Event Notification Report for August 3, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/02/2001 - 08/03/2001 ** EVENT NUMBERS ** 38179 38180 38181 38182 38183 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38179 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 08/01/2001| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 09:05[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 08/01/2001| +------------------------------------------------+EVENT TIME: 07:01[CDT]| | NRC NOTIFIED BY: BRUCE ANDERSON |LAST UPDATE DATE: 08/02/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |PATRICK HILAND R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO NEGATIVE FLUX RATE | | | | The unit automatically tripped from 100%; the first out annunciator was Flux | | Rate Reactor Trip. Immediately following the trip, the rod position | | indicator showed that five control rods did not insert completely. The stuck | | control rods indicated 15-20 steps out from bottom. Operators entered their | | reactor trip/safety injection emergency procedure (1E0), but were able to | | transition to the trip recovery procedure (1ES0.1). One of the stuck control | | rods subsequently indicated full insertion. The unit is currently stable in | | Mode 3. Operators are emergency borating the reactor per 1ES0.1 a total of | | 1000 gallons (250 gallons per stuck rod). The licensee is continuing their | | trip recovery. Preliminary investigation indicates a problem with the rod | | control system may have led to one or more dropped control rods. | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | * * * UPDATE 1025 EDT 8/1/01 FROM DAMMANN TAKEN BY JONES * * * | | | | The licensee reported that the auxiliary feedwater (AFW) system (pumps 11 | | and 12) automatically actuated on steam generator low-low level following | | the trip, as expected. In addition, two of the stuck rods are now | | indicating full insertion. The NRC resident inspector has been informed of | | this update. | | | | * * * UPDATE 1624 EDT 08/01/01 FROM GOSMAN TAKEN BY MACKINNON * * * | | | | After interviewing the Reactor Operators it was determined that 6 rod bottom | | lights did not immediately come on after the reactor trip. Also a media | | press release will be made concerning this event. R3DO (John Madera) | | notified. | | | | The NRC resident inspector was notified of this update by the licensee. | | | | * * * UPDATE 0431 EDT 8/2/01 FROM IRVIN TAKEN BY STRANSKY * * * | | | | "Investigation into the cause of the reactor trip has determined that | | control rods associated with Rod Control Power Cabinet 2AC began to insert | | into the core. As designed, the reactor protection system actuated to insert | | the remaining control rods. | | | | "In accordance with procedures, operators verified the reactor had safely | | shutdown. However, indicator lights for six of twenty-nine individual | | control rods did not indicate that the rods had fully inserted. This | | situation is addressed in the reactor trip procedure and the operators | | responded appropriately by borating to compensate. | | | | "Control rod drop testing has been performed and has verified that all | | control rods fully inserted. Individual rod position indication calibration | | check is in progress." | | | | The NRC resident inspector will be informed of this update by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38180 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NTH CONSULTANTS |NOTIFICATION DATE: 08/02/2001| |LICENSEE: NTH CONSULTANTS |NOTIFICATION TIME: 08:49[EDT]| | CITY: FARMINGTON HILLS REGION: 3 |EVENT DATE: 08/02/2001| | COUNTY: STATE: MI |EVENT TIME: 07:50[EDT]| |LICENSE#: 21-14894-01 AGREEMENT: N |LAST UPDATE DATE: 08/02/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN MADERA R3 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM CARSONS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN TROXLER MOISTURE DENSITY GAUGE | | | | The licensee reported a missing (presumed stolen) Troxler moisture density | | gauge, model #3401 serial #14236. The gauge was discovered missing from the | | bed of a pickup where it had been locked in its case and the case cabled to | | the truck. The gauge contains 2 sources, one of approximately 8 mCi Cs-137 | | and the other 40 mCi Am-241:Be. The licensee intends to make a police | | report and is retracing the trucks route from the work site back to the | | driver's home located in Farmington Hills, MI. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38181 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 08/02/2001| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 10:07[EDT]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 08/02/2001| +------------------------------------------------+EVENT TIME: 08:23[CDT]| | NRC NOTIFIED BY: TOM OSELAND |LAST UPDATE DATE: 08/02/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |JOHN MADERA R3 | |10 CFR SECTION: |PAT MADDEN NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |JOSEPH HOLONICH IRO | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|MARK RING R3 | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT|JAMES DYER R3 | | |STEINDURF FEMA | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER FOLLOWING LIGHTNING | | STRIKE | | | | At 0823 CDT, the licensee declared an Unusual Event due to a lightning | | strike on or near the Unit 2 main transformer which caused a fire in the | | transformer and a loss of offsite power to the unit. Both emergency diesel | | generators (the Unit 2 and swing EDGs) started and loaded. An automatic | | reactor scram occurred and all control rods inserted following the scram. | | The unit is currently in Hot Shutdown with decay heat being removed via the | | safety/relief valves and reactor