Event Notification Report for June 9, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/08/2000 - 06/09/2000 ** EVENT NUMBERS ** 37021 37067 37068 37069 37070 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37021 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/23/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 08:44[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/23/2000| +------------------------------------------------+EVENT TIME: 05:05[EDT]| | NRC NOTIFIED BY: ART BREADY |LAST UPDATE DATE: 06/08/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 4 Startup |4 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HIGH PRESSURE COOLANT INJECTION SYSTEM INOPERABLE DUE TO STUCK OPEN CHECK | | VALVE - | | | | At 0505 on 05/23/00, the High Pressure Coolant Injection (HPCI) System was | | determined to be inoperable as a result of the discharge check valve being | | stuck partially open. This condition was discovered during investigation of | | a low injection header pressure alarm, and subsequent attempts to fill and | | vent the discharge header were unsuccessful. It is believed that the check | | valve stuck partially open when the system was secured after a low pressure | | surveillance test at about 0305. The discharge check valve was mechanically | | agitated at 0700, and reseated as evidenced by an audible sound and rise in | | injection header pressure. | | | | At the time of discovery, the plant was in Operational Condition 2 with | | reactor power at 4% and reactor pressure at approximately 500 psig. All | | other safety related equipment was operable at the tune of discovery, with | | the exception of the 'A' Residual Heat Removal Pump, which was aligned for | | suppression pool cooling mode of operation. There was no significant impact | | to overall plant safety as a result of this condition. | | | | Plant maintenance and engineering personnel are currently evaluating the | | failure of the HPCI System discharge check valve. injection header fill and | | vent is in progress to determine the amount of air that is present and | | restore the system to an available condition. This information will be used | | to determine if the safety function of the HPCI System was unavailable as a | | result of the discharge check valve malfunction. | | | | A root cause investigation team has been assembled, and evaluation of system | | and personnel performance is in progress. | | | | The licensee notified the NRC Resident Inspector and plans to notify local | | officials. | | | | * * * UPDATE ON 6/8/00 @ 1219 BY CONICELLA TO GOULD * * * RETRACTION | | | | | | | | As discussed in the notification. the HPCI low discharge header pressure | | alarm was received, prompting an immediate investigation. The discharge | | check valve was mechanically agitated which resulted in the seating of the | | valve and clearing of the alarm. Sticking of the discharge check Valve | | provided a leakage path thus preventing the keep fill system from achieving | | pressure sufficient to clear the alarm setpoint. The amount of mechanical | | agitation required was minimal. HPCI was then removed from service to allow | | maintenance troubleshooting on the valve. | | | | It is believed that the discharge check valve stuck in the partially open | | position following the low pressure response time surveillance testing which | | had been completed approximately two hours prior to the event. This was a | | result of the low delta P across the valve associated with that testing. | | Prior to the cited surveillance test, a different HPCl surveillance (HPCI | | Flowpath Verification) had been successfully completed and HPCI had been | | determined to be operable. Investigation of the valve revealed very minor | | misalignment which may have been the cause at the slight binding. This | | condition would not prevent the safety function of HPCI from being | | performed. Following the investigation HPCI was removed from service and | | the plant entered a 14 day LCO. The valve was repaired and HPCI was retested | | and declared operable. The keep fill system was always sufficient. | | | | | | The NRC Resident Inspector will be notified. The Reg 1 RDO (Moslak) was | | notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37067 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 06/08/2000| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 11:09[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 06/07/2000| +------------------------------------------------+EVENT TIME: 11:16[EDT]| | NRC NOTIFIED BY: RICH DIBLER |LAST UPDATE DATE: 06/08/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE EMPLOYEE TESTED POSITIVE FOR ALCOHOL DURING A RANDOM | | FITNESS-FOR-DUTY TEST (24-HOUR REPORT) | | | | A non-licensed employee tested positive for alcohol during a random | | fitness-for-duty test conducted on 06/07/00. The individual has been | | relieved of duty and placed on indefinite suspension. The individual's | | access authorization has been suspended, and the licensee is currently | | reviewing the individual's activities. (Call the NRC operations officer for | | additional information.) | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37068 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 06/08/2000| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 