The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for August 3, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           08/02/2001 - 08/03/2001

                              ** EVENT NUMBERS **

38179  38180  38181  38182  38183  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38179       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PRAIRIE ISLAND           REGION:  3  |NOTIFICATION DATE: 08/01/2001|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 09:05[EDT]|
|   RXTYPE: [1] W-2-LP,[2] W-2-LP                |EVENT DATE:        08/01/2001|
+------------------------------------------------+EVENT TIME:        07:01[CDT]|
| NRC NOTIFIED BY:  BRUCE ANDERSON               |LAST UPDATE DATE:  08/02/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |PATRICK HILAND       R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |
|AESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC REACTOR TRIP DUE TO NEGATIVE FLUX RATE                             |
|                                                                              |
| The unit automatically tripped from 100%; the first out annunciator was Flux |
| Rate Reactor Trip.  Immediately following the trip, the rod position         |
| indicator showed that five control rods did not insert completely. The stuck |
| control rods indicated 15-20 steps out from bottom. Operators entered their  |
| reactor trip/safety injection emergency procedure (1E0), but were able to    |
| transition to the trip recovery procedure (1ES0.1). One of the stuck control |
| rods subsequently indicated full insertion. The unit is currently stable in  |
| Mode 3. Operators are emergency borating the reactor per 1ES0.1 a total of   |
| 1000 gallons (250 gallons per stuck rod). The licensee is continuing their   |
| trip recovery.  Preliminary investigation indicates a problem with the rod   |
| control system may have led to one or more dropped control rods.             |
|                                                                              |
| The NRC resident inspector has been informed of this event by the licensee.  |
|                                                                              |
| * * * UPDATE 1025 EDT 8/1/01 FROM DAMMANN TAKEN BY JONES * * *               |
|                                                                              |
| The licensee reported that the auxiliary feedwater (AFW) system (pumps 11    |
| and 12) automatically actuated on steam generator low-low level following    |
| the trip, as expected.  In addition, two of the stuck rods are now           |
| indicating full insertion. The NRC resident inspector has been informed of   |
| this update.                                                                 |
|                                                                              |
| * * * UPDATE 1624 EDT 08/01/01 FROM GOSMAN TAKEN BY MACKINNON * * *          |
|                                                                              |
| After interviewing the Reactor Operators it was determined that 6 rod bottom |
| lights did not immediately come on after the reactor trip.  Also a media     |
| press release will be made concerning this event.  R3DO (John Madera)        |
| notified.                                                                    |
|                                                                              |
| The NRC resident inspector was notified of this update by the licensee.      |
|                                                                              |
| * * * UPDATE 0431 EDT 8/2/01 FROM IRVIN TAKEN BY STRANSKY * * *              |
|                                                                              |
| "Investigation into the cause of the reactor trip has determined that        |
| control rods associated with Rod Control Power Cabinet 2AC began to insert   |
| into the core. As designed, the reactor protection system actuated to insert |
| the remaining control rods.                                                  |
|                                                                              |
| "In accordance with procedures, operators verified the reactor had safely    |
| shutdown. However, indicator lights for six of twenty-nine individual        |
| control rods did not indicate that the rods had fully inserted. This         |
| situation is addressed in the reactor trip procedure and the operators       |
| responded appropriately by borating to compensate.                           |
|                                                                              |
| "Control rod drop testing has been performed and has verified that all       |
| control rods fully inserted. Individual rod position indication calibration  |
| check is in progress."                                                       |
|                                                                              |
| The NRC resident inspector will be informed of this update by the licensee.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   38180       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  NTH CONSULTANTS                      |NOTIFICATION DATE: 08/02/2001|
|LICENSEE:  NTH CONSULTANTS                      |NOTIFICATION TIME: 08:49[EDT]|
|    CITY:  FARMINGTON HILLS         REGION:  3  |EVENT DATE:        08/02/2001|
|  COUNTY:                            STATE:  MI |EVENT TIME:        07:50[EDT]|
|LICENSE#:  21-14894-01           AGREEMENT:  N  |LAST UPDATE DATE:  08/02/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JOHN MADERA          R3      |
