The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for January 12, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           01/11/2001 - 01/12/2001

                              ** EVENT NUMBERS **

37613  37627  37659  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37613       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SALEM                    REGION:  1  |NOTIFICATION DATE: 12/18/2000|
|    UNIT:  [1] [] []                 STATE:  NJ |NOTIFICATION TIME: 09:52[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        12/18/2000|
+------------------------------------------------+EVENT TIME:        06:40[EST]|
| NRC NOTIFIED BY:  RUSS GUMBERT                 |LAST UPDATE DATE:  01/11/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JOHN WHITE           R1      |
|10 CFR SECTION:                                 |                             |
|AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| CONTAINMENT FAN COOLER UNITS DECLARED INOPERABLE                             |
|                                                                              |
| "At 0640 on 12/18/00, '11' service water accumulator was declared inoperable |
| based on water level low out of specification for Technical Specifications.  |
| This condition was identified following calibration of the 'B' level device. |
| The service water accumulators support containment integrity by ensuring the |
| containment fan coils remain properly filled during a design basis accident. |
| Tech Spec 3.6.1.1 and Tech Spec 3.6.2.3 were entered for containment         |
| integrity and '11' and '12' containment fan coil unit inoperability. Actions |
| were taken within one hour to comply with containment integrity Tech Spec.   |
| The service water accumulator was filled to within specification at 0713 at  |
| which time Tech Spec 3.6.1.1 was exited. The '11' and '12' containment fan   |
| coil units were restored to operable at 0744 and Tech Spec 3.6.2.3 was       |
| exited. Actions are underway to calibrate the 'A' channel of level           |
| indication. All power plant parameters remained stable throughout the event  |
| and no other safety systems were affected."                                  |
|                                                                              |
| The NRC resident inspector will be informed of this notification by the      |
| licensee.                                                                    |
|                                                                              |
| * * * UPDATE 1312EST ON 1/11/01 FROM BENSON BINGGELI TO S. SANDIN * * *      |
|                                                                              |
| The licensee is retracting this report based on the following:               |
|                                                                              |
| "On December 18, 2000, a four-hour report was made for Salem Unit 1 in       |
| accordance with 10CFR50.72(B) (2) (iii) due to the water level for the 11    |
| Service Water accumulator being out of specification low based on readings   |
| from the 'B' level device. The service water accumulators support            |
| containment integrity by ensuring the containment fan coils remain properly  |
| filled during a design basis accident.                                       |
|                                                                              |
| "There are two level devices, 'A' and 'B', associated with each SW           |
| accumulator. During the time that the 'B' level device indicated that the SW |
| accumulator was out of specification, the 'A' level device continued to show |
| that the accumulator level was within the required level specification.      |
|                                                                              |
| "Following the calibration of the 'B' level device which showed that level   |
| on the 'B' channel was reading low out                                       |
| of specification, M&TE equipment (differential pressure gauge) was connected |
| to the 11 SW accumulator to provide an independent reading of the tank       |
| level. The M&TE equipment confirmed that the 11 SW accumulator level was     |
| within 0.5 inches of the level indicated by the 'A' level device. Based on   |
| this confirmation, the 'A' level device on the 11 SW accumulator is          |
| providing  an accurate indication of level in the tank.                      |
|                                                                              |
| "Since the 'A' level device readings were within the required Technical      |
| Specification level band for the 11 SW accumulator, the 11 SW accumulator    |
| was always operable and capable of performing its design basis function.     |
| Based on this information, the 4-hour report is being retracted."            |
|                                                                              |
| The licensee will inform the NRC resident inspector.  Notified R1DO(Lew).    |
+------------------------------------------------------------------------------+