vessel water level control being maintained | | using the safe shutdown makeup pump and the reactor core isolation cooling | | (RCIC) system. | | | | Offsite firefighting assistance was requested to combat the fire, which has | | since been extinguished. The licensee is currently in the process of | | restoring offsite power to the unit. The electrical transient did not | | significantly affect the operation of Unit 1. | | | | The NRC resident inspector has been informed by the licensee. | | | | HOO NOTE: The NRC senior resident inspector notified the NRC Operations | | Center of this event at 0933 EDT. The agency entered the monitoring phase of | | normal mode at 1003 EDT. | | | | * * * UPDATE 1220EDT ON 8/2/01 FROM FOSTER (REGION 3 IRC) TO S. SANDIN * * | | * | | | | Region 3 has secured from Monitoring at 1120CDT based on current plant | | conditions and the licensee's on-going restoration of offsite power. | | Notified IRO(Holonich). | | | | * * * UPDATE 1253EDT ON 8/2/01 FROM CHRISSOTIMOS TO S. SANDIN * * * | | | | Unit 2 exited the Unusual Event at 1147CDT. The following information was | | provided via fax: | | | | "The Unit 2 and 1/2 [Swing] Emergency Diesel Generators Auto Started on the | | ESF signal. Group II and III isolations were received as expected. Local | | Fire Department assisted in fire activities and extinguished transformer | | fire. RCIC and the Safe Shutdown Makeup Pump were manually initiated to | | provide level control. Relief valves were manually operated to control | | pressure. At 1048 CDT Transformer 22 power was restored and is providing | | loads to Unit 2. Both EDG's have been shutdown. The Illinois Emergency | | Management Agency has been notified of the Hazmat spill from the transformer | | fire. | | | | "A courtesy call was also made to the National Response Center for a | | potential of a Hazmat spill into the Mississippi River [NRC Incident Report | | # 575186]. | | | | "The Unusual Event was terminated at 1147 CDT." | | | | The licensee is in the process of informing state/local agencies and has | | informed the NRC resident inspector. Notified R3DO(Madera), EO(Madden), | | IRO(Holonich), EDO(Bergman) and FEMA(Caldwell). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38182 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/02/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 18:10[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/02/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 12:38[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/02/2001| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |JOHN MADERA R3 | | DOCKET: 0707001 |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: M. C. PITTMAN | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR REPORT INVOLVING A SAFETY SYSTEM ACTUATION DUE TO A VALID SIGNAL | | | | "At 1250 on 08/02/01, the PSS office was notified that a High Autoclave | | Steam Pressure alarm was received on the C-337A autoclave position 2 west | | Autoclave Steam Pressure Control System (SPCS). The SPCS system is required | | to be operable while feeding in mode 5 according to TSR 2.2.3.3. The | | autoclave was in Mode 5 at the time of the actuation. The indications were | | checked according to the alarm response procedure and the alarm was | | determined to be a valid signal. The autoclave was removed from service and | | the Steam Pressure Control System was declared inoperable by the Plant Shift | | Superintendent. | | | | "This safety system actuation is reportable to the NRC as required by Safety | | Analysis Report, section 6.9, table 1, criteria J.2, Safety System actuation | | due to a valid signal as a 24-hour event notification. | | | | "The NRC Senior Resident Inspector has been notified of this event." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38183 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 08/02/2001| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 19:17[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 08/02/2001| +------------------------------------------------+EVENT TIME: 15:00[EDT]| | NRC NOTIFIED BY: TIM RIEGER |LAST UPDATE DATE: 08/02/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CLIFFORD ANDERSON R1 | |10 CFR SECTION: |HERB BERKOW NRR | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANALYZED CONDITION INVOLVING SEISMIC EVENT DISCOVERED DURING ENGINEERING | | REVIEW | | | | "On August 2, 2001, at approximately 1500 hours, Engineering notified | | operations that the Service Water (SW) System may not meet analyzed flow | | requirements after a seismic event as a result of a system re-alignment | | change implemented June 4, 2001. The SWS re-alignment change placed an 8 | | inch non-seismic SW line on the essential SW header. The SWS was originally | | analyzed for a seismic event with the break of a 10 inch non-seismic SW | | line. The change evaluation concluded that this configuration was bounding | | for the alignment. The assessment of the alignment change did not adequately | | consider the effects of the seismic event. After a review of the change, | | Engineering judged that the SWS would not meet system design flow | | requirement after a seismic event with two out of three pumps due to the | | failure of both non-seismic lines that were aligned as a result of the | | change. Operations initiated realignment of the 8 inch SW line back to the | | non-essential header which was completed at 1640 hours. Engineering is | | performing evaluations but judged that the SWS would have met flow | | requirements for plant shutdown with three SW pumps operable after a seismic | | event with no random single failure (three pumps operable)." | | | | The licensee will inform the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021