Event Notification Report for February 2, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/01/2001 - 02/02/2001 ** EVENT NUMBERS ** 37703 37707 37708 37709 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37703 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 01/31/2001| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 13:09[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 11/27/2000| +------------------------------------------------+EVENT TIME: 12:00[EST]| | NRC NOTIFIED BY: L. W. MYERS |LAST UPDATE DATE: 02/01/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |DANIEL HOLODY R1 | |10 CFR SECTION: |VERN HODGE NRR | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PART 21 REPORT ON CAP SCREW FAILURE USED IN AN AUXILIARY FEEDWATER PUMP AT | | THE BEAVER VALLEY POWER STATION UNIT ONE | | | | One of the four cap screws on the collar of the hydraulic balancing drum of | | the steam-driven Auxiliary Feedwater pump (AFP) 1FW-P-2 failed. The head of | | the screw broke off and became lodged in the area between the stuffing box | | extension and the balancing drum collar, preventing 1FW-P-2 from starting on | | 11/27/00. The root cause of the cap screw failure was material defect. | | Final metallurgical analysis revealed that the failure was due to | | intergranular failure. The defects noted in the fastener surface were | | attributed to the original manufacture of the cap screw. The probable cause | | of the failure was the propagation of manufacturing cracks under static | | preload, which caused tensile stress of approximately 88% of the yield | | stress of the cap screw. Hydrogen absorption and diffusion into regions of | | high stress caused propagation of the cracks. The failure was a time | | delayed process. | | | | The material defect led to the failure of one AFP cap screw which prevented | | the AFP from starting. Failure of one or more Auxiliary Feedwater Pumps to | | start when required, would result in a major degradation of essential safety | | related equipment, and the required Auxiliary Feedwater System may not have | | been able to perform its safety related function, which would constitute a | | substantial safety hazard. | | | | Though not attributed as part of root cause for the one cap screw failure, | | two related noteworthy non-compliant issues were identified with the four | | cap screws found on the 1FW-P-2 AFP collar. An emission spectrograph test | | run on a cap screw showed a chromium content of 0.148% (indicating the screw | | was carbon steel). The vendor Material Release for 1FW-P-2 (MR 912004) shows | | that the cap screws are 410 stainless steel that should have contained 12% | | chromium. FENOC is not able to conclude whether operating with carbon steel | | cap screws (in place of the required stainless steel) could have caused the | | AFP to fail. | | | | The cap screws also had hardness values of 41-44 HRC (Hardness Rockwell C). | | The purchase specification requires 410 stainless steel with a hardness less | | than 22 HRC. Although carbon steel bolts are less susceptible to stress | | corrosion cracking than stainless steel bolts, FENOC is not able to conclude | | whether operating with carbon steel cap screws with a hardness of 41-44 HRC | | (in excess of the required hardness limit of 22 HRC) could have caused the | | AFP to fail. | | | | | | THE LICENSEE ALSO SUBMITTED THE FOLLOWING INFORMATION RELATED TO THE | | REPLACEMENT SCREWS THAT WERE ORDERED FROM FLOWSERVE CORPORATION AND | | MANUFACTURED BY U.S. BOLT: | | | | The specified maximum hardness value was exceeded for 16 of 20 cap screws | | supplied for use on a balancing drum located on the Auxiliary Feedwater Pump | | (AFP) shaft. Exceeding the hardness limit makes these cap screws | | susceptible to stress corrosion cracking. Therefore, the defect, if gone | | undetected and installed, could have caused these cap screws to fail during | | their operating life. A failed cap screw could jam and prevent a standby | | AFP from starting. Failure of one or more AFPs to start when required, | | would result in a major degradation of essential safety related equipment, | | and the required Auxiliary Feedwater System may not have been able to | | perform its safety related function, which would constitute a significant | | safety hazard. As such, the defect is reportable pursuant to 10 CFR Part 21 | | requirements. | | | | HOO NOTE: This report was modified to identify the licensee rather than the | | reporting organization (FirstEnergy Nuclear Operating Company) which is the | | owner/operator of Beaver Valley. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37707 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 02/01/2001| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 01:08[EST]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 01/31/2001| +------------------------------------------------+EVENT TIME: 21:47[CST]| | NRC NOTIFIED BY: SHANE MARIK |LAST UPDATE DATE: 02/01/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 EXPERIENCED AN AUTOMATIC REACTOR SCRAM FOLLOWING FAILURE OF A MAIN | | POWER TRANSFORMER | | | | "At 21:47 CST, U-1 automatically scrammed from a main turbine 'NON-EHC' trip | | caused from a failure of a main power transformer. The main power | | transformers received an auto deluge signal and an acrid smell is reported | | in the area. The main generator tripped from the loss of the main power | | transformer causing the main turbine to trip, which caused an automatic | | reactor scram. The fast closure of the main turbine valves caused a reactor | | pressure spike which tripped both reactor recirculation pumps and caused two | | safety relief valves to actuate. | | | | "All automatic actions initiated as designed, but the following anomalies | | were noted; | | | | - 1A circulating water pump tripped | | - Division 1 alternate rod insertion failed to reset on scram recovery | | - 1B recirculation pump received a low oil level alarm on restart attempt | | - U2 received an electrical perturbation from the U1 scram which resulted in | | a loss of the 2A heater drain pump and two heaters. Cram rods were inserted | | in accordance with Operating procedures. U2 was stabilized at 930 MWE." | | | | All rods fully inserted. The two safety relief valves reseated after | | actuation. Decay heat is currently being removed via the bypass valves to | | the main condenser. RCIC is inoperable but available, if needed. There are | | no challenges to offsite power and the system auxiliary transformer is fully | | available. The licensee is presently resetting the deluge system in order | | to assess if there is mechanical damage on the 1 west main power transformer | | and will determine whether a U-1 cooldown is required to evaluate the 1B | | recirculation pump problem. The NRC resident inspector was informed and is | | currently onsite. | | | | * * * UPDATE AT 2007 EST ON 2/1/01 BY SHANE MARIK TO FANGIE JONES * * * | | | | "This is a follow up notification to event #37707 to enhance and clarify | | plant response following the post scram investigation. It was determined | | that a bushing/insulator failure on the 'C' phase of the 1 West Main Power | | Transformer failed causing the lockout of the main generator. The failed | | bushing/insulator is not located directly on the 1 West Main Power | | transformer but is located on the first main tower between the transformer | | and the switchyard. | | | | "During the turbine trip and reactor scram the reactor vessel level | | instrumentation spiked causing a 'ringing phenomenon' initiated from the | | increase in pressure. This phenomenon was identified from the transient | | analyses data and seen during previous pressure transients. The ringing in | | the level instrumentation caused varying level indication (<1/2 second | | cycles) which is indication only, not a real change in reactor level. This | | ringing phenomenon caused to the actuations and 1/2 isolations identified | | during the scram. | | | | "The following is offered to clarify the anomalies identified during the | | event. | | 1. The main steam isolation valves received a 1/2 group one isolation due | | to the ringing phenomenon. | | 2. Reactor recirculation pumps tripped off due to the ringing phenomenon. | | 3. Four safety relief valves opened. Previously reported as two. All four | | safety relief valves re-closed properly. | | 4. Reactor building ventilation tripped due to the inboard isolation | | dampers closing on low voltage transient. | | 5. The main generator voltage regulator failed to auto transfer to manual. | | 6. A division one ground was received and was subsequently isolated to | | three alarm points associated with the main power transformers which | | received a deluge on the bushing fault." | | | | The licensee notified the NRC Resident Inspector. The R3DO (David Hills) | | has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37708 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 02/01/2001| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 11:12[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 02/01/2001| +------------------------------------------------+EVENT TIME: 07:30[EST]| | NRC NOTIFIED BY: DAVID T. WALSH |LAST UPDATE DATE: 02/01/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DANIEL HOLODY R1 | |10 CFR SECTION: | | |*DEG 50.72(b)(3)(ii)(A) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT THE MAIN STEAM ISOLATION VALVE (MSIV) MAX PATH LIMIT COULD | | HAVE BEEN EXCEEDED DUE TO INABILITY TO DEPRESSURIZE THE STEAM LINE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[The] Unit 2 [Reactor Core Isolation Cooling] System was removed from | | service to perform scheduled maintenance. Control Room operators closed the | | inboard containment isolation valve, HV249F007, to depressurize the steam | | line. The steam line did not depressurize as expected. Operators then | | closed the outboard containment isolation valve, HV249F008, and were | | successful in isolating the pathway and depressurizing the steam piping. At | | 07:30, the inboard isolation valves were declared inoperable. Due to the | | inability to depressurize the steam line and following a technical review of | | the system response and supporting data, it appears that the MSIV max path | | limit could have been exceeded, and therefore, this event is reportable | | under 10CFR50.72(b)(3)(ii), Degraded or Unanalyzed Condition." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37709 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ROSEMOUNT NUCLEAR INSTRUMENTS, INC. |NOTIFICATION DATE: 02/01/2001| |LICENSEE: ROSEMOUNT NUCLEAR INSTRUMENTS, INC. |NOTIFICATION TIME: 13:11[EST]| | CITY: EDEN PRAIRIE REGION: 3 |EVENT DATE: 02/01/2001| | COUNTY: STATE: MN |EVENT TIME: [CST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 02/01/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID HILLS R3 | | |VERN HODGE NRR | +------------------------------------------------+ | | NRC NOTIFIED BY: JEFFREY W. SCHMITT | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10 CFR PART 21 REPORT FOR MODEL 353C AND 353C1 CONDUIT SEALS | | | | "This notification relates to Model 353C and 353C1 conduit seals which | | exhibit an electrical short condition. Any model 353C and 353C1 conduit seal | | which does not indicate a short condition is deemed acceptable and this | | notification is not applicable to such units. | | | | "This notification is not applicable to units which are currently | | operational, or have successfully completed a functional test by the | | customer that would verify the insulation resistance of the lead wires. | | | | "RNII [Rosemount Nuclear Instruments, Inc.] does not have sufficient | | information to determine the safety impact related to plant applications. | | Licensees must determine the impact on plant operations and plant safety and | | take action as deemed necessary." | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021