13:11[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/08/2000| +------------------------------------------------+EVENT TIME: 09:31[EDT]| | NRC NOTIFIED BY: DEPUYDT |LAST UPDATE DATE: 06/08/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN JACOBSON R3 | |10 CFR SECTION: |ED GOODWIN NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION |MICHAEL CASE EDO | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N N 0 Hot Shutdown |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD AUTOSTART OF THE EMERGENCY DIESELS ON BOTH UNITS | | | | On June 8, 2000, at 0931 hours, power was lost to the CD bus on each unit | | during switching operations involving the #4 and #5 transformers in the main | | switchyard. During the switching operation a loss of offsite power occurred, | | affecting one train of 4KV electrical power in each unit and causing the | | auto start of the CD EDGs on each unit. The EDGs started and loaded as | | expected. | | | | Unit 1 is currently defueled. When power was lost, the Spent Fuel Pool | | Cooling pump that was in service tripped. It was placed back in service 0953 | | hours. The spent fuel pool temperature rose 1 degree from 84 to 85 during | | this time. Temperature is now stable at 85 degrees. | | | | Unit 2 is currently in Mode 4. When power was lost to the CD bus, Reactor | | Coolant pumps (RCPs) #22 and #23 tripped. Additionally, the 4 KV bus under | | frequency signal caused the #21 and #24 RCPs to trip as designed. As a | | result, Unit 2 was in the natural circulation mode using the steam | | generators as a heat sink. RCS temperature at the time of loss of power was | | 335 degrees and cooled to approximately 315 degrees during the time the unit | | was in natural circulation. | | | | Offsite power was restored through TR5 at 1019 hours. #24 RCP was restarted | | at 1047 hours, restoring forced circulation, #23 RCP was restarted at 1159 | | hours. RCPs #21and #22 are still currently secured. The unit is stable and | | equipment is being restored. | | | | An Event Response Team has been convened to assess the event, and develop | | recovery plans. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37069 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 06/08/2000| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 15:26[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 06/08/2000| +------------------------------------------------+EVENT TIME: 15:15[EDT]| | NRC NOTIFIED BY: RUSSEL LONG |LAST UPDATE DATE: 06/08/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OUTSIDE DESIGN BASIS - CABLE SEPARATION ISSUE | | | | At approximately 1515 hours on June 8, 2000, operations determined that | | plant cable separation criteria had potentially been violated which would | | place the plant outside the design basis. Two wires were routed from a test | | jack in the control rod cabinets located in the cable spreading room to a | | terminal block in Rack C3 in the control room. The routing of the wires | | takes them into cable trays in the cable spreading room that are carrying | | control cables for channels 1, 2 and 3. This is in violation of the | | electrical separation criteria defined in the FSAR. Corrective action is | | being taken to remove the wires from the cable trays. A preliminary | | evaluation indicates the wires were used during testing of the control rod | | drive mechanism during initial plant startup. They are no longer in use. | | This event was identified during an extent of condition walkdown for the | | separation criteria violation identified in incident log 37043, dated May | | 26, 2000. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37070 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 06/08/2000| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 15:59[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/08/2000| +------------------------------------------------+EVENT TIME: 07:45[CDT]| | NRC NOTIFIED BY: KATHLEEN WORK |LAST UPDATE DATE: 06/08/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN PELLET R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR REPORT - HIGH BATTERY ELECTROLYTE LEVEL | | | | On May 15, 2000, a surveillance test was performed on the E1A11 battery. | | The electrolyte level in cell #18 was reported as + � inch above the high | | level line on the cell which exceeds the Tech spec limit of < � inch, as | | stated in Tech Spec Table 4.8-2, Battery Surveillance Requirements for | | Category B. This condition was not recognized during Maintenance review of | | the data. Tech Spec Surveillance 4.8.2.1.b.1 which allows 7 days to restore | | electrolyte level within the Category B limits or declare the battery | | inoperable was exceeded and the battery was considered inoperable. The LCO | | for an inoperable battery, which is 2 hours to restore to operable or be in | | hot standby within 6 hours, was not met. This was a violation of Tech Spec | | 3.8.2.1.a. The condition was corrected on May 30, 2000. There is no safety | | significance to this event. The electrolyte level in cell 18 at no time | | compromised the ability of the E1A11 battery to perform its design | | function. | | | | 24-hour notification is being made pursuant to Operating License NPF-76, | | paragraph 2.G. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021