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37627       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 12/20/2000|
|    UNIT:  [] [2] []                 STATE:  NC |NOTIFICATION TIME: 22:58[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        12/20/2000|
+------------------------------------------------+EVENT TIME:        20:08[EST]|
| NRC NOTIFIED BY:  REINSBURROW                  |LAST UPDATE DATE:  01/11/2001|
|  HQ OPS OFFICER:  LEIGH TROCINE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MIKE ERNSTES         R2      |
|10 CFR SECTION:                                 |                             |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP           |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FAILURE OF A REACTOR CORE ISOLATION COOLING (RCIC) BYPASS TO CONDENSATE      |
| STORAGE TANK VALVE TO FULLY STROKE DURING STROKE TIME TESTING                |
|                                                                              |
| The following text is a portion of a facsimile received from the licensee:   |
|                                                                              |
| "EVENT:  At 2008 on 12/20/00 during performance of OPT-10.1.8 (RCIC System   |
| Valve Operability Test), the 2-E51-F022 (RCIC bypass to condensate storage   |
| tank) failed to fully stroke during stroke timing of the valve.  A valve     |
| thermal overload annunciator was received.  This rendered the Brunswick Unit |
| 2 RCIC system inoperable.  RCIC was not in operation at the time of this     |
| failure."                                                                    |
|                                                                              |
| "INITIAL SAFETY SIGNIFICANCE EVALUATION:  Minimal safety significance.       |
| Remaining ECCS systems are operable."                                        |
|                                                                              |
| "CORRECTIVE ACTION(S):  Determine the cause of the 2-E51-F022 valve failure. |
| Return the Unit 2 RCIC system to operable following repair of 2-E51-F022."   |
|                                                                              |
| The licensee stated that this event did not result in any radiological       |
| release or reactor coolant leaks.  The licensee also stated that all systems |
| functioned as required and that there was nothing unusual or misunderstood.  |
| This event placed the unit in a 14-day technical specification limiting      |
| condition for operation.                                                     |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
|                                                                              |
| * * * RETRACTION ON 01/11/01 AT 1059ET BY CHARLES ELBERFELD TAKEN BY         |
| MACKINNON* * *                                                               |
|                                                                              |
| Upon further evaluation, it has been determined that the conditions          |
| resulting in the RCIC system being declared inoperable for Technical         |
| Specification LCO 3.5.3 did not result in a loss of the system's function to |
| remove residual heat.  The function of the RCIC system is to respond to      |
| transient events by providing makeup coolant to the reactor.  The RCIC       |
| system is not an Engineered Safety Feature system, and no credit is taken in |
| the Updated Final Safety Analysis Report (UFSAR) for RCIC system operation   |
| mitigating the consequences of a postulated accident.  The RCIC system is    |
| designed to operate either automatically or manually following reactor       |
| pressure vessel (RPV) isolation accompanied by a loss of normal coolant flow |
| from the reactor feedwater system to provide adequate core cooling and       |
| control of the RPV water level.  Its operational purpose is to provide an    |
| alternate source of reactor coolant to the vessel and to provide sufficient  |
| cooling to remove residual heat following reactor shutdown and loss of       |
| feedwater flow without requiring depressurization of the reactor. Neither    |
| the 2-E51-F022 being de-energized in the open position, nor the questionable |
| capability of the 2-E51-F029 resulted in the loss  of the ability of the     |
| RCIC system to remove residual heat.                                         |
|                                                                              |
| In the case of the RCIC Bypass to Condensate Storage Tank valve 2-E51-F022,  |
| with the valve de-energized in the open position, injection flow into the    |
| RPV is not diverted to the Condensate Storage Tank, or into the High         |
| Pressure Coolant Injection system due to additional closed valves in the     |
| test flow path. Therefore, if the RCIC system had been called upon to        |
| perform its needed function to remove residual heat, the system would have   |
| performed as required.                                                       |
|                                                                              |
| In the case of the RCIC Torus Suction valve 2-E51-F029, although the ability |
| for the RCIC system sump suction to align to the Torus must be available to  |
| meet its Technical Specification LCO Operability requirements, the RCIC      |
| system has the capacity to meet its function to remove residual heat when    |
| aligned to the Condensate Storage Tank. Although the RCIC system is a single |
| train injection system, it has redundant suction flow paths that are fully   |
| capable of meeting these injection requirements.  Loss of one suction flow   |
| path does not prevent the RCIC system from performing its required function  |
| to remove residual heat.                                                     |
|                                                                              |
| Subsequently, it has been determined that the malfunction of the RCIC system |
| components did not adversely impact that system function to remove residual  |
| heat.  Carolina Power and Light Company has determined that this event does  |
| not meet 10 CFR 50.72 or 10 CFR 50.73 reporting criteria and this            |
| notification is being retracted.                                             |
| NRC R2DO (Chuck Ogle) notified.                                              |
|                                                                              |
| The NRC Resident Inspector was notified of this retraction by the licensee.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37659       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PILGRIM                  REGION:  1  |NOTIFICATION DATE: 01/11/2001|
|    UNIT:  [1] [] []                 STATE:  MA |NOTIFICATION TIME: 17:37[EST]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        01/11/2001|
+------------------------------------------------+EVENT TIME:        17:15[EST]|
| NRC NOTIFIED BY:  ERIC OLSON                   |LAST UPDATE DATE:  01/11/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:                                |DAVID LEW            R1      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DISCOVERY OF CONDITION INVOLVING INABILITY OF THE LOW PRESSURE COOLANT       |
| INJECTION (LPCI) SYSTEM TO PERFORM DESIGN FUNCTION BETWEEN APRIL 1999 AND    |
| JANUARY 2001                                                                 |
|                                                                              |
| "On 1/2/01, discovered incorrect relays (27-B2X2 and 27-B2Z2) had been       |
| installed in Bus B6 (480 VAC swing bus) during RFO 12 (April, 1999).  The    |
| bus transfer logic was declared inoperable at the time and entry was made    |
| into a 7-day cold shutdown LCO for LPCI.                                     |
|                                                                              |
| "Further analysis of the circuit has determined that the B6 Bus would have   |
| remained de-energized following a loss of offsite power if the 'A' side      |
| power supply became unavailable (i.e., 'A' Emergency Diesel failed or 'A'    |
| 125 VDC Battery failed).                                                     |
|                                                                              |
| "This condition is outside the design in accordance with Pilgrim Station     |
| FSAR.                                                                        |
|                                                                              |
| "The relays were replaced with the correct design and the LPCI LCO cleared   |
| at approximately 0745 Sunday, January 7, 2001."                              |
|                                                                              |
| The licensee will inform the NRC resident inspector.                         |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021