|                                                |BRIAN SMITH          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  JIM CARSONS                  |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|BAB1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| STOLEN TROXLER MOISTURE DENSITY GAUGE                                        |
|                                                                              |
| The licensee reported a missing (presumed stolen) Troxler moisture density   |
| gauge, model #3401 serial #14236.  The gauge was discovered missing from the |
| bed of a pickup where it had been locked in its case and the case cabled to  |
| the truck.  The gauge contains 2 sources, one of approximately 8 mCi Cs-137  |
| and the other 40 mCi Am-241:Be.  The licensee intends to make a police       |
| report and is retracing the trucks route from the work site back to the      |
| driver's home located in Farmington Hills, MI.                               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38181       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: QUAD CITIES              REGION:  3  |NOTIFICATION DATE: 08/02/2001|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 10:07[EDT]|
|   RXTYPE: [1] GE-3,[2] GE-3                    |EVENT DATE:        08/02/2001|
+------------------------------------------------+EVENT TIME:        08:23[CDT]|
| NRC NOTIFIED BY:  TOM OSELAND                  |LAST UPDATE DATE:  08/02/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNUSUAL EVENT         |JOHN MADERA          R3      |
|10 CFR SECTION:                                 |PAT MADDEN           NRR     |
|AAEC 50.72(a) (1) (i)    EMERGENCY DECLARED     |JOSEPH HOLONICH      IRO     |
|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|MARK RING            R3      |
|AESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|JAMES DYER           R3      |
|                                                |STEINDURF            FEMA    |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     A/R        Y       100      Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER FOLLOWING LIGHTNING      |
| STRIKE                                                                       |
|                                                                              |
| At 0823 CDT, the licensee declared an Unusual Event due to a lightning       |
| strike on or near the Unit 2 main transformer which caused a fire in the     |
| transformer and a loss of offsite power to the unit. Both emergency diesel   |
| generators (the Unit 2 and swing EDGs) started and loaded.  An automatic     |
| reactor scram occurred and all control rods inserted following the scram.    |
| The unit is currently in Hot Shutdown with decay heat being removed via the  |
| safety/relief valves and reactor vessel water level control being maintained |
| using the safe shutdown makeup pump and the reactor core isolation cooling   |
| (RCIC) system.                                                               |
|                                                                              |
| Offsite firefighting assistance was requested to combat the fire, which has  |
| since been extinguished. The licensee is currently in the process of         |
| restoring offsite power to the unit. The electrical transient did not        |
| significantly affect the operation of Unit 1.                                |
|                                                                              |
| The NRC resident inspector has been informed by the licensee.                |
|                                                                              |
| HOO NOTE: The NRC senior resident inspector notified the NRC Operations      |
| Center of this event at 0933 EDT. The agency entered the monitoring phase of |
| normal mode at 1003 EDT.                                                     |
|                                                                              |
| * * * UPDATE 1220EDT ON 8/2/01 FROM FOSTER (REGION 3 IRC) TO S. SANDIN * *   |
| *                                                                            |
|                                                                              |
| Region 3 has secured from Monitoring at 1120CDT based on current plant       |
| conditions and the licensee's on-going restoration of offsite power.         |
| Notified IRO(Holonich).                                                      |
|                                                                              |
| * * * UPDATE 1253EDT ON 8/2/01 FROM CHRISSOTIMOS TO S. SANDIN * * *          |
|                                                                              |
| Unit 2 exited the Unusual Event at 1147CDT.  The following information was   |
| provided via fax:                                                            |
|                                                                              |
| "The Unit 2 and 1/2 [Swing] Emergency Diesel Generators Auto Started on the  |
| ESF signal. Group II and III isolations were received as expected. Local     |
| Fire Department assisted in fire activities and extinguished transformer     |
| fire. RCIC and the Safe Shutdown Makeup Pump were manually initiated to      |
| provide level control. Relief valves were manually operated to control       |
| pressure.  At 1048 CDT Transformer 22 power was restored and is providing    |
| loads to Unit 2. Both EDG's have been shutdown. The Illinois Emergency       |
| Management Agency has been notified of the Hazmat spill from the transformer |
