Event Notification Report for May 16, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/15/2001 - 05/16/2001 ** EVENT NUMBERS ** 37815 37816 37968 37989 37990 37991 37992 37993 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37815 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 03/08/2001| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 13:04[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 03/05/2001| +------------------------------------------------+EVENT TIME: 16:08[CST]| | NRC NOTIFIED BY: PAT DECKER |LAST UPDATE DATE: 05/15/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN MADERA R3 | |10 CFR SECTION: | | |*UNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOW PRESSURE CORE SPRAY STRUCTURAL ANALYSIS DID NOT CONSIDER ALL POSSIBLE | | FLOW CONDITIONS | | | | "On March 5, 2001, it was discovered that the structural analysis of | | in-vessel Core Spray piping did not consider all applicable flow conditions. | | A notification should have been made at that time because the effect of the | | unanalyzed condition on degradation of plant safety was not considered with | | respect to all plant operating conditions (i.e., the plant was shut down at | | the time of discovery). Preliminary analysis results indicated that | | previous analyses are bounding." | | | | This issue will be resolved before the next plant startup. | | | | The licensee will notify the NRC resident inspector. | | | | **** RETRACTION RECEIVED AT 1641 EDT ON 05/15/01 FROM PATRICK DECKER TO | | LEIGH TROCINE **** | | | | The licensee is retracting this event notification. The following text is a | | portion of a facsimile received from the licensee: | | | | "[...] On [03/08/01], we reported that structural analysis of the in-core | | spray piping did not consider all the applicable flow conditions. Upon | | re-evaluation, this is not reportable since: 1) this condition only | | affected one train of core spray piping, and 2) the flaw condition believed | | to have been overlooked was determined [analytically] to be bounded by | | [existing] analyses." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R3DO (Parker). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37816 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 03/09/2001| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 04:30[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 03/09/2001| +------------------------------------------------+EVENT TIME: 01:30[CST]| | NRC NOTIFIED BY: TIM ROGERS |LAST UPDATE DATE: 05/15/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN MADERA R3 | |10 CFR SECTION: | | |*SHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A N 0 Refueling |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MODE CHANGE DUE TO LITERAL INTERPRETATION OF REQUIREMENTS | | | | "To meet compliance with literal interpretation of Tech Spec 3.7.A.5 and | | 3.8.B.6, containment venting and purging using SBGT is required above 'Cold | | Shutdown.' Plant is < 212�, all rods in BUT mode switch was in 'Refuel.' To | | comply with Tech Specs, a Tech Spec shutdown with mode switch was performed. | | All rods were already in but it wasn't a preplanned shutdown evolution. | | Other similar 'Cold Shutdown' Tech Spec compliance issues are being looked | | at." | | | | An automatic scram signal was generated when the mode switch was taken to | | the 'Shutdown' position. Although all control rods were already inserted, | | the licensee considers this action to be reportable as a valid safety system | | actuation. The NRC resident inspector will be informed of this event by the | | licensee. | | | | **** RETRACTION RECEIVED AT 1641 EDT ON 05/15/01 FROM PATRICK DECKER TO | | LEIGH TROCINE **** | | | | The licensee is retracting this event notification. The following text is a | | portion of a facsimile received from the licensee: | | | | "[...] On [03/09/01], we reported the failure to literally comply with | | [Technical] Specification 3.7.A and 3.8.B.6. This event is being retracted | | since 1) the requirement to use SBGT 'above' Cold Shutdown does not apply to | | plant conditions where the plant is below the Cold Shutdown temperature of | | 212 degrees F with the mode switch in 'refuel,' and 2) moving the mode | | switch back to shutdown from 'refuel' was required to comply with a | | prerequisite of an approved plant procedure. Therefore, this was part of a | | preplanned sequence." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R3DO (Parker). