Event Notification Report for February 1, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/31/2001 - 02/01/2001 ** EVENT NUMBERS ** 37703 37704 37705 37706 37707 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37703 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FIRSTENERGY NUCLEAR OPERATING CO. |NOTIFICATION DATE: 01/31/2001| |LICENSEE: INGERSOLL-DRESSER PUMP COMPANY |NOTIFICATION TIME: 13:09[EST]| | CITY: SHIPPINGPORT REGION: 1 |EVENT DATE: 11/27/2000| | COUNTY: STATE: PA |EVENT TIME: 12:00[EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 01/31/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DANIEL HOLODY R1 | | |VERN HODGE NRR | +------------------------------------------------+ | | NRC NOTIFIED BY: L.W. MYERS | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PART 21 REPORT ON CAP SCREW FAILURE USED IN AN AUXILIARY FEEDWATER PUMP AT | | THE BEAVER VALLEY POWER STATION UNIT ONE | | | | One of the four cap screws on the collar of the hydraulic balancing drum of | | the steam-driven Auxiliary Feedwater pump (AFP) 1FW-P-2 failed. The head of | | the screw broke off and became lodged in the area between the stuffing box | | extension and the balancing drum collar, preventing 1FW-P-2 from starting on | | 11/27/00. The root cause of the cap screw failure was material defect. | | Final metallurgical analysis revealed that the failure was due to | | intergranular failure. The defects noted in the fastener surface were | | attributed to the original manufacture of the cap screw. The probable cause | | of the failure was the propagation of manufacturing cracks under static | | preload, which caused tensile stress of approximately 88% of the yield | | stress of the cap screw. Hydrogen absorption and diffusion into regions of | | high stress caused propagation of the cracks. The failure was a time | | delayed process. | | | | The material defect led to the failure of one AFP cap screw which prevented | | the AFP from starting. Failure of one or more Auxiliary Feedwater Pumps to | | start when required, would result in a major degradation of essential safety | | related equipment, and the required Auxiliary Feedwater System may not have | | been able to perform its safety related function, which would constitute a | | substantial safety hazard. | | | | Though not attributed as part of root cause for the one cap screw failure, | | two related noteworthy non-compliant issues were identified with the four | | cap screws found on the 1FW-P-2 AFP collar. An emission spectrograph test | | run on a cap screw showed a chromium content of 0.148% (indicating the screw | | was carbon steel). The vendor Material Release for 1FW-P-2 (MR 912004) shows | | that the cap screws are 410 stainless steel that should have contained 12% | | chromium. FENOC is not able to conclude whether operating with carbon steel | | cap screws (in place of the required stainless steel) could have caused the | | AFP to fail. | | | | The cap screws also had hardness values of 41-44 HRC (Hardness Rockwell C). | | The purchase specification requires 410 stainless steel with a hardness less | | than 22 HRC. Although carbon steel bolts are less susceptible to stress | | corrosion cracking than stainless steel bolts, FENOC is not able to conclude | | whether operating with carbon steel cap screws with a hardness of 41-44 HRC | | (in excess of the required hardness limit of 22 HRC) could have caused the | | AFP to fail. | | | | | | FENOC ALSO SUBMITTED THE FOLLOWING INFORMATION RELATED TO THE REPLACEMENT | | SCREWS THAT WERE ORDERED FROM FLOWSERVE CORPORATION AND MANUFACTURED BY U.S. | | BOLT: | | | | The specified maximum hardness value was exceeded for 16 of 20 cap screws | | supplied for use on a balancing drum located on the Auxiliary Feedwater Pump | | (AFP) shaft. Exceeding the hardness limit makes these cap screws | | susceptible to stress corrosion cracking. Therefore, the defect, if gone | | undetected and installed, could have caused these cap screws to fail during | | their operating life. A failed cap screw could jam and prevent a standby | | AFP from starting. Failure of one or more AFPs to start when required, | | would result in a major degradation of essential safety related equipment, | | and the required Auxiliary Feedwater System may not have been able to | | perform its safety related function, which would constitute a significant | | safety hazard. As such, the defect is reportable pursuant to 10CFR Part 21 | | requirements. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37704 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 01/31/2001| | UNIT: [] [2] [] STATE: FL |NOTIFICATION TIME: 15:08[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 01/09/2001| +------------------------------------------------+EVENT TIME: 09:30[EST]| | NRC NOTIFIED BY: ALBRITTON |LAST UPDATE DATE: 01/31/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LEONARD WERT R2 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL FOR THE CONTROL ROOM OPERATORS TO EXCEED GENERAL DESIGN CRITERIA | | 19 LIMITS DURING AN ACCIDENT | | | | Following evaluation and analysis, FPL identified a condition that could | | have potentially led to the control room operators receiving a dose in | | excess of GDC 19 limits during accident conditions. St. Lucie recently | | identified weaknesses in the Unit 2 procedures that could result in the | | operators not taking action to manually align the control room outside air | | intakes to pressurize the control room when the control room ventilation | | system is operating in the emergency recirculation mode. The procedures | | direct which outside air intake should be used depending on existing | | radiological conditions. However, the procedures do not direct the operators | | to establish outside makeup air (i.e.. throttle open the outside air intake | | valves) if minimum control room pressurization is met. In addition to the | | procedural weaknesses identified, the control room differential pressure | | indicators exhibit a small positive pressure bias that could have misled the | | operators into believing that the control room was maintained at a positive | | differential pressure without the need to open the outside air intake | | valves. During the course of the hypothesized accident, operation of the | | control room ventilation system in this condition would have been ultimately | | discovered and corrected by the technical advisors in the Technical Support | | Center or Emergency Operations Facility. | | | | St. Lucie issued Night Orders to the operating crews to clarify operational | | requirements for the control room ventilation systems until the requisite | | procedure changes are implemented. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37705 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 01/31/2001| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 17:24[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/31/2001| +------------------------------------------------+EVENT TIME: 14:00[CST]| | NRC NOTIFIED BY: RUSS WALTON |LAST UPDATE DATE: 01/31/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BLAIR SPITZBERG R4 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION - SEWAGE SPILL | | | | At approximately 1400 CST on 01/31/01, an untreated sewage spill, | | overflowing from an underground manhole cover, of approximately 200 gallons | | occurred outside of the Generation Support Building. The sewage spilled | | into the storm drains which drain into East Creek. The spill has been | | isolated and contained. The spill occurred outside the Protected Area but | | remained inside the Owner Controlled Area during the event with no spillage | | reaching the Mississippi River. The Louisiana Department of Environmental | | Quality was notified by River Bend personnel at | | 1451. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37706 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 01/31/2001| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 18:48[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/31/2001| +------------------------------------------------+EVENT TIME: 11:45[EST]| | NRC NOTIFIED BY: LEE JOHNSON |LAST UPDATE DATE: 01/31/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |*INC 50.72(b)(3)(v)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL INABILITY TO CONTROL A RADIOACTIVE RELEASE | | | | At 1145 on 1/31/01, the door to the auxiliary engineered safeguards suction | | side vestibule in unit 2 was found stuck open. This bypasses the normal | | flowpath for both trains of ESF fans and renders them inoperable. The plant | | made an unrecognized entry into Technical Specification 3.0.3 until the door | | could be closed, which occurred in approximately one minute. This eight | | hour report is being made in accordance with 10 CFR 50.72 based on the | | temporary inability to control a possible radioactive release. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37707 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 02/01/2001| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 01:08[EST]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 01/31/2001| +------------------------------------------------+EVENT TIME: 21:47[CST]| | NRC NOTIFIED BY: SHANE MARIK |LAST UPDATE DATE: 02/01/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 EXPERIENCED AN AUTOMATIC REACTOR SCRAM FOLLOWING FAILURE OF A MAIN | | POWER TRANSFORMER | | | | "At 21:47 CST, U-1 automatically scrammed from a main turbine 'NON-EHC' trip | | caused from a failure of a main power transformer. The main power | | transformers received an auto deluge signal and an acrid smell is reported | | in the area. The main generator tripped from the loss of the main power | | transformer causing the main turbine to trip, which caused an automatic | | reactor scram. The fast closure of the main turbine valves caused a reactor | | pressure spike which tripped both reactor recirculation pumps and caused two | | safety relief valves to actuate. | | | | "All automatic actions initiated as designed, but the following anomalies | | were noted; | | | | - 1A circulating water pump tripped | | - Division 1 alternate rod insertion failed to reset on scram recovery | | - 1B recirculation pump received a low oil level alarm on restart attempt | | - U2 received an electrical perturbation from the U1 scram which resulted in | | a loss of the 2A heater drain pump and two heaters. Cram rods were inserted | | in accordance with Operating procedures. U2 was stabilized at 930 MWE." | | | | All rods fully inserted. The two safety relief valves reseated after | | actuation. Decay heat is currently being removed via the bypass valves to | | the main condenser. RCIC is inoperable but available, if needed. There are | | no challenges to offsite power and the system auxiliary transformer is fully | | available. The licensee is presently resetting the deluge system in order | | to assess if there is mechanical damage on the 1 west main power transformer | | and will determine whether a U-1 cooldown is required to evaluate the 1B | | recirculation pump problem. The NRC resident inspector was informed and is | | currently onsite. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021