Event Notification Report for September 21, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/20/2001 - 09/21/2001 ** EVENT NUMBERS ** 38263 38300 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38263 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATTS BAR REGION: 2 |NOTIFICATION DATE: 09/04/2001| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 16:54[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/04/2001| +------------------------------------------------+EVENT TIME: 13:04[EDT]| | NRC NOTIFIED BY: RODEN |LAST UPDATE DATE: 09/20/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN MONNINGER R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR MANUALLY TRIPPED FROM 100% POWER DUE TO STEAM GENERATOR LEVEL | | APPROACHING THE LO-LO LEVEL SETPOINT | | | | While operating at 100% power, the Watts Bar Unit 1 reactor was manually | | tripped at approximately 1304 EDT on September 4, 2001 due to steam | | generator (SG) level approaching the Lo-Lo level setpoint. Just prior to | | the manual trip of the reactor, an abnormal voltage alarm was received on | | 125V Vital Battery Board 1-1. The immediate cause of the trip is considered | | to be the loss of the 1-1 Vital AC Inverter which caused a feedwater | | regulating valve to close. Subsequently, the maintenance power supply was | | used to restore power to the 1-1 vital AC bus. | | | | All control rods inserted properly in response to the reactor trip. The | | Auxiliary Feedwater (AFW) System actuated as expected. However, subsequent | | to the initial actuation signal, additional operator action was required | | to[manually] start 1B motor driven pump. After the 1B pump was | | successfully started, the motor driven AFW pump 1A was secured based on | | instrument indications available to the operating staff. After power was | | restored to the vital AC bus, the 1A pump was subsequently started and | | performed properly. Inspections are currently underway to determine the | | exact cause of the loss of the 1-1 Vital Inverter and basis for the 1B pump | | failing to [auto] start. | | | | No ECCS injection occurred, but the steam generator atmospheric relief | | valves lifted and fully reseated. | | | | The manual actuation of the Reactor Protection System (RPS) is being | | reported as a four hour report under 10 CFR 50.72 (b)(2)(iv). The actuation | | of the Auxiliary Feedwater System (an engineered safety feature) is being | | reported as an eight hour report under 10 CFR 50.72 (b)(3)(iv). | | | | The plant is stable in mode 3. | | | | The NRC Resident Inspector was notified. | | | | * * * UPDATE 1244EDT ON 9/20/01 FROM CHARLES TOUCHSTONE TO S. SANDIN * * * | | | | The following information was received as an update: | | | | "This report supplements the report made by TVA at approximately 1654 on | | September 4, 2001 - NRC Event Report 38263. | | | | "Description of Event: | | | | "While operating at 100% power, the Watts Bar Unit 1 reactor was manually | | tripped at approximately 1305 EDT on September 4, 2001, due to the level of | | Steam Generator (SG) Number 1 approaching the low-low level setpoint. The | | immediate cause of the trip is considered to be the loss of the 1-I Vital AC | | Inverter which caused the Number 1 SG feedwater regulating valve to close. | | Subsequently, the maintenance power supply was used to restore power to the | | 1-I Vital AC board. | | | | "10 CFR 50.72 Notification: | | | | "Initial notification to NRC of the reactor trip was made by WBN Operations | | at 1654 EDT The manual actuation of the Reactor Protection System (RPS) was | | reported as a four hour report under 10 CFR 50.72 (b)(2)(iv). The actuation | | of the Auxiliary Feedwater System (an engineered safety feature) was | | reported as an eight hour report under 10 CFR 50.72 (b)(3)(iv). This report | | supplements the initial report and is being reported under the same | | criteria. | | | | "Cause of the Event: | | | | "The root cause of the reactor trip was the failure of the sensing/current | | limiting card installed in vital battery charger 6-S or its associated edge | | connector. The failure of the component resulted in the DC output of the | | charger rising to 209V. The high DC output voltage resulted in a high input | | to inverters 1-I and 2-I. Inverter 1-I input and output fuses were blown, | | while inverter 2-I continued without failure. This occurred because inverter | | 1-I is equipped with parallel 5 and 15 KVA constant voltage transformers | | (CVTs), which are more sensitive to high input voltage than the type used in | | inverter 2-1 which utilizes a single 20 KVA CVT. The inverters are rated for | | a maximum input of 140 volts. | | | | "Equipment Response: | | | | "All control rods inserted properly in response to the reactor trip. For | | WBN, the AFW system consist of a turbine driven AFW (TDAFW) pump and two | | trains (Train A and Train B) of motor driven AFW (MDAFW) pumps. The design | | calls for the MDAFW arid TDAFW pumps to start due to the loss of both Main | | Feedwater (MFW) pumps or an AMSAC actuation, In addition, the MDAFW pumps | | will actuate on low-low S/G level in any S/G and the TDAFW pump will actuate | | on low-low level in any two S/Gs. For this event, actuation of the TDAFW | | pump resulted from the required logic being met for SGs Number 1 and 4. | | Based on data obtained subsequent to the reactor trip, an auto start for the | | TDAFW train was initiated immediately after S/G low-low level setpoints were | | met. | | | | "Subsequent to the initial AFW actuation signal, additional operator action | | was required to start the 1A-A and 1B-B motor driven pumps. For the Train A | | MDAFW, the pump did not receive an auto start signal due to the loss of | | Vital Board 1-I. This resulted from the power for the signal generating | | circuit being lost with the Vital Board. The evaluation performed to | | establish the cause for the Train B MDAFW not starting found that the | | breaker for the pump did not close as a result of the automatic signal | | initiated by the low SG level. The breaker was subsequently tested and | | performed as designed and therefore, no conclusive cause was found for the | | breaker not closing. However, it was established that the most likely cause | | of the problem was dirty relay contacts on the 1X and 30RX relays." | | | | The licensee informed the NRC resident inspector. Notified R2DO(Sparks). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38300 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 09/20/2001| |LICENSEE: STEVEN RAAS AND ASSOCIATES, INC. |NOTIFICATION TIME: 15:15[EDT]| | CITY: WATSONVILLE REGION: 4 |EVENT DATE: 09/19/2001| | COUNTY: STATE: CA |EVENT TIME: 16:30[PDT]| |LICENSE#: 5214 AGREEMENT: Y |LAST UPDATE DATE: 09/20/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN PELLET R4 | | |SUSAN FRANT NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT GREGER | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING A DAMAGED TROXLER GAUGE | | | | "A Troxler model 3401B moisture density gauge (serial #016692) was run over | | by earth moving/compacting equipment while the gauge was in use (i.e., the | | source rod was extended). The source rod was bent such that the source could | | not be retracted into the shielded position. The unshielded source contained | | nominally 10 mCi of Cs-137. The source rod was cut by the fire department | | with the source in a lead 'pig' provided by the UC Santa Cruz health physics | | program. The source and the gauge housing will be sent to Troxler for | | repairs." | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021