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37968 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 05/06/2001| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 06:02[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/06/2001| +------------------------------------------------+EVENT TIME: 03:10[CDT]| | NRC NOTIFIED BY: SCHMIDT |LAST UPDATE DATE: 05/15/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |*INA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 90 Power Operation |73 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MAIN TURBINE STOP VALVE FAILED TO CLOSE DURING TESTING | | | | The #4 main turbine stop valve failed to close during the performance of | | turbine valve testing procedure. Failure of the turbine valve to close | | affects the turbine stop valve closure scram function of both A&B reactor | | protection trip systems. Reactor power is currently being reduced to less | | than 45% power which is required when the minimum conditions for the turbine | | stop valve closure scram function are not satisfied. The licensee believes | | the cause of the problem is probably due to a bad solenoid valve. | | | | The NRC Resident Inspector will be notified. | | | | **** RETRACTION RECEIVED AT 1641 EDT ON 05/15/01 FROM PATRICK DECKER TO | | LEIGH TROCINE **** | | | | The licensee is retracting this event notification. The following text is a | | portion of a facsimile received from the licensee: | | | | "[...] On [05/06/01], we reported the failure to close of Main Turbine Stop | | Valve #4 during routine testing. Subsequently, it was learned that the | | failure affected the test circuit only and had no effect on the normal | | operation of the stop valve. Therefore, this event is not reportable. The | | test circuit failure has been corrected, and the Main Turbine Stop Valve #4 | | retested successfully." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R3DO (Parker). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37989 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: OTTWELL MALBY |NOTIFICATION DATE: 05/15/2001| |LICENSEE: OTTWELL MALBY |NOTIFICATION TIME: 10:42[EDT]| | CITY: TRAVERSE CITY REGION: 3 |EVENT DATE: 05/15/2001| | COUNTY: STATE: MI |EVENT TIME: 10:30[EDT]| |LICENSE#: 21-32235-01 AGREEMENT: N |LAST UPDATE DATE: 05/16/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GARY SHEAR R3 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: TOD CRAMER | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STRUCTURE FIRE INVOLVING NUCLEAR GAUGE | | | | The licensee reported that a fire is currently occurring at their field | | office. A Troxler Model 3411 moisture/density gauge is currently stored in | | the building. The sources are locked in their safe positions, and the gauge | | is located in a storage locker. The licensee has notified local police and | | fire departments regarding the presence of this device. | | | | ***** UPDATE RECEIVED AT 1515 ON 05/15/01 FROM TOD CRAMER TO LEIGH TROCINE | | ***** | | | | The licensee is updating this event notification. The gauge was not damaged | | in the fire. There was some water damage, and that area of the building was | | reported to be underwater after the fire. The HAZMAT team obtained a | | surface reading on the gauge, and the reading was 1 millirem per hour. The | | gauge was intact, and there was no heat damage, melting, or physical damage. | | The licensee plans to perform a wipe test and possibly repair the gauge. | | | | The licensee notified the Fire Department, HAZMAT, local/city police | | agencies, and NRC region 3 office (Jim Hastings). The NRC operations | | officer notified the R3DO (Parker) and NMSS EO (Cool). | | | | (Please call the NRC operations officer for a licensee contact telephone | | number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37990 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NC DIVISION OF RADIATION PROTECTION |NOTIFICATION DATE: 05/15/2001| |LICENSEE: S&ME |NOTIFICATION TIME: 14:56[EDT]| | CITY: GREENSBORO REGION: 2 |EVENT DATE: 05/12/2001| | COUNTY: STATE: NC |EVENT TIME: [EDT]| |LICENSE#: 041-0922-1 AGREEMENT: Y |LAST UPDATE DATE: 05/15/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES R. OGLE R2 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SHARN JEFFRIES | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT REGARDING A TROXLER MOISTURE DENSITY GAUGE | | LOST/STOLEN FROM S&ME IN WINSTON SALEM, NORTH CAROLINA | | | | The following text is a portion of a facsimile received from the North | | Carolina Department of Environment and Natural Resources, Division of | | Radiation Protection: | | | | "SUBJECT: Incident 01-14" | | | | "Today, a North Carolina Portable Gauge Licensee (S&ME 041-0922-1 | | Greensboro) reported a loss/theft of a Portable Moisture Density Gauge from | | Winston Salem, NC, between the evening on Friday, May 11, 2001, and | | Saturday, May 12, 