Event Notification Report for June 20, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/19/2001 - 06/20/2001 ** EVENT NUMBERS ** 38079 38080 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38079 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 06/19/2001| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 12:13[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 06/19/2001| +------------------------------------------------+EVENT TIME: 09:15[CDT]| | NRC NOTIFIED BY: PEDERSON |LAST UPDATE DATE: 06/19/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM DECLARED INOPERABLE | | | | HPCI system was declared inoperable due to all alarm functions not | | operating. The local undervoltage alarms did not annunciate in the control | | room. This condition was discovered during a normal routine test. They | | were attempting to send a signal from the local HPCI panel in the plant to | | the control room, but the control room did not receive it. They verified | | that the local panel is operable. An operator was locally stationed at the | | subject panel to verify current alarm status and call the control room. | | Therefore, in this mode of operation, the HPCI system has been declared | | operable. They are still investigating the problem with signal | | transmission. | | | | The NRC Resident Inspector was notified. | | | | The State and local agencies will be informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38080 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 06/20/2001| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 04:07[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 06/20/2001| +------------------------------------------------+EVENT TIME: 00:11[CDT]| | NRC NOTIFIED BY: GEORGE RUITER |LAST UPDATE DATE: 06/20/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 96 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO FEEDWATER REGULATING VALVE FAILING SHUT. | | | | At 0011 CDT feedwater regulating valve to steam generator "B" failed to the | | closed position and manual control was not effective. The reactor/turbine | | tripped on steam flow greater than feed flow coincident with low steam | | generator water level. Following the trip, the rod bottom light for rod D4 | | (interior rod) was off and valve LD-2 indicated mid-position (letdown | | isolated on low pressurizer water level). Individual Rod Position | | Indication for rod D4 indicates zero, however, emergency boration was used | | to inject the required amount of boric acid for one stuck rod. Excess | | letdown was established at 0028 CDT hours, since normal letdown was not | | available due to the failure of valve LD-2. All emergency core cooling | | systems, emergency diesel generators are fully operable if needed and the | | electrical grid is stable. | | | | Both Motor Driven and the Turbine Driven Auxiliary Feedwater Pumps | | automatically started. The Turbine Driven Auxiliary Feedwater pump was | | secured per procedure and steam generator water is being maintained by the | | Motor Driven Auxiliary Feedwater Pumps. | | | | At this time the licensee thinks that rod bottom light for rod D4 is burned | | out. The licensee is also investigating why letdown isolation valve, LD-2, | | indicates mid-position and the unexpected closure of feedwater regulating | | valve for steam generator "B". The steam dump bypass control system is | | operating properly. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021