Event Notification Report for September 11, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/08/2000 - 09/11/2000 ** EVENT NUMBERS ** 37266 37268 37299 37300 37301 37302 37303 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37266 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 08/28/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 20:17[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 08/28/2000| +------------------------------------------------+EVENT TIME: 16:30[EDT]| | NRC NOTIFIED BY: RICHARD LANGE |LAST UPDATE DATE: 09/08/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETE ESELGROTH R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INOPERABILITY OF THE PASS AND BOTH DIVISION I/II H2O2 MONITORING SYSTEMS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 8/28/2000, at 1630, [the Division] I and [II] Hydrogen/Oxygen (H2O2) | | Containment Monitoring Systems were declared inoperable. The Division I | | system was declared inoperable on 8/28/2000, at 0818, for planned | | maintenance. Subsequently, the Division II system was declared inoperable | | due to a failed channel check." | | | | "In addition, the Post Accident Sampling System (PASS) was previously | | declared inoperable. With the PASS and both Division I/II H2O2 Monitoring | | Systems inoperable, this event is reportable in accordance with 10 CFR | | 50.72(b)(2)(iii)(D)." | | | | "Also, on 8/28/2000, at 1905, the Division I H2O2 Monitor was restored to | | operable [status] following completion of planned maintenance." | | | | The licensee stated that the unit remained in a 30-day limiting condition | | for operation (LCO) and that a 7-day shutdown LCO was exited when the | | Division I H2O2 Monitor was restored to operable status. | | | | The licensee notified the NRC resident inspector. | | | | ***** UPDATE/RETRACTION AT 0024 ON 09/08/00 FROM ANTHONY PETRELLI TO LEIGH | | TROCINE ***** | | | | The licensee is retracting this event notification. The following text is a | | portion of a facsimile received from the licensee: | | | | "On 08/28/00, 1630 EDT, Nine Mile Point Unit 2 reported that Divisions 1 and | | 2 of the Hydrogen/Oxygen (H2/02) Containment Monitoring Systems were | | declared inoperable under Event Number 37266." | | | | "[The licensee is] retracting that notification based on the fact that the | | Division 1 H2/O2 monitoring system was removed from service as part of | | planned maintenance in accordance with approved procedures and plant | | Technical [Specifications]. During planned maintenance, a discrepancy was | | found in the Division 1 H2/O2 system. Subsequent evaluation indicated that | | the condition discovered would not have prevented the system from performing | | its safety function if called upon. Therefore, this event is not | | reportable." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R1DO (Dimitriadis). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37268 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/29/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 01:36[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/28/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:29[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/09/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MELVYN LEACH R3 | | DOCKET: 0707002 |JOSEPHINE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RICK LARSON | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT | | | | "On 8/28/00 at 1529, during implementation of NCSA 0705_076 (Inadvertent | | Containers) a concern was raised about the maximum distance of spray from a | | leak from a pressurized pipe. Calculations were reevaluated and the | | corrected spray distance for the system in question resulted in a distance | | of 106 feet. This new distance for the system in question is greater than | | the original implementation distance of 15 feet, which the NCSA had | | previously predicted for the entire X-705. This is considered a loss of one | | control. The control considered lost is control #2 which states in part, | | 'When unattended all potential inadvertent containers shall be: | | -modified to prevent unsafe accumulation | | -covered to prevent the in-leakage of spilled materials | | -oriented to prevent an unsafe accumulation | | | | "The PSS(Plant Shift Superintendent) directed the facility custodian to | | enter an anomalous condition. The system in question was previously shut | | down prior to recalculation of the spray distance. The same equipment | | remains shutdown until compliance with NCSA 0705_076 can be determined. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | | | "Safety significance is low. The resulting situation is conservatively being | | identified as a violation of one control contained in NCSA 0705_076 which | | requires that all potential inadvertent containers utilized in the X-705 be | | modified, covered, or oriented to prevent an unsafe accumulation. However, | | since the system in question maintained its physical integrity and thus no | | uranium bearing material was involved the safety significance of this event | | is low. | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | "If a sufficient amount of uranium bearing material had leaked, spilled, | | splashed from the micro filtration system and the resuming material | | accumulated on/in an inadvertent container, an unsafe geometry could have | | resulted. If the leaking solution had contained a sufficient amount of | | uranium, the resulting configuration could have been sufficient for a | | criticality to occur. it should be noted that the allowed safe geometry and | | volume limits established in NCSA 0705-076 are based on optimally moderated | | solution which contains uranium enriched to 100 wt% U235. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC): | | | | "The parameter which was violated during this upset was maintaining | | geometry/volume controls regarding potential accumulation points available | | on/in nearby inadvertent containers. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | "No uranium-bearing material was actually involved in the upset. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | "NCSA 0705_076 takes credit for the physical integrity of systems which | | contain uranium bearing materials. NCSA 0705_076 also takes Credit that | | unsafe volume/geometry containers are either modified, covered or oriented | | while in areas where uranium bearing material can leak, spill or spray to | | prevent an unsafe configuration from resulting in the event of a leak. The | | administrative control #2 was not being followed for the new area identified | | where uranium bearing materials can leak, spill or spray. The resulting | | situation is conservatively being identified as a violation of the | | administrative control in NCSA 0705_076. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | "The PSS (Plant Shift Superintendent) directed the facility custodian to | | enter an anomalous condition. The system in question was previously shut | | down prior to recalculation of the spray distance. The same equipment will | | remain shutdown until NCS (Nuclear Criticality Safety) can assist in | | determination of operability of that system and compliance with NCSA | | 0705_076." | | | | The NRC resident inspector has been informed of this event. | | | | * * * UPDATE 1021EDT ON 9/9/00 FROM JEFF CASTLE TO S. SANDIN * * * | | | | "9/9/00 - Update #1 - An engineering evaluation (EVAL-PS-2000-0415) of the | | system and pumps associated with implementation of NCSA_0705_076 identified | | that the spray distances used to originally determine the reportability of | | this event were excessive. The original distance (15 feet) used to implement | | this NCSA has since been identified to adequately bound the credible | | scenarios for solutions spraying from various systems in the X-705. This | | issue would not have been reportable based on the newly acquired information | | as a result of the recent technical review." | | | | The NRC resident inspector and DOE site representative have been informed. | | Notified R3DO(Shear). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37299 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 09/08/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 15:39[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/08/2000| +------------------------------------------------+EVENT TIME: 13:30[EDT]| | NRC NOTIFIED BY: PAUL UNDERWOOD |LAST UPDATE DATE: 09/08/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK LESSER R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM DECLARED INOPERABLE | | | | "At 1330 on 09/08/00, HPCI Flow Controller, 1E41-R612, was observed to be | | exhibiting erratic indication of flow. Flow indication was oscillating from | | 0 to >500 gpm with HPCI in its standby condition. Investigation is | | continuing." | | | | The NRC resident inspector will be informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37300 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/09/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:21[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/08/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 20:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/09/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |GARY SHEAR R3 | | DOCKET: 0707002 | | +------------------------------------------------+ | | NRC NOTIFIED BY: JEFF CASTLE | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT INVOLVING SAFETY SYSTEM ACTUATION | | | | "On 9/8/2000 at 2000 hours a safety system actuation occurred in the X344 | | building. Autoclave #4 was in Mode II 'Heating' when the High Condensate | | Level Shutoff safety system actuated. Per TSR 2.1.3.7, the autoclave was | | placed in Mode VII 'Shutdown', a mode in which the High Condensate level | | Shutoff system is not required, and declared inoperable. This is being | | reported as a valid safety system actuation. An engineering evaluation has | | been initiated to review the system conditions that surrounded the actuation | | of the safety system." | | | | Operations notified both the NRC resident inspector and DOE site | | representative. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37301 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CROW BUTTE RESOURCES |NOTIFICATION DATE: 09/10/2000| |LICENSEE: CROW BUTTE RESOURCES |NOTIFICATION TIME: 09:52[EDT]| | CITY: CRAWFORD REGION: 4 |EVENT DATE: 09/09/2000| | COUNTY: STATE: NE |EVENT TIME: 18:30[CDT]| |LICENSE#: SUA1534 AGREEMENT: Y |LAST UPDATE DATE: 09/10/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JOHNSON R4 | | |DANIEL GILLEN NMSS | +------------------------------------------------+E. WILLIAM BRACH NMSS | | NRC NOTIFIED BY: MIKE GRIFFIN | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONDITION OF LICENSEE REPORT INVOLVING A MONITOR WELL EXCURSION | | | | RESULTS OF SAMPLES REPORTED AT 1830MDT ON 9/9/00 CONFIRMED THAT FOUR | | PARAMETER SINGLE UPPER CONTROL LIMITS (UCLs) AND THE FIFTH MULTIPLE UCL | | WERE EXCEEDED IN SHALLOW MONITOR WELL SM6-12. | | | | PARAMETERS /UCLs/ MEASURED VALUES[UNITS] ARE: | | | | SODIUM /36/ 43 | | [milligrams/liter] | | SULFATE /19/ 85 | | [milligrams/liter] | | CHLORIDES /7/ 55 | | [milligrams/liter] | | CONDUCTIVITY /736/ 910 | | [microMHOs/cm] | | ALKALINITY /290/ 294 | | [milligrams/liter] | | | | THE LICENSEE WILL DISCUSS POSSIBLE CORRECTIVE ACTIONS WITH THEIR HYDROLOGIST | | AND GEOLOGISTS IN THE MORNING. THIS COULD INCLUDE DRILLING SAMPLE TEST | | WELLS. | | | | THE LICENSEE WILL NOTIFY THE NEBRASKA DEPARTMENT OF ENVIRONMENTAL QUALITY | | AND THE NRC PROJECT MANAGER. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37302 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATTS BAR REGION: 2 |NOTIFICATION DATE: 09/10/2000| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 19:55[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/10/2000| +------------------------------------------------+EVENT TIME: 16:28[EDT]| | NRC NOTIFIED BY: BENJAMIN HUNT |LAST UPDATE DATE: 09/10/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK LESSER R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC START OF TURBINE DRIVEN AUXILIARY FEEDWATER PUMP | | | | "At 1628 hours on 9/10/2000, with the reactor in Mode 5 for a refueling | | outage; Watts Bar engineering reported preliminary results of an | | investigation into the inadvertent start of the turbine driven auxiliary | | feedwater pump. At approximately 0200 hours on 9/10/2000, operators found | | the auxiliary feedwater pump operating without the presence of start signal. | | Steam generator level was being provided by previously started motor driven | | AFW pumps and operations secured the turbine driven pump. There was no | | impact from the event on plant refueling preparations and no safety | | consequence. | | | | "There was no valid AFW start signal in place at the time and plant | | conditions were not such that a signal was required. Engineering was | | requested to investigate the event and identified that at about the time of | | the pump start, maintenance technicians were working in an adjacent part of | | this rack where the relay believed to have been involved in the actuation is | | located. A review of the circuit determined that an inadvertent bump of the | | relay could result in the start of the pump and the independent actuation of | | turbine driven AFW steam generator level control valves. Based on this | | information, Operations concluded that based on the preliminary engineering | | information an invalid start of an ESF train had occurred and declared the | | event reportable under 10 CFR 50.72(b)(2)(ii) and 50.73(a)(2)(iv). | | | | "At the time the pump was found in operation it was known that there was no | | valid start signal, but it was thought that the issue involved only a single | | component. Because other S/G level maneuvers were in process independent of | | the AFW start, it was not recognized at the time that the level control | | valves were involved in the event. After the preliminary engineering review, | | it was concluded that although it was an invalid actuation, the event | | involved a train level actuation and was, therefore, reportable." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37303 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 09/10/2000| | UNIT: [1] [] [] STATE: MD |NOTIFICATION TIME: 23:02[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 09/10/2000| +------------------------------------------------+EVENT TIME: 21:23[EDT]| | NRC NOTIFIED BY: ROBERT PACE |LAST UPDATE DATE: 09/11/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANTHONY DIMITRIADIS R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO CLOSURE OF MAIN STEAM ISOLATION VALVES | | | | An automatic reactor trip/turbine trip occurred due to the spurious closure | | of both main steam isolation valves (MSIVs). The spurious MSIV closure was | | the result of a failed logic module in the engineered safety features | | actuation system (ESFAS). All control rods inserted following the trip, and | | all systems functioned as expected. The auxiliary feedwater (AFW) system | | automatically started as designed following the trip. The unit is currently | | stable in Hot Standby with decay heat being removed through steam released | | via the steam generator atmospheric dump valves. Steam generator water | | levels are being maintained by the AFW system. | | | | The licensee anticipates that replacement of the logic module and | | establishment of decay heat removal via the main condenser will occur within | | the next few hours. The NRC resident inspector has been informed of this | | event by the licensee. The licensee reported that nearby residents have | | contacted emergency services regarding the noises caused by the steam | | release through the atmospheric dump valves. The licensee plans to make a | | press release regarding this event. | | | | * * * UPDATE 0428EDT ON 9/11/00 FROM ROBERT PACE TO S. SANDIN * * * | | | | The MSIVs were reopened and the main condenser placed back in service at | | 0420EDT for decay heat removal. Preparations are underway to restore one | | main feedwater pump and secure the AFW system. Notified R1DO(Dimitriadis). | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021