Event Notification Report for May 29, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/25/2001 - 05/29/2001 ** EVENT NUMBERS ** 38011 38031 38032 38033 38034 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38011 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/18/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 15:37[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/17/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:37[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/25/2001| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |GARY SHEAR R3 | | DOCKET: 0707001 |SUSAN FRANT NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WHITE | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 RESPONSE | | | | At 1640 CDT on 05/17/01, the Plant Shift Superintendent (PSS) was notified | | that the independent verification required by procedure CP2-CU-CH2137 was | | not performed. The maintenance segment was not independently verified to be | | isolated. The same person signed for performance as well as the | | verification of the segment isolation. NCSA 400.009 requires that fissile | | operations that credit AQ-NCS function that is disabled due to maintenance | | must be identified independently and disabled using a tagout prior to | | disabling the feature and commencing maintenance. This is done to prevent | | operation of a system while an AQ-NCS component function is disabled. Since | | the independent verification was not performed, the process condition was | | not maintained. Therefore, double contingency was not maintained. | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | While the NCS control was violated, the fissile operation containing the | | component(s) undergoing maintenance was tagged out using LOTO both as a | | standard maintenance practice in C-400 and due to other NCS requirements. | | In addition, the equipment items removed had no AQ-NCS function which was | | affected by the maintenance actions. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR): | | | | In order for criticality to be possible, the components undergoing | | maintenance must have an AQ-NCS function that is disabled, and the affected | | operations must be subsequently performed with fissile solution. | | Additionally, the maintenance activity must be one of the relatively few | | maintenance activities that do not require tagout for another NCS reason, | | such as to prevent fissile solution from leaking from the system. | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | Double contingency for this scenario is established by implementing | | independently verifying the prevention of the affected fissile operation. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE CRITICAL MASS): | | | | Maximum assay of 2.75 wt. % U-235. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | The first leg of double contingency is based on preventing operation of the | | Cylinder Wash Facility during maintenance affecting the AQ-NCS component. | | The components were properly identified as non-AQ-NCS; therefore, this | | control was not violated. | | | | The second leg of double contingency is based on independently preventing | | operation of the Cylinder Wash Facility during maintenance affecting the | | AQ-NCS component. The requirement to independently verify the AQ-NCS | | function of all components affected by maintenance was not performed. The | | control was violated, and the process condition was not maintained. | | | | Since the independent verification was not performed, the process condition | | was not maintained. Therefore, double contingency was not maintained. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLEMENTED: | | | | This condition was identified while reviewing completed maintenance work | | packages. There is no action that can be performed to resolve this | | condition and bring the process back into compliance since the maintenance | | activity has been completed. | | | | The NRC Resident Inspector was notified, and the DOE Representative will be | | informed. | | | | * * * UPDATE ON 5/22/01 @ 1235 BY HUDSON TO GOULD * * * | | | | As a result of this NCS violation, a review of work packages was initiated | | to determine if other instances exist where the required second signature | | was not obtained. On 05/21/01 at 1520 CDT, the PSS was notified that | | another incident involving the violation of this requirement was discovered | | pertaining to maintenance on the RF (radio frequency) furnace. | | | | The NRC Senior Resident has been notified of this event by Paducah | | personnel. The Reg 3 RDO (Burgess) and the NMSS EO (Cool) were informed by | | the NRC Operations Officer. | | | | * * * UPDATE 1440 ON 5/25/2001 FROM WALKER TAKEN BY STRANSKY * * * | | | | "This report updated on 5-25-01 to document the results of NCS reevaluation | | of the subject incidents. It has been determined that double contingency was | | maintained and these incidents are not reportable. | | | | "The first leg of double contingency is based on preventing fissile | | operation of the equipment during maintenance affecting the AQ-NCS | | component. The components were properly identified as non-AQ-NCS, therefore, | | this control was not violated. | | | | "The second leg of double contingency is based on independently preventing | | fissile operation of the equipment/system during maintenance affecting the | | AQ-NCS component. The requirement to independently verify the AQ-NCS | | function of all components affected by maintenance was not performed so this | | control was violated. Since the component does not have an AQ-NCS function, | | there was no process parameter being relied on for double contingency. | | Therefore, the process condition was maintained. | | | | "Although the independent verification was not performed, there was no | | reliance on NOS parameters since the component had no AQ-NCS function. | | Therefore there was no parameter to lose and the process condition was | | maintained. Therefore, double contingency was maintained." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Burgess). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38031 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TRISTATE INSPECTION AND CONSULTANTS |NOTIFICATION DATE: 05/25/2001| |LICENSEE: TRISTATE INSPECTION AND CONSULTANTS |NOTIFICATION TIME: 10:15[EDT]| | CITY: FLINT REGION: 3 |EVENT DATE: 05/24/2001| | COUNTY: GENESEE STATE: MI |EVENT TIME: 21:10[EDT]| |LICENSE#: 37-19640-01 AGREEMENT: N |LAST UPDATE DATE: 05/25/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |SONIA BURGESS R3 | | |JOHN KINNEMAN R1 | +------------------------------------------------+JOHN HICKEY NMSS | | NRC NOTIFIED BY: PAT DURKIN | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |IBBE 30.50(b)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SOURCE HANG-UP AT A TRISTATE INSPECTION AND CONSULTANTS TEMPORARY JOB SITE | | IN HOMER CITY, PENNSYLVANIA | | | | The licensee reported that there was a source hang-up at a temporary job | | site in Homer City, Pennsylvania. The radiography camera involved was an | | Amersham-660B which contained a 52-curie iridium-192 source. | | | | When the source hang-up occurred, the crew involved (two radiographers) | | secured the area and notified an AEA Technologies Retrieval Team. Prior to | | the Retrieval Team's arrival, the Tristate crew (with assistance from other | | workers) was able to successfully shield the guide tube, straighten it out, | | and retrieve the source to its shielded position. As a result, the AEA | | Technologies Retrieval Team was not required. | | | | A pocket dosimeter for one of the original two crew members when off scale | | at some point during the process, but it was also reported that the | | radiographer had dropped it two exposures prior to this one. He then | | noticed that the dose had increased by 10 millirem, but it remained on | | scale. It was later re-zeroed, and it was still approximately 10 millirem | | high. The second radiographer's total dose was 85 millirem. | | | | The licensee plans to send the dosimetry out for analysis today. The | | licensee also plans to return the camera to Amersham for possible repairs. | | | | (Call the NRC operations officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 38032 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIVERSITY OF MED. AND DENT. OF NJ |NOTIFICATION DATE: 05/25/2001| |LICENSEE: UNIVERSITY OF MED. AND DENT. OF NJ |NOTIFICATION TIME: 16:21[EDT]| | CITY: NEWARK REGION: 1 |EVENT DATE: 05/23/2001| | COUNTY: STATE: NJ |EVENT TIME: 16:30[EDT]| |LICENSE#: 29-02957-13 AGREEMENT: N |LAST UPDATE DATE: 05/25/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN KINNEMAN R1 | | |THOMAS ESSIG NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: LANKA | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING IR-192 SEEDS | | | | On 5/23/01, six ribbons of Ir-192 seeds were implanted into a patient as | | part of a treatment. When the ribbons were removed from the patient at | | approximately 1000 on 5/25/01, only five of the six ribbons were recovered. | | The patient stated that one of the ribbons had come out approximately one | | hour after implantation and he had discarded it in the trash; however, the | | doctor had not observed any disturbance to the implantation site during an | | examination conducted on 5/24/01. The missing ribbon contains nine seeds; | | each seed contains 0.49 mg Ra equivalent activity. | | | | The licensee has conducted an exhaustive search of the facility but has been | | unable to locate the missing seeds. In addition, interviews were conducted | | with housekeeping personnel. The licensee has contacted the NRC Region I | | office regarding this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38033 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 05/25/2001| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 18:36[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 05/24/2001| +------------------------------------------------+EVENT TIME: 20:15[EDT]| | NRC NOTIFIED BY: MICHAEL CONWAY |LAST UPDATE DATE: 05/25/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |87 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR REPORT MADE IN ACCORDANCE WITH FACILITY OPERATING LICENSE | | | | "On 5/24/01 at 2015 hrs, Nine Mile Point Unit 2 experienced a sudden failure | | on the control circuitry of one of two Reactor Recirculation System flow | | control valves. The failure mechanism of the 'B' flow control valve produced | | reactor core flow changes in both the increase and decrease directions which | | had a resultant effect of raising and lowering reactor power. At the time of | | the failure, Nine Mile Point Unit 2 was operating at 100% power. The core | | flow changes occurred within a ninety second period and changed neutron flux | | (APRM) by approximately 30 to 40%. Plant conditions were stabilized by | | hydraulically locking the malfunctioning flow control valve in a stable | | position. Reactor Power is now 87% of rated. No Technical Specification | | Limiting Condition for Operation (LCO) violations are known to have | | occurred. | | | | "This report is being made as required by the Nine Mile Point Unit 2 | | Facility Operating License #NPF-69 section 2.F. During this event, Reactor | | Power may have nominally exceeded 102% of rated for several seconds. As | | such, this event is required to be reported to the NRC Operations Center | | within 24 hrs as a violation of License section 2.C(1) Maximum Power Level. | | Event analysis is continuing and may result in retraction of this | | notification at a later date." | | | | The licensee will inform the NRC resident inspector of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38034 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 05/27/2001| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 08:40[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 05/27/2001| +------------------------------------------------+EVENT TIME: 06:18[CDT]| | NRC NOTIFIED BY: T. GRANLUND |LAST UPDATE DATE: 05/27/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |SONIA BURGESS R3 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 80 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC SCRAM FOLLOWING MAIN TURBINE TRIP DURING SURVEILLANCE TESTING | | | | "Unit 2 was operating at 80% Reactor Power, 937 Mwe. LOS-RP-M5, Turbine | | Control Valve Surveillance was in progress. An Automatic Main Turbine Trip | | and Reactor Scram occurred at 0618. Initial investigation indicates the | | cause of the Main Turbine Trip was High Vibration and Electro Hydraulic | | Controls (EHC) Master Turbine Trip. | | | | "All systems operated as designed, there were no ECCS actuations. The lowest | | Reactor Water Level was minus 10 inches and recovered to the normal band. | | Reactor Pressure responded normally. No Safety Relief Valves Actuated. All | | Control Rods fully inserted. | | | | "2A and 2C Circulating Water Pumps tripped during the Electrical Bus | | transfer following the Main Turbine Trip. This is suspected to be caused by | | electrical perturbation on the system but will be further investigated." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021