Event Notification Report for May 24, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/23/2000 - 05/24/2000 ** EVENT NUMBERS ** 36958 36980 37015 37018 37019 37020 37021 37022 37023 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36958 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 05/02/2000| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 17:10[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 05/02/2000| +------------------------------------------------+EVENT TIME: 07:40[CDT]| | NRC NOTIFIED BY: GARY HARRINGTON |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - 'A' TRAIN EMERGENCY SAFEGUARDS BUS UNEXPECTEDLY DEENERGIZED DURING | | MAINTENANCE - | | | | At 0740 CDT on 05/02/00, while electrical bus maintenance was in progress, | | the 'A' train emergency safeguards bus unexpectedly deenergized. | | DEENERGIZING the bus initiated an ESF start signal for the associated 'A' | | emergency diesel generator (EDG). At the time, the 'A' EDG had been removed | | from service for refueling outage scheduled maintenance and no EDG start | | occurred. | | | | In response to the loss of power to the 'A' train safeguards bus, the | | licensee manually started the 'B' train residual heat removal pump to | | reestablish decay heat removal There was no temperature rise in the | | primary system. | | | | The licensee is determining the cause of the bus deenergization. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE ON 5/23/00 @ 1216 BY HARRINGTON TO GOULD * * * RETRACTION | | | | "For the event that occurred on May 2, 2000, there was no actual ESF | | equipment (pumps, valves, etc.) actuated directly as a consequence of the | | event. Therefore, no ESF equipment operated to mitigate the event. As such, | | the event would not be reportable. However, there are implications that the | | reporting requirements apply equally to ESF signals that are generated as | | part of an event, regardless of whether the event caused equipment to | | operate or not. For instance, NUREG-1022 contains a paragraph that states, | | in part, that, " [t]he Statement of Considerations also indicates that | | "actuation" of multichannel ESF actuation systems is defined as actuation | | of enough channels to complete the actuation logic." Accordingly, the May 2 | | event was evaluated in greater detail considering that the loss of power to | | the bus in itself could be understood to be an ESF actuation. | | | | "At the time of the event, work on the emergency bus relays was in process. | | During the work the bus was unexpectedly de-energized when the breaker | | providing power to the bus from the off-site power source opened. From our | | investigation, it appears a relay which was not being directly worked on | | actuated. Since power was removed from the relay, the relay appears to have | | been bumped or jarred which manually actuated it. The relay that was | | actuated was a trip relay for the breakers providing power to the affected | | bus. | | | | "The ESF function that could be interpreted to be actuated as a result of | | the relay being actuated is the loss of power to the safeguards bus start | | signal to the associated diesel. However, the diesel was tagged out of | | service and the bus voltage restoring control circuit was defeated as part | | of the bus work that was in progress. | | | | "In order to defeat the voltage restoring circuit the bus voltage restoring | | control switch was placed in "manual," and the voltage restoring relays were | | de-energized. With the switch in manual, a voltage search signal is not | | generated. As a result, the diesel does not receive a start signal if a loss | | of power to the bus occurs. Additionally, as part of the voltage restoring | | circuit, once power is lost to the bus, a power search is initiated whereby | | the circuit electrically seeks an available off-site power source and then | | would seek the diesel if no off-site source were available. With the bus | | voltage restoring circuit in manual there was no power source search | | initiated. The bus power was not automatically restored, even though the | | power to the bus was available. | | | | "Included in NUREG-1022 are a number of examples of situations where NRC has | | described reportable events. Of those that are described, all either | | involved equipment (pumps, valves, etc.) that actuated or the condition that | | generated a signal needed the ESF function to mitigate the event whether | | equipment actuated or not. In the event reported on May 2, no equipment | | operated and there was no reliance on any accident mitigation function as | | well as no need for any accident mitigation feature. Therefore, the event | | should not have been reported as an ESF actuation simply because the | | condition that occurred could have resulted in an ESF signal being | | actuated. | | | | "According to the reporting criteria, if the actuation is invalid, and the | | system was properly removed from service a report need not be filed. | | According to NUREG-1022, "[v]alid ESF actuations are those that result from | | "valid signals" or from intentional manual initiation, unless it is part of | | a preplanned test. Valid signals are those signals that are initiated in | | response to actual plant conditions or parameters satisfying the | | requirements for ESF initiation. Note this definition of "valid" requires | | that the initiation signal must be an ESF signal. This distinction | | eliminates actuations which are the result of non-ESF signals from the class | | of valid actuations. Invalid actuations are, by definition, those that do | | not meet the criteria for being valid. Thus invalid actuations include | | actuations that are not the result of valid signals and are not intentional | | manual actuations." | | | | "The ESF signal of concern for the start of the diesel generator is that | | which is generated in response to a loss of off-site power to the affected | | bus. During the subject event, off-site power was not lost. Although the | | off-site power was not automatically restored according to normal system | | operational design, it remained available. Consequently, there was no need | | for the diesel to supply the bus and as such no valid signal was generated. | | Additionally, the power restoration circuit was properly removed from | | service during the event; the voltage restoring switch was in manual. | | Therefore, no ESF signal was generated. | | | | "In summary, the event described is not reportable based on 1) there not | | being a need for any ESF feature to mitigate the event, and 2) the event not | | causing a valid (or any) ESF signal along with the related ESF equipment | | being properly removed from service." | | | | | | The NRC Resident Inspector was notified. Reg 3 RDO (Hiland) was | | informed. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36980 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 05/07/2000| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 13:53[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 05/07/2000| +------------------------------------------------+EVENT TIME: 11:25[CDT]| | NRC NOTIFIED BY: TERRY GENCIUS |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNEXPECTED LOAD SHED OCCURRED DURING ELECTRICAL MAINTENANCE TESTING | | | | "On May 7, 2000 at 0933, electrical testing was being performed on the | | emergency diesel generator A load sequencer. The diesel generator was | | out-of-service at the time [for annual maintenance]. An unexpected load | | shed signal was developed, which removed charging pump C, service water pump | | A2, containment fan coil A, and residual heat removal (RHR) pump A from the | | train A emergency safeguards bus (Bus 5). In response to the load shed, | | equipment was manually restarted from the control room. RHR pump A was | | restarted in 90 seconds, restoring shutdown cooling. The cause of the load | | shed was the post modification testing of the load sequencer, and is | | continuing to be investigated." | | | | There was no increase in reactor coolant temperature during the 90 seconds | | without RHR flow. Also, the RHR B pump was available if it had been | | needed. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE ON 5/23/00 @ 1216 BY HARRINGTON TO GOULD * * * RETRACTION | | | | After further review, appears this event is NOT reportable based upon the | | initiation signal was invalid and the system was properly removed from | | service. Also the Load Shed Signal is a component of the Diesel Generator | | engineered safety feature (ESF) and not the actuation of the ESF train. | | | | "NUREG 1022, "Event Reporting Guidelines: 10 CFR 50.72 and 50.73" Revision I | | (NUREG 1022) provides guidance on what the NRC wants the industry to report. | | Under section 3.3.2, "Actuation of an Engineered Safety Feature or the RPS" | | is a definition of "valid signals." Valid signals are those signals that | | are initiated in response to actual plant conditions or parameters | | satisfying the requirements for ESF initiation. The actual plant condition | | that actuates this ESF is an undervoltage condition on Bus 5, this did not | | occur therefore it was an invalid signal. | | | | "During the test for DCR 3002 initial conditions were in place to prevent | | the ESF from providing its intended feature. Preventive Maintenance | | Procedure (PMP) 42-14, "DGE-Train "A" Auto Sequencing Test with Diesel A in | | Pullout (Degraded Grid)" disables the ESF by placing the control switch (ES | | 46641) for Emergency Diesel Generator A in "PULLOUT." To start the test the | | control room operator places the Bus 5 Voltage Restoring Logic Test switch | | to the "TEST" position, this disables the rest of the ESF from actuating | | unless a valid signal is generated. | | | | "By looking at the actions required to mitigate the consequences of a | | significant event, the load shed is only one component of the safety | | feature. The shedding of loads from bus 5 does not, of itself, mitigate the | | consequences of any significant event. | | | | "In addition, during the test sequence the load shed relays are in a state | | which, if not blocked, would cause the same equipment to trip. This event | | occurred because the block was removed prior to the load shed relays | | resetting to their normal state. | | | | "Therefore, one component, Load Shed, of the Diesel Generator ESF actuated | | due to an invalid signal while the ESF was properly removed from service. | | Thus the event is not reportable." | | | | The NRC Resident Inspector was notified. Reg 3 RDO (Hiland) was informed. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37015 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 05/22/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 04:48[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 02:53[EDT]| | NRC NOTIFIED BY: BOB KIDDER |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN MADERA R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - ESF ACTUATION OF REACTOR WATER CLEANUP SYSTEM FOR UNKNOWN REASONS - | | | | At 0253 on 05/22/00, the plant experienced an isolation of the Reactor Water | | Cleanup System on a Division 2 isolation signal when the Residual Heat | | Removal heat exchanger vent valve closed unexpectedly. An apparent | | electrical power supply spike to the Division 2 isolation instrumentation | | occurred. No testing or maintenance activities or electrical storms were | | occurring at the time of the isolation. The licensee is investigating the | | cause of the isolation. | | | | The licensee notified the NRC Resident Inspector. | | | | | | * * * UPDATE ON 5/23/00 @ 1317 BY SANFORD TO GOULD * * * RETRACTION | | | | Upon further review, "the power supply fluctuation was determined to be | | caused by a failed capacitor in a Division 2 regulating transformer and the | | Division 2 electrical distribution subsystem was declared inoperable. The | | momentary power system perturbation caused a partial ESF isolation to be | | generated with the voltage on the Division 2 electrical distribution system | | remaining at the specified value. Since there was not an actual loss of | | power to the divisional subsystem that would have required an ESF actuation | | on loss of power, this is not a valid signal. Therefore, in accordance with | | 10 CFR 50.72(b)(2)(ii)(B), Reactor Water Clean-Up isolations from invalid | | signals are not reportable. | | | | "Additionally, the Residual Heat Removal (RHR) Heat Exchanger Vent valve is | | a single component of a complex train (Both RHR and Isolation System) and | | does not, in itself, mitigate the consequences of a significant event. | | Therefore, in accordance with the guidance provided in NUREG 1022, Section | | 3.3.2, the vent valve closure is not reportable. | | | | "The electrical distribution power supply was restored to Operable at 1701, | | May 22. 2000." | | | | The NRC Resident Inspector was notified. The Reg 3 RDO (Hiland) was | | informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37018 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 05/23/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 00:11[EDT]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 21:59[CDT]| | NRC NOTIFIED BY: JOHN LECHMAIER |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AUTO Rx SCRAM FROM 100% AFTER REPLACEMENT OF MAIN TURBINE CONTROL VALVE | | SOLENOID - | | | | On 05/21/00, the Unit 2 Main Turbine #1 Control Valve Fast Acting Solenoid | | failed its required Tech Spec Surveillance Test. | | | | At 2159 CDT on 05/22/00, during return to service activities following | | replacement of this solenoid, Unit 2 automatically scrammed from 100% power | | due to receipt of an APRM High-High RPS Actuation signal. All control rods | | inserted completely. No safety/relief valves lifted. Steam is being dumped | | to the main condenser. During the transient, reactor vessel water level | | dropped to +8 inches (normal level is +30 inches) and all PCIS Group II | | actuations occurred, as expected. These actuations included Reactor | | Building Ventilation Valves closed, Train 'A' Standby Gas Treatment System | | auto started (Train 'B' SBGT System was inoperable), Control Room | | Ventilation System isolated, and Containment Isolation Valves closed. Quad | | Cities has one Emergency Diesel Generator (EDG) for each unit and a shared | | EDG. The Unit 2 EDG received a spurious auto start signal during the 4 KV | | auxiliary bus power transfer to the reserve transformer. The licensee | | secured the Unit 2 EDG. | | | | Unit 2 is now stable in Condition 3 (Hot Shutdown) with reactor vessel water | | level within its normal band. | | | | This event had no effect on Unit 1 which is at 100% power. | | | | The licensee is investigating the cause of this reactor scram. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 0708 ON 05/23/00 BY JOHN LECHMAIER TO JOLLIFFE * * * | | | | During the above transient, the reactor vessel water level reached +8 inches | | and all PCIS Group II actuations occurred, as expected. The reactor vessel | | water level then increased to +48 inches, the Reactor Feedwater Pump trip | | level. At 2215 CDT, the Reactor Water Cleanup (RWCU) System was placed in | | service to assist in reactor vessel water level control. The reactor vessel | | water level decreased again and subsequently, at 2229 CDT, reached +8 | | inches. The RWCU System isolated and all PCIS Group II actuations occurred. | | | | | | Unit 2 remains stable in Condition 3 (Hot Shutdown) with reactor vessel | | water level within its normal band. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R3DO Pat Hiland. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37019 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/23/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 02:52[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 23:38[EDT]| | NRC NOTIFIED BY: NICK CONICELLA |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 4 Startup |4 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HIGH PRESSURE COOLANT INJECTION SYSTEM AUTO ISOLATED WHILE BRINGING IT ON | | LINE - | | | | At 2338 on 05/22/00, the High Pressure Coolant Injection (HPCI) System | | isolated due to a spurious high steam flow isolation signal. A valid high | | steam line flow condition would normally be indicative of a piping break; | | however, a piping break did not occur. Although the signal was not valid, | | this is nonetheless considered an Engineered Safety Features (ESF) Actuation | | since a containment isolation had occurred. | | | | The Hope Creek reactor was in Operational Condition 2 (Startup) with Reactor | | Coolant System (RCS) pressure at 200 psig and power at about 4%. The HPCI | | System steam line warmup, which is required to place the HPCI System in a | | standby alignment, had just commenced. When shutdown, the HPCI steam line | | is isolated from the reactor by three containment isolation valves. These | | valves are an outboard valve, an inboard valve, and a bypass valve around | | the inboard valve for steam line warm-up purposes. As part of the steam | | line warmup procedure, the outboard valve is fully opened and the inboard | | bypass valve is throttled to slowly heat up and pressurize the steam line. | | Once the steam line is pressurized, the inboard valve is opened. | | | | During the initial phases of the steam line warmup process, a high steam | | line flow signal was generated when the bypass valve was throttled open. | | This occurred due to steam pressure and flow perturbations within the steam | | line. As a result, an isolation signal was generated and the bypass valve | | automatically closed as expected for this isolation signal. Prior to | | resetting the isolation signal, the HPCI steam line was verified to be | | operable. The HPCI System warmup was then recommenced and the HPCI System | | is currently in its standby alignment. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37020 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 05/23/2000| | UNIT: [] [2] [3] STATE: CA |NOTIFICATION TIME: 06:10[EDT]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 05/23/2000| +------------------------------------------------+EVENT TIME: 02:00[PDT]| | NRC NOTIFIED BY: JACK FITCH |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLAUDE JOHNSON R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PHYSICAL SECURITY REPORT - | | | | UNSECURED/UNATTENDED SECURITY GUARD WEAPON AND AMMUNITION INSIDE PLANT | | PROTECTED AREA FOR ABOUT 25 MINUTES. COMPENSATORY MEASURES WERE IMMEDIATELY | | TAKEN UPON DISCOVERY. THE LICENSEE PLANS TO NOTIFY THE NRC RESIDENT | | INSPECTOR. CONTACT THE NRC OPERATIONS OFFICER FOR ADDITIONAL DETAILS. | | | | * * * UPDATE ON 5/23/00 @ 1342 BY PLUMLEE TO GOULD * * * RETRACTION | | | | LICENSEE IS RETRACTING THIS EVENT SINCE NO WEAPON WAS LOST. | | | | THE NRC RESIDENT INSPECTOR WILL BE INFORMED. THE REG 4 RDO (JOHNSON) WAS | | NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37021 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/23/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 08:44[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/23/2000| +------------------------------------------------+EVENT TIME: 05:05[EDT]| | NRC NOTIFIED BY: ART BREADY |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 4 Startup |4 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HIGH PRESSURE COOLANT INJECTION SYSTEM INOPERABLE DUE TO STUCK OPEN CHECK | | VALVE - | | | | At 0505 on 05/23/00, the High Pressure Coolant Injection (HPCI) System was | | