Event Notification Report for January 16, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/12/2001 - 01/16/2001 ** EVENT NUMBERS ** 37554 37626 37660 37661 37662 37663 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37554 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 11/28/2000| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 16:50[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 11/28/2000| +------------------------------------------------+EVENT TIME: 15:13[EST]| | NRC NOTIFIED BY: BOB COOLIDGE |LAST UPDATE DATE: 01/12/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANIELLO DELLA GRECA R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) DECLARED INOPERABLE DUE TO | | INSTRUMENTATION FAILURE | | | | "The HPCI System was taken out of service for surveillance testing earlier | | in the day. The surveillance's were completed and HPCI was placed back in | | service in standby lineup. At this time, the high flow isolation | | instrumentation was found to be reading well beyond the limits of the normal | | in service band (+10 to -10). At that time, HPCI was removed from service | | (availability) and isolated. The proper LCO was entered and troubleshooting | | is underway." | | | | The licensee informed the NRC resident inspector. | | | | * * * UPDATE 1415EST ON 1/12/01 FROM OLSON TO MacKINNON * * * | | | | The licensee is retracting this report based on the following: | | | | "This is a retraction of event no. 37554 made on November 28, 2000 at 1651 | | in accordance with 10CFR50.72(b)(2)(iii)(D). | | | | "An Engineer had noted a flow switch that provides a high steam flow to the | | HPCI system reading -17 inches of water while the other indicated -2 inches | | of water. The Primary Containment Isolation capability of the HPCI | | isolation valves was declared inoperable and the valves de-energized in the | | isolated condition. HPCI was declared inoperable and a 14 day cold shutdown | | LCO entered. Subsequent testing of the differential pressure switches found | | the trip setpoints to be correct. The face plate had not been 'zeroed' | | during previous calibration. This had no effect on switch operation, | | therefore could not have prevented fulfillment of safety function." | | | | The licensee informed the NRC resident inspector. Notified R1DO(Lew). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37626 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 12/20/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 22:25[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 12/20/2000| +------------------------------------------------+EVENT TIME: 20:14[EST]| | NRC NOTIFIED BY: ROBERT McCOY |LAST UPDATE DATE: 01/12/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANTHONY DIMITRIADIS R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC CONTROL ROOM VENTILATION SYSTEM SHIFT FROM NORMAL TO EMERGENCY | | RECIRCULATION MODE WHILE A PLANNED GAS DECAY TANK RELEASE WAS IN PROGRESS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 2014, with a gas decay tank release in progress (total activity 0.215 | | Ci, (Kr-85 = 0.214 Ci, Xe-133 = 0.001 Ci)), control room ventilation gas | | monitor R-36 went into alarm causing ventilation to shift to mode F. During | | the [2-second] spike, R-36 counts went from 30 cpm to 856 cpm and back to 30 | | cpm. Local air samples taken by the RP Tech both in the control room and in | | the area of the control room ventilation intake revealed no activity." | | | | The licensee stated that the gas decay tank release was planned and that the | | counts going through the plant stack were considered normal. (These counts | | peaked at 120 cpm.) The licensee stated that the planned gas decay tank | | release was within both the expected and required release limits. The wind | | was blowing in a favorable direction, and the stability class for | | meteorological conditions was stable. Although counts have returned to | | normal, the licensee plans to leave control room ventilation in the | | emergency recirculation mode until tomorrow morning. | | | | The licensee notified the NRC resident inspector. | | | | * * * UPDATE ON 1/12/01 @ 1113 BY GOMEZ TO GOULD * * * RETRACTION | | | | Rochester Gas and Electric (RG&E) is retracting this notification. This | | event was originally thought to be in response to a valid radiological | | condition because a waste gas decay tank release was in progress at the same | | time as this event. RG&E has confirmed that the alarm on Control Room Noble | | Gas radiation monitor | | R-36 that occurred at 20:14 EST on December 20, 2000, causing the shift in | | Control Room ventilation to "Mode F" (emergency recirculation mode), was the | | result of a spurious spike on R-36. The alarm was not in response to any | | radiation condition, | | | | Local samples taken by radiation protection technicians on December 20, both | | in the Control Room and in the area of the Control Room ventilation intake, | | revealed no activity. The Plant Process Computer (PPCS) plots show that | | R-36 counts were steady just before and immediately after the spike. | | Further engineering evaluation of this event has determined that the alarm | | on R-36 was caused by a sudden spike and was not in response to any | | radiation condition. Therefore, this event is not reportable and is | | retracted. | | | | Other occurrences of spiking on R-36 took place during December 2000 and | | January 2001. Some of these spikes resulted in alarms on R-36 and | | subsequent shift in Control Room ventilation to "Mode F". These alarms were | | recognized at the time of alarm as invalid actuations of the HVAC System for | | the Control Room, and did not result in NRC notification. Trouble-shooting | | and corrective maintenance is on-going on the R-36 monitor. | | | | The licensee has notified the NRC Resident Inspector. | | | | The Region 1 RDO (Lew) was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37660 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATTS BAR REGION: 2 |NOTIFICATION DATE: 01/12/2001| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 13:36[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/12/2001| +------------------------------------------------+EVENT TIME: 10:30[EST]| | NRC NOTIFIED BY: TERRY KNUETTEL |LAST UPDATE DATE: 01/12/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES R. OGLE R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AN ACTING SUPERVISOR TESTED POSITIVE FOR AN ILLEGAL DRUG DURING A RANDOM | | TEST | | | | A non-licensed employee was determined to be under the influence of | | marijuana during a random test. The employee's access to the plant has been | | terminated. Contact the Headquarters Operations Officer for additional | | details. | | | | The licensee will inform the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37661 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 01/12/2001| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 13:40[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 01/12/2001| +------------------------------------------------+EVENT TIME: 09:28[CST]| | NRC NOTIFIED BY: R BARTON |LAST UPDATE DATE: 01/12/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DALE POWERS R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INVALID ACTUATION OF AN ENGINEERED SAFETY FEATURE SYSTEM | | | | During performance of "A" Train Trip Actuations Device Operational Test a | | reactor protection signal was generated when a procedure step was | | inadvertently skipped. At the time this occurred the "A" reactor trip | | bypass breaker was closed when the trip signal was generated. This caused | | the "A" reactor trip breaker to open. The reactor did not trip because the | | "A" bypass breaker was closed. | | | | This event resulted in an invalid actuation of an Engineered Safety Feature | | system. It was concluded that this event was reportable per | | 10CFR50.72(b)(2)(ii) since: | | (1) This actuation was not anticipated to occur as part of this pre-planned | | evolution since the trip signal was expected to be inhibited by the omitted | | procedure step and | | (2) The omitted step resulted in the system not being properly removed from | | service as required by the surveillance procedure (source range trip signal | | not being bypassed or inhibited). | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37662 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TENNESSEE DIV OF RAD HEALTH |NOTIFICATION DATE: 01/12/2001| |LICENSEE: AEROJET ORDNANCE TENNESSEE, INC. |NOTIFICATION TIME: 15:33[EST]| | CITY: JONESBOROUGH REGION: 2 |EVENT DATE: 01/11/2001| | COUNTY: STATE: TN |EVENT TIME: 11:30[EST]| |LICENSE#: S-90009 AGREEMENT: Y |LAST UPDATE DATE: 01/12/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES R. OGLE R2 | | |JOSEPH HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DEBRA SHULTZ (via fax) | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING FIRE IN AN INCINERATOR AIR EFFLUENT | | CLEANING SYSTEM | | | | "Event description: The licensee called to report a fire in their | | incinerator's air effluent cleaning system. The fire in the baghouse lasted | | approximately two hours. The building was evacuated, and onsite personnel | | extinguished the fire. The baghouse filter has not yet been opened to assess | | the damage. The area is secured and no routine operations are ongoing at | | this time. Smears taken in the area were maximum of 100-dpm/100 sq. cm. | | Clean up of the area has not begun. The total release from this event is | | estimated to be 0.013 microcuries of depleted uranium. Sample results will | | be available soon. | | | | "These events do not pose a threat to public health and safety but may be | | reportable under 1200-2-5-.141(2)c.(4). | | | | | | "Media attention: None" | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37663 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ABB POWER DISTRIBUTION |NOTIFICATION DATE: 01/15/2001| |LICENSEE: ABB POWER DISTRIBUTION |NOTIFICATION TIME: 16:33[EST]| | CITY: Florence REGION: 2 |EVENT DATE: 01/15/2001| | COUNTY: STATE: SC |EVENT TIME: 15:20[EST]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 01/15/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES R. OGLE R2 | | |RICHARD BARKLEY R1 | +------------------------------------------------+JOHN JACOBSON R3 | | NRC NOTIFIED BY: DARALL HARRIS |DALE POWERS R4 | | HQ OPS OFFICER: JOHN MacKINNON |VERN HODGE NRR | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL DEFECT PER 10 CFR PART 21 CONTROL DEVICE FOR HK AND K-LINE CIRCUIT | | BREAKERS | | | | | | In December 1998, Sequoyah Nuclear Plant (Chattanooga, TN) experienced a | | failure to close of a 7.5HK500/1200 Medium Voltage circuit breaker (Serial | | Number 48672-A101-1-3B) manufactured 3/30/1973. The cause of the breaker | | failure as determined by TVA was a failure of the Control Device (Part | | Number 191921T06). Specifically, a movable contact within the Control Device | | was found to have a broken spring retainer, which is a protuberance holding | | the return spring in place on the contact. This broken spring retainer | | allowed the spring to move out of its intended position, causing failure of | | the control contacts to make and break properly. This occurrence was | | documented and evaluated by the Tennessee Valley Authority Central | | Laboratories & Field Testing Service in their Technical Report #99-0550 on | | 11 February 1999. | | | | On February 29, 2000, Catawba Nuclear Station (York, SC) experienced a | | failure to close of a 5HK250/1200 Medium Voltage circuit breaker (Serial | | Number 50465F-1 -10186) manufactured 3/28/1979. The cause of the breaker | | failure as determined by Duke Power and ABB Florence was similar to the | | failure reported by TVA in 1998. Material analysis of the failed movable | | contact concluded that the material for the contact was correct to that | | specified. A dissected profile analysis of the failed contact revealed that | | the material at the base of the spring retainer on the movable contact was | | thin and failed due to fatigue. This failure was documented and evaluated by | | Duke Engineering Testing and Laboratory Services in their Metallurgical | | Analysis Report #2624 on 29 March 2000. | | | | On October 30, 2000, during a routine inspection of a Control Device on a | | 7.5HK500/1200 Medium Voltage circuit breaker (Serial Number 50464L-2-07210) | | manufactured 2/29/1979, Catawba Nuclear Station found a movable contact that | | had failed in a similar manner as the other two previously reported. This | | failure was documented and evaluated by Duke Engineering Testing and | | Laboratory Services in their Metallurgical Analysis Report #2726 on 01 | | November 2000. | | | | The cause of these three failures was fatigue of the metal at the base of | | the spring retainer on the movable contacts, due to insufficient metal mass | | at the base of the retainer. The spring retainer on the contact is formed | | with a die by punching the movable contact from the opposite side of the | | electrical contact mounting location during fabrication. The height of the | | spring retainer, therefore, determines the amount of material left at the | | base. | | | | Corrective action for this incident has been taken. After further | | investigation, ABB Florence has determined that the height of the spring | | retainer was changed in September 1979 to a lower specification, leaving | | more material at the base of the spring retainer. The movable contact formed | | with the greater spring retainer height specification prior to 1979 has a | | small possibility of failure as discussed above. There have been no other | | reports of movable contact failures. | | | | There have been only these three reports of this movable contact failure | | since the control device was introduced to the market in 1960. Since its | | introduction, more than 22,000 control devices have been produced for both | | HK and K-line type circuit breakers, each with 5 movable contacts. ABB | | therefore believes this problem is not significant enough to require | | immediate action from users. However, we recommend that control devices | | older than 1981 be replaced with new control devices on both HK and K-line | | breakers at the next scheduled maintenance of the breaker. | | | | ABB will notify all customers who purchased this product. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021