Event Notification Report for May 4, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/03/2001 - 05/04/2001 ** EVENT NUMBERS ** 37962 37963 37964 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37962 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 05/03/2001| | UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 09:54[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/03/2001| +------------------------------------------------+EVENT TIME: 07:00[EDT]| | NRC NOTIFIED BY: A. WISNIEWSKI |LAST UPDATE DATE: 05/03/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |HAROLD GRAY R1 | |10 CFR SECTION: | | |*DEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOCAL LEAK RATE FAILED | | | | At 0700, on 05/03/01, the Control Room was informed that the HPCI Steam | | Exhaust Check Valves, V23-3 & V23-4, failed their local leak rate test such | | that the minimum pathway leakage rate was exceeded, greater than 193.674 | | scfh which is in excess of 0.6La Tech Spec limit. The valves were declared | | inoperable and repairs are underway. | | | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37963 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 05/03/2001| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 13:36[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 03/12/2001| +------------------------------------------------+EVENT TIME: 00:30[EDT]| | NRC NOTIFIED BY: KEN RUSSELL |LAST UPDATE DATE: 05/03/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |*INV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ACTUATION OF DIVISION 1 BALANCE-OF-PLANT OUTBOARD ISOLATION VALVES - INVALID | | SYSTEM ACTUATION | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On March 12, 2001, at approximately 0030 hours, the Perry Nuclear Power | | Plant experienced an actuation of Division 1 Balance-of-Plant (BOP) outboard | | isolation valves. At the time of the event, the plant was in Mode 5 | | (Refueling), and had been subcritical for approximately 23 days. The | | reactor pressure vessel (RPV) head was removed and the refuel cavity and | | upper containment pools were flooded; no core alterations were in progress | | at the time. Shutdown cooling was being provided by the Fuel Pool Cooling | | and Clean-up system (FPCC), which was aligned to the upper containment pool. | | The isolation signal closed one or more valves in each of the following | | Division 1 subsystems: FPCC, Containment Drywell purge, Two-Bed | | Demineralized Water System, Fire Protection, Liquid Radwaste Sumps, Liquid | | Radwaste Disposal, Instrument Air, Containment Vessel Chilled Water, | | Condensate Transfer and Storage. In addition, the isolation signal caused a | | temporary interruption of shutdown cooling flow through the FPCC system, | | until it was re-established by on-shift Operations personnel." | | | | "The event is considered an invalid system actuation, and is reportable | | under 10 CFR 50.73(a)(2)(iv)(A). The isolation was not initiated in | | response to actual plant conditions or parameters, and was not a manual | | initiation. It meets the criteria specified in 10 CFR 50.73(a)(2)(iv)(B)(2) | | as a general containment isolation signal affecting containment isolation | | valves in more than one system. Therefore, notification is being provided | | via 60-day optional phone call in accordance with 10 CFR 50.73(a)(1). All | | systems functioned as expected for a partial BOP (outboard) isolation." | | | | "The interruption of shutdown cooling lasted for 111 minutes, from 0030 | | hours to 0221 hours on March 12, 2001. During this time, the reactor water | | temperature increased approximately 3 degrees, from 99 to 102 degrees. The | | estimated time to boil was conservatively calculated at 28 hours. The | | affected Fire Protection (drywell CO2) isolation valve was not required to | | be open, since the fire-protected equipment was secured during the refueling | | outage. Repositioning of the other valves did not present operational | | concerns; they were re-opened per restoration procedures. The cooling flow | | path was available immediately with manual operator action." | | | | "The BOP isolation was attributed to scheduled maintenance activities being | | conducted in the Control Room. The replacement of a bayonet-socket-style | | relay caused two fuses to blow in the BOP manual initiation logic circuit. | | The apparent cause was an inadvertent ground from the seismic strap of the | | new relay during installation that resulted in the required logic for the | | isolation." | | | | "This event was documented in the Corrective Action Program. Remedial | | actions include review of the event with instrumentation and control | | technicians, and evaluation of depowering valves which could interrupt | | shutdown cooling during maintenance activities." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37964 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: 3M COMPANY |NOTIFICATION DATE: 05/03/2001| |LICENSEE: W. L. GORE |NOTIFICATION TIME: 14:06[EDT]| | CITY: EAUCLAIRE REGION: 3 |EVENT DATE: 10/22/2000| | COUNTY: STATE: WI |EVENT TIME: [CDT]| |LICENSE#: 1429-1811GL AGREEMENT: N |LAST UPDATE DATE: 05/03/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MELVYN LEACH R3 | | |DON COOL NMSS | +------------------------------------------------+DICK WESSMAN IRO | | NRC NOTIFIED BY: MIKE LEWANDOWSKI | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 3M COMPANY REPORT REGARDING A W. L. GORE FACILITY LOSS OF A STATIC | | ELIMINATOR CONTAINING 10 MILLICURIES OF POLONIUM-210 | | | | On 09/12/00, 3M Company (located in St. Paul, Minnesota) announced its | | intent to purchase W. L. Gore (located in Eauclaire, Wisconsin). The | | acquisition took place during late October or early November 2000. On | | 03/14/01, 3M Company representatives visited the newly acquired W. L. Gore | | facility and discovered the existence of static eliminators. An audit was | | subsequently performed, and 3M Company was able to account for all but one | | static eliminator. | | | | Apparently, the W. L. Gore facility received the polonium static eliminator | | in question on 08/10/00. This static eliminator was manufactured by Nuclear | | Radiation Development (NRD), and it was comprised of an in-line ionizer tube | | approximately 4 inches long and 1/4 inch in diameter with 10 millicuries of | | polonium-210 plated on the inside of the device. The static eliminator was | | installed on a large circuit substrate manufacturing machine for use in the | | W. L. Gore facility under the NRD general license (1429-1811GL). | | | | On 09/06/00, the circuit substrate manufacturing machine was sent back to | | its manufacturer (Everrett Charles) for an upgrade. The static eliminator | | was reported to be on the machine when it was shipped to Everrett Charles | | (location unknown); however, the static eliminator was determined to be | | missing after Everrett Charles returned the upgraded machine to W. L. Gore | | on 10/22/00. | | | | Everrett Charles was notified of the missing static eliminator during the | | week of 04/09/01. NRD was also notified during the week of 04/16/01. It | | was reported that searches were performed, but the missing static eliminator | | was not found. | | | | (Call the NRC operations officer for a 3M Company contact telephone number.) | +------------------------------------------------------------------------------+
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