Event Notification Report for December 19, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/18/2000 - 12/19/2000 ** EVENT NUMBERS ** 37532 37608 37613 37614 37615 37616 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37532 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 11/17/2000| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 20:41[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/17/2000| +------------------------------------------------+EVENT TIME: 20:10[EST]| | NRC NOTIFIED BY: SCOTT RICHARDSON |LAST UPDATE DATE: 12/18/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 ENTERED TS 3.0.3 AFTER DECLARING BOTH LOOPS ECCS INOPERABLE | | | | "Tech Spec 3.5.2 requires two independent Emergency Core Cooling System | | (ECCS) loops, each capable of taking suction from the Refueling Water | | Storage Tank (RWST) and being transferred to the containment recirculation | | sump. This spec applies in modes 1 - 3. Following evaluation of recent | | modifications to the containment recirc sump ECCS suction isolation valves, | | it has been determined that neither of the two isolation valves (2-ICM-305 | | and 2-ICM-306) could be relied upon to open when transfer of ECCS suction is | | required. This is attributed to a lack of assurance that between seat | | relief valves on 2-ICM-305 and 2-ICM-306 would lift and preclude thermal | | hydraulic locking of the valves in the closed position. Since neither ECCS | | loop recirc sump suction is operable, the action statement of TS 3.5.2 is | | not valid. This led to the Shift Manager declaring entry into TS 3.0.3 with | | a requirement to place the unit in a mode for which TS 3.5.2 does not apply. | | A unit shutdown at 2% per hour has been initiated. Plans are to implement | | compensatory actions or have the unit in hot standby within 6 hours." | | | | The licensee anticipates exiting TS 3.0.3 after bleeding the fluid trapped | | between the double disk valves in approximately two hours. The licensee | | informed the NRC resident inspector. | | | | * * * UPDATE 0310 11/18/2000 FROM RICHARDSON TAKEN BY STRANSKY * * * | | | | The united exited the shutdown LCO at 2315. Reactor power had been reduced | | from 100% to 90%. The licensee removed approximately 4.5 gallons of water | | from the body of each valve in order to prevent thermal locking. The NRC | | resident inspector will be informed. Notified R3DO (Jorgensen). | | | | ***** UPDATE AT 1834 ON 12/18/00 FROM BRENDA L'ROURKE TO LEIGH TROCINE | | ***** | | | | The licensee is retracting this event notification. The following text is a | | portion of a facsimile received from the licensee: | | | | "The Donald C. Cook Nuclear Plant is withdrawing [its] 1-hour Non-Emergency | | notification made to the NRC at 2041 hours on [11/17/00] (Event # 37532). | | At that time, it was reported that Unit 2 entered TS 3.0.3 after declaring | | both ECCS loops inoperable. Both loops were declared inoperable because | | neither of the two containment recirculation sump ECCS suction isolation | | valves (2-ICM-305 and 2-ICM-306), could be relied upon to open when transfer | | of ECCS suction is required. This was attributed to a lack of assurance | | that the thermal relief valves (2-SV-344 East and West) installed between | | the seats of 2-ICM-305 and 2-ICM-306, would lift at the required 20 psid | | design pressure to preclude thermal hydraulic locking of the normally closed | | ECCS suction valves. These relief valves were installed prior to Unit 2 | | entering Mode 4. On [11/18/00] at 2315 hours, Unit 2 exited the TS-required | | shutdown after 2-ICM-305 and 2-ICM-306 were declared operable after | | approximately 4.5 gallons of water was drained from each valve." | | | | "Further Engineering evaluation concluded that both ECCS loops are and have | | been operable because 2-ICM-305 and 2-ICM-306 were determined not to be in a | | 'water solid' condition and, therefore, not susceptible to thermal hydraulic | | locking. This conclusion was confirmed by draining the volume of fluid | | present between the ECCS suction valve seats and comparing the total amount | | of fluid drained to the free space available inside each valve. It was | | determined, by calculation, that of the 30 gallons of free space available | | inside each valve, only 2 gallons of free space are needed to ensure the | | valves will open when transfer of ECCS suction is required. Both valves | | were drained on three separate occasions between 11/17/00 and 11/22/00. A | | total of 6.74 gallons was drained from 2-ICM-305, and a total of 8.25 | | gallons was drained from 2-ICM-306. Based on the total amount of fluid | | drained from each valve, both 2-ICM-305 and 2-ICM-306 have been operable | | during all periods when the ECCS is required to be operable." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R3DO (Kozak). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37608 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 12/17/2000| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 00:57[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/16/2000| +------------------------------------------------+EVENT TIME: 23:00[CST]| | NRC NOTIFIED BY: JAMES MERTINK |LAST UPDATE DATE: 12/18/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHUCK CAIN R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |ACCS 50.72(b)(1)(iv) ECCS INJECTION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO CLOSURE OF TURBINE GOVERNOR VALVES | | | | "Unit 1 manually tripped the reactor at 2300 on 12/16/00. The unit was in | | the process of performing main turbine valve operability testing when all | | four Governor Valves went closed. The crew manually tripped the reactor and | | entered emergency operating procedures. Primary pressure continued to lower | | to the Safety Injection actuation setpoint. All ESF equipment actuated and | | performed as expected with the exception of one Source Range Nuclear | | Instrument. The cause of the Safety Injection actuation is not fully | | understood at this time." | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | ***** UPDATE AT 2330 EST ON 12/18/00 FROM JOHN PIERCE TO LEIGH TROCINE | | ***** | | | | The following text is a portion of a facsimile received from the licensee: | | | | "This is a supplemental notification to EVENT #37608 for a [1-hour] report | | for any event that results or should have resulted in Emergency Core Cooling | | System (ECCS) discharge into the RCS as a result of a valid signal | | (10CFR50.72(b)(1)(iv)(B)) and [for a 4-hour] notification [for] RPS | | actuation and ESF actuation (10CFR50.72(b)(2)(ii))." | | | | "Unit 1 was preparing to [perform] main turbine valve operability testing | | when all four governor valves went closed. Unit 1 was manually tripped at | | 2300 [CST] on 12/16/2000, and emergency operating procedures were entered. | | Safety injection occurred approximately 1 minute and 25 seconds following | | the reactor trip. All ESF equipment responded normally during the safety | | injection including initiation of auxiliary feedwater (AFW) flow to the | | steam generators. RCS pressure lowered to approximately 1470 psig within | | approximately 6 minutes of safety injection actuation prior to recovering | | and increasing pressure. Taking manual control to close the pressurizer | | spray valves, after indicating not fully closed, and throttling AFW flow | | appeared to stop the pressure decrease. Safety injection termination | | criteria was met, and the safety injection was terminated by approximately | | 2348 hours [CST]." | | | | "The highest RCS pressure was 2303 psig. An adequate margin of subcooling | | was maintained, and the reactor head area indicated it remained water solid | | during the transient. Maximum pressurizer level during the event was | | approximately 63.8%. Following termination of the transient, it was noted | | that RCS temperature did not return to the expected no-load temperature | | value. Plant walk down found 3 of 12 steam dump valves approximately 10% | | open which contributed to the initial plant cooldown. These valves were | | isolated." | | | | "An STP Event Review Team is analyzing plant data to determine the | | [detailed] sequence of events and cause of event." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R4DO (Bill Jones). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37613 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 12/18/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 09:52[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/18/2000| +------------------------------------------------+EVENT TIME: 06:40[EST]| | NRC NOTIFIED BY: RUSS GUMBERT |LAST UPDATE DATE: 12/18/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN WHITE R1 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTAINMENT FAN COOLER UNITS DECLARED INOPERABLE | | | | "At 0640 on 12/18/00, '11' service water accumulator was declared inoperable | | based on water level low out of specification for Technical Specifications. | | This condition was identified following calibration of the 'B' level device. | | The service water accumulators support containment integrity by ensuring the | | containment fan coils remain properly filled during a design basis accident. | | Tech Spec 3.6.1.1 and Tech Spec 3.6.2.3 were entered for containment | | integrity and '11' and '12' containment fan coil unit inoperability. Actions | | were taken within one hour to comply with containment integrity Tech Spec. | | The service water accumulator was filled to within specification at 0713 at | | which time Tech Spec 3.6.1.1 was exited. The '11' and '12' containment fan | | coil units were restored to operable at 0744 and Tech Spec 3.6.2.3 was | | exited. Actions are underway to calibrate the 'A' channel of level | | indication. All power plant parameters remained stable throughout the event | | and no other safety systems were affected." | | | | The NRC resident inspector will be informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37614 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 12/18/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 15:58[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/18/2000| +------------------------------------------------+EVENT TIME: 13:29[CST]| | NRC NOTIFIED BY: ROBERT POWERS |LAST UPDATE DATE: 12/18/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS KOZAK R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM DUE TO ISOLATION OF THE MAIN STEAM ISOLATION VALVES | | DURING THE PERFORMANCE OF MAINTENANCE/SURVEILLANCE (Refer to event #37616 | | for details regarding an additional reactor scram.) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 1329 CST, the plant experienced an isolation of the 'Main Steam | | Isolation Valves which subsequently initiated an automatic reactor SCRAM. | | The Main Steam Isolation Valve Closure was part of a Group I isolation which | | is believed to be caused by performance of a maintenance surveillance on the | | Main Steam Line Tunnel Leak Detection System." | | | | "The plant is stable, and there were no other abnormal occurrences in | | conjunction with this event." | | | | "Since closure of the Main Steam Isolation Valves is an actuation of the | | Reactor Protection System this condition is being reported pursuant to | | 10CFR50.72(b)(2)(ii)." | | | | The licensee stated that all control rods fully inserted due to the reactor | | scram and that the reactor core cooling isolation system was manually | | actuated and secured during this event. There were no emergency core | | cooling systems actuations, and none were required. The licensee's | | investigation is currently ongoing. | | | | The licensee also stated that water is currently being supplied to the | | reactor vessel via normal condensate and feedwater and that safety relief | | valves are being utilized for pressure control. Containment parameters were | | reported to be normal, and offsite power is available. The emergency core | | cooling systems are also available if required. | | | | The licensee notified the NRC resident inspector and the State. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37615 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 12/18/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 19:30[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 12/18/2000| +------------------------------------------------+EVENT TIME: 14:36[CST]| | NRC NOTIFIED BY: STEVE WHEELER |LAST UPDATE DATE: 12/18/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BILL JONES R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |65 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TRIP OF A RECIRCULATION PUMP DUE TO LOSS OF A SUPPORT SYSTEM FOLLOWING LOAD | | SHEDDING FROM AN ESSENTIAL BUS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "During surveillance testing of the Division I undervoltage logic, a step | | was performed out of sequence. This resulted in load shedding from the | | Division I essential bus. Undervoltage actuations occurred as expected | | including a trip of one reactor [recirculation] pump. Plant operation was | | stabilized in single loop operation with recovery planning in progress." | | | | The licensee stated that the unit was operating at 100% power prior to the | | event and that it is currently operating at 65% power (in single loop | | operation). It was reported that the trip of the recirculation pump was not | | the direct result of the undervoltage condition. It actually occurred due | | to the loss of a support system because the load shedding resulted in a loss | | of power to an oil pump that supplied the recirculation pump. All systems | | functioned as expected, and there was nothing unusual or misunderstood. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37616 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 12/18/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 21:00[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/18/2000| +------------------------------------------------+EVENT TIME: 18:45[CST]| | NRC NOTIFIED BY: MONTY KNAPP |LAST UPDATE DATE: 12/18/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS KOZAK R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM ON REACTOR PRESSURE VESSEL (RPV) LOW LEVEL 3 WHILE | | THE UNIT WAS IN HOT SHUTDOWN (Refer to event #37614 for details regarding a | | previous reactor scram.) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 1845 CST, the plant was in Mode 3 with the scram reset. Roughly 5 hours | | earlier the plant had experienced a scram upon a Group 1 isolation. While | | re-opening the MSIVs to re-establish the main condenser as the heat sink and | | transfer pressure control, the plant experienced an RPV Low Level 3 and | | scrammed." | | | | "The MSIVs are now open, the scram reset, and level and pressure are | | stable." | | | | The licensee stated that RPV Low Level 3 occurs at +8.9 inches narrow | | range. | | | | It was reported that the unit experienced a problem with the procedure which | | delayed opening of the MSIVs. As pressure creeped up which caused the pumps | | that were feeding the vessel to feed less. Therefore, level started | | creeping down as pressure started creeping up. It is not believed that | | level went much below RPV Low Level 3 because water would have been injected | | as a result of the scram. The licensee stated that there were no engineered | | safety feature actuations or emergency core cooling injections and that none | | were required. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021