The licensee will inform the NRC resident inspector. | | | | **** RETRACTION ON 09/28/01 AT 1002 HOURS BY TIM RIEGER TAKEN BY MACKINNON | | **** | | | | Upon further assessment, the re-alignment condition is not considered | | reportable. Additional engineering reviews showed that the alignment to the | | non-seismic SW lines to the Essential header was not risk significant. | | Engineering judgement and analysis concluded that the plant design basis | | events, including the seismic event, would not cause a consequential loss of | | the non-seismic lines aligned to the Essential header. Therefore, the | | condition did not significantly degrade plant safety and although at the | | time was unanalyzed, the condition does not meet reporting requirements. As | | part of Indian Point 3's corrective action program, the cause and extent of | | condition of the event is being evaluated and identified corrective actions | | will be performed. R3DO (John Kinneman) notified. | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38326 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NE DIV OF RADIOACTIVE MATERIALS |NOTIFICATION DATE: 09/28/2001| |LICENSEE: THOMPSON DREESSEN DORNER INC. |NOTIFICATION TIME: 11:43[EDT]| | CITY: SPRINGFIELD REGION: 4 |EVENT DATE: 09/27/2001| | COUNTY: STATE: NE |EVENT TIME: 13:00[CDT]| |LICENSE#: 01-7001 AGREEMENT: Y |LAST UPDATE DATE: 09/28/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GREG PICK R4 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOHN FASSELL | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DENSITY GAUGE SOURCE ROD BROKEN OFF | | | | A Humboldt Model # 5001gauge was run over by a 50-ton blader vehicle. The | | density gauge source rod was broken off, and the gauge itself was flattened. | | The blader vehicle ran over the density gauge in a landfill while the person | | who was assigned to guard the gauge had his back turned. The source was in | | its stored position when it was run over by the blader vehicle. There was | | no contamination on the blader vehicle and no radioactive release from the | | gauge. The Humboldt Model # 5001 has 8 mCi of cesium-137 and 40 mCi of | | americium-241/beryllium. The owner of the gauge is Thompson Dreessen Dorner | | Inc., which is located in Omaha. | | | | (Call the NRC operations officer for State contact information.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38328 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: US ARMY |NOTIFICATION DATE: 09/28/2001| |LICENSEE: US ARMY |NOTIFICATION TIME: 13:34[EDT]| | CITY: ABERDEEN PROVING GROUNDS REGION: 1 |EVENT DATE: 09/28/2001| | COUNTY: STATE: MD |EVENT TIME: 12:07[EDT]| |LICENSE#: 19-30563-01 AGREEMENT: Y |LAST UPDATE DATE: 09/28/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN KINNEMAN R1 | | |MONTE PHILLIPS R3 | +------------------------------------------------+FRED BROWN NMSS | | NRC NOTIFIED BY: JOYCE KUYKENDAL | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING CHEMICAL AGENT DETECTOR CONTAINING 30 MICROCURIES OF AMERICIUM-241 | | | | A chemical agent detector (CAD) containing 30 microcuries of americium-241 | | was discovered to be missing during a physical inventory conducted during | | 08/01. A search was performed at all units, and the US Army Aberdeen | | Proving Ground in Maryland was notified of the missing CAD at 1207 on | | 09/28/01. It is believed that the CAD may have been last used by the | | Wisconsin Army National Guard located in Black River Falls during nuclear | | biological chemical (NBC) training. | | | | (Call the NRC operations officer for licensee contact information.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38329 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/28/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:11[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/28/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:20[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/28/2001| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MONTE PHILLIPS R3 | | DOCKET: 0707002 |PATRICIA HOLAHAN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING AN OPACITY VIOLATION (4-hour Report) | | | | The following text is a portion of a facsimile received from Portsmouth | | personnel: | | | | "At 1520 hours [on] 09/28/01, the Ohio Environmental Protection Agency | | (OEPA) was notified per Ohio Administrative Code (OAC) 3745-15-06(B) that an | | opacity exceedance had occurred at the X-600 Steam Plant. The opacity | | violation occurred on [the] #2 Boiler when our #2A Precipitator voltages | | began to fluctuate. Operators adjusted load/air requirements on the #2 | | Boiler in an effort to prevent further exceedances. [The] cause of the | | voltage fluctuations has not been determined at this time." | | | | "This is reportable as a 4-hour NRC Event due to notification to an outside | | agency (OEPA) being made per Nuclear Regulatory Reporting Procedure | | UE2-RA-RE1030, Appendix D, Criteria P (Miscellaneous)." | | | | Portsmouth personnel notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38330 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 09/28/2001| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 18:39[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 09/28/2001| +------------------------------------------------+EVENT TIME: 16:25[EDT]| | NRC NOTIFIED BY: MIKE PHILIPPON |LAST UPDATE DATE: 09/28/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL MAXIMUM POWER LEVEL VIOLATION | | | | The following text is a portion of a facsimile received from the licensee: | | | | "This report is being made in accordance with Fermi 2 License Condition 2.F, | | as a potential violation of the Maximum Power Level of 3430 MWth as | | described in License Condition 2.C(1)." | | | | "GE report titled, 'Impact of Steam Carryover Fraction on Process Computer | | Heat Balance Calculations, September 2001,' documents a non-conservative | | assumption for moisture [carryover] used in the calculation of core thermal | | power. The assumed carryover fraction of .1% was discovered to be closer to | | 0.0% (non-conservative) in later model GE BWRs." | | | | "An initial review at Fermi 2 was completed at 1625 on 09/28/01. The | | initial review indicated that Fermi is susceptible to the non-conservative | | core thermal power calculation, with an estimated bias of 1.64 MWth. This | | initial analysis was based on a carryover test performed in 1996 at Fermi | | 2." | | | | "Fermi 2 has an administrative 8-hour average power limit of 3428.8 MWth. | | Given the 1.64 MWth bias, it is possible that the license limit of 3430 MWth | | has been exceeded in the past. Fermi 2 took immediate action to reduce the | | administrative power limit to 3427 MWth. Reactor power was reduced by 3 | | MWth." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38332 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 09/30/2001| | UNIT: [] [] [3] STATE: AZ |NOTIFICATION TIME: 20:28[EDT]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 09/30/2001| +------------------------------------------------+EVENT TIME: 14:00[MST]| | NRC NOTIFIED BY: STEVE BANKS |LAST UPDATE DATE: 09/30/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |GREG PICK R4 | |10 CFR SECTION: |JOHN ZWOLINSKI NRR | |ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N N 0 Cold Shutdown |0 Cold Shutdown | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EVIDENCE OF REACTOR COOLANT SYSTEM PRESSURE BOUNDARY LEAKAGE DISCOVERED | | WHILE IN COLD SHUTDOWN. | | | | The following text is a portion of a facsimile received from the licensee: | | | | "The following event description is based on information currently | | available. If through subsequent reviews of this event, additional | | information is identified that is pertinent to this event or alters the | | information being provided at this time, a follow-up notification will be | | made via the ENS or under the reporting requirements of 10CFR50.73." | | | | "On September 30, 2001, at approximately 1400 MST, Palo Verde Nuclear | | Generating Station (PVNGS) Unit 3 discovered evidence of reactor coolant | | system (RCS) pressure boundary leakage. PVNGS Unit 3 was shutdown in Mode 5 | | conducting cooldown and depressurization in its [ninth] refueling outage at | | the time of discovery. Current RCS temperature is approximately 135 degrees | | Fahrenheit and RCS pressure is approximately 20 psia." | | | | "The leakage was discovered at two [Inconel] alloy 600 nozzle locations | | during inservice inspection (ISI); one in a RCS hot leg temperature detector | | nozzle and another in a pressurizer heater sleeve. The RCS hot leg leakage | | is located in the RTD nozzle for an inservice temperature [detector] (Loop | | #1, Equipment ID: 3JRCETW112HD). The pressurizer heater sleeve leakage is | | located at pressurizer heater B17. The leakage was identified in the form | | of small deposits of boron accumulation around the circumferences of the hot | | leg nozzle and that of the pressurizer sleeve. PVNGS has conducted | | inspections of these nozzles [and] sleeves during each refueling outage | | since the discovery that Inconel alloy 600 nozzles are susceptible to axial | | cracking. No evidence of leakage was identified when inspected during the | | last refueling outage approximately 18 months ago." | | | | "The timing of this ENS report was based on the determination at 14:00 MST | | on September 30, 2001, that the boron accumulation represented a serious of | | a principle safety barrier. PVNGS Unit 3 Technical Specification Limiting | | Condition for Operation (LCO) 3.4.14 (RCS Operational Leakage) permits no | | reactor coolant system pressure boundary leakage. It was therefore | | conservatively concluded that any evidence of pressure boundary leakage, | | regardless of magnitude, represents serious degradation of a principle | | safety barrier. Technical Specification [LCO] 3.4.14 is applicable in Modes | | 1, 2, 3, and 4. Unit 3 was in Mode 5 in a planned refueling outage at the | | time of discovery; therefore, LCO 3.4.14 is currently not applicable. | | The-hot leg nozzle and pressurizer sleeve will be repaired prior to | | re-entering Mode 4. It is anticipated that the repair will be utilizing the | | Mechanical Nozzle Seal Assembly (MNSA). No ESF actuations occurred and none | | were required. No structures systems or components were inoperable that | | contributed to this event particularly the fuel cladding and the containment | | fission product barriers. The event did not result in the release of | | radioactivity to the environment and did not adversely affect the safe | | operation of the plant or the health and safety of the public." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021