| fire.                                                                        |
|                                                                              |
| "A courtesy call was also made to the National Response Center for a         |
| potential of a Hazmat spill into the Mississippi River [NRC Incident Report  |
| # 575186].                                                                   |
|                                                                              |
| "The Unusual Event was terminated at 1147 CDT."                              |
|                                                                              |
| The licensee is in the process of informing state/local agencies and has     |
| informed the NRC resident inspector.  Notified R3DO(Madera), EO(Madden),     |
| IRO(Holonich), EDO(Bergman) and FEMA(Caldwell).                              |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   38182       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 08/02/2001|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 18:10[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        08/02/2001|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        12:38[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  08/02/2001|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |JOHN MADERA          R3      |
|  DOCKET:  0707001                              |LARRY CAMPER         NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  M. C. PITTMAN                |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NONR                     OTHER UNSPEC REQMNT    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24-HOUR REPORT INVOLVING A SAFETY SYSTEM ACTUATION DUE TO A VALID SIGNAL     |
|                                                                              |
| "At 1250 on 08/02/01, the PSS office was notified that a High Autoclave      |
| Steam Pressure alarm was received on the C-337A  autoclave position 2 west   |
| Autoclave Steam Pressure Control System (SPCS). The SPCS system is required  |
| to be operable while feeding in mode 5 according to TSR 2.2.3.3. The         |
| autoclave was in Mode 5 at the time of the actuation. The indications were   |
| checked according to the alarm response procedure and the alarm was          |
| determined to be a valid signal. The autoclave was removed from service and  |
| the Steam Pressure Control System was declared inoperable by the Plant Shift |
| Superintendent.                                                              |
|                                                                              |
| "This safety system actuation is reportable to the NRC as required by Safety |
| Analysis Report, section 6.9, table 1, criteria J.2, Safety System actuation |
| due to a valid signal as a 24-hour event notification.                       |
|                                                                              |
| "The NRC Senior Resident Inspector has been notified of this event."         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38183       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: INDIAN POINT             REGION:  1  |NOTIFICATION DATE: 08/02/2001|
|    UNIT:  [] [3] []                 STATE:  NY |NOTIFICATION TIME: 19:17[EDT]|
|   RXTYPE: [2] W-4-LP,[3] W-4-LP                |EVENT DATE:        08/02/2001|
+------------------------------------------------+EVENT TIME:        15:00[EDT]|
| NRC NOTIFIED BY:  TIM RIEGER                   |LAST UPDATE DATE:  08/02/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |CLIFFORD ANDERSON    R1      |
|10 CFR SECTION:                                 |HERB BERKOW          NRR     |
|AUNA 50.72(b)(3)(ii)(B)  UNANALYZED CONDITION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNANALYZED CONDITION INVOLVING SEISMIC EVENT DISCOVERED DURING ENGINEERING   |
| REVIEW                                                                       |
|                                                                              |
| "On August 2, 2001, at approximately 1500 hours, Engineering notified        |
| operations that the Service Water (SW) System may not meet analyzed flow     |
| requirements after a seismic event as a result of a system re-alignment      |
| change implemented June 4, 2001. The SWS re-alignment change placed an 8     |
| inch non-seismic SW line on the essential SW header. The SWS was originally  |
| analyzed for a seismic event with the break of a 10 inch non-seismic SW      |
| line. The change evaluation concluded that this configuration was bounding   |
| for the alignment. The assessment of the alignment change did not adequately |
| consider the effects of the seismic event. After a review of the change,     |
| Engineering judged that the SWS would not meet system design flow            |
| requirement after a seismic event with two out of three pumps due to the     |
| failure of both non-seismic lines that were aligned as a result of the       |
| change. Operations initiated realignment of the 8 inch SW line back to the   |
| non-essential header which was completed at 1640 hours. Engineering is       |
| performing evaluations but judged that the SWS would have met flow           |
| requirements for plant shutdown with three SW pumps operable after a seismic |
| event with no random single failure (three pumps operable)."                 |
|                                                                              |
| The licensee will inform the NRC resident inspector.                         |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021