2001. Local and State law enforcement agencies were | | notified on Saturday, May 12, 2001. This Agency was notified by NC | | Emergency Management of the incident at [1630] on Monday, May 14, 2001. The | | Licensee reported the incident to this Agency [on] May 15, 2001." | | | | "The device that was lost/stolen is:" | | | | "Troxler 3411B Moisture Density Gauge SN 14682 | | Cs-137 #50-3361 8 mCi | | Am-241:Be #47-10037 40 mCi" | | | | (Call the NRC operations officer for a State contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37991 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: STORK TWIN CITY TESTING |NOTIFICATION DATE: 05/15/2001| |LICENSEE: STORK TWIN CITY TESTING |NOTIFICATION TIME: 15:31[EDT]| | CITY: ST. PAUL REGION: 3 |EVENT DATE: 05/08/2001| | COUNTY: RAMSEY STATE: MN |EVENT TIME: 09:00[CDT]| |LICENSE#: 22-01376-02 AGREEMENT: N |LAST UPDATE DATE: 05/15/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MICHAEL PARKER R3 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PATRICK LIEBL | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STUCK IRIDIUM-192 SOURCE AND FAILURE TO MAKE AN EVENT NOTIFICATION WITHIN 24 | | HOURS | | | | On 05/05/01, an X-ray crew in Heron Lake, MN, was inspecting a flat bottom | | tank using an Amertest-660A device containing 80 curies of iridium-192. At | | 0900 CDT, during performance of an exposure, the stand that the guide tube | | was connected to fell over and kinked the tube. As a result, the crew could | | not initially retract the source. The crew subsequently followed procedures | | and successfully retracted the source to its shielded position. There were | | no overexposures as a result of this event. | | | | In preparation for submitting a 30-day letter, the licensee discovered | | (today) that this event should have been reported as a 24-hour event | | notification. | | | | (Call the NRC operations officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37992 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 05/15/2001| | UNIT: [1] [2] [] STATE: MD |NOTIFICATION TIME: 16:44[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 05/15/2001| +------------------------------------------------+EVENT TIME: 16:08[EDT]| | NRC NOTIFIED BY: BRUCE SHICK |LAST UPDATE DATE: 05/15/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |*COM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 68 Power Operation |68 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MAJOR LOSS OF EMERGENCY PREPAREDNESS CAPABILITIES IN THE CALVERT COUNTY | | AREA | | | | At 1608 on 05/15/01, the control room was notified that 40 of the 49 | | [emergency] sirens failed to respond [during] the weekly silent test at | | 1445. The apparent cause is currently believed to be a potential | | transformer failure. Troubleshooting and repairs are in progress. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37993 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BYRON REGION: 3 |NOTIFICATION DATE: 05/16/2001| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 05:38[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/15/2001| +------------------------------------------------+EVENT TIME: 07:00[CDT]| | NRC NOTIFIED BY: BRYAN HERRING |LAST UPDATE DATE: 05/16/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHAEL PARKER R3 | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 98 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT MAY HAVE OPERATED ABOVE 100% POWER | | | | During power up-rate data verification, Byron Station identified that an | | improper feedwater density factor and thermal expansion coefficient had been | | used to calculate feedwater flow constants (referred to as AMAG constants) | | on Units 1 and 2. The improper constants resulted in a non-conservative | | determination of reactor power via the thermal power calorimetric | | calculation. Thermal power was underestimated by 0.12 percent rated thermal | | power. The improper AMAG constants have been utilized since AMAG was | | implemented at Byron Station in May of 2000 (Unit 1 on 5/16/00 and Unit 2 on | | 5/12/00). It is believed since May of 2000 either unit may have exceeded | | 100 percent rated thermal power over an eight hour period based on the | | non-conservative AMAG constants. There is no evidence that either unit ever | | exceeded 102.0 percent rated thermal power. A formal review of past power | | history for both units is in progress. The AMAG constants have been | | corrected for Unit 2 and are in progress for Unit 1. Unit 1 is being | | maintained at or below 99.88 percent rated thermal power until the AMAG | | constants have been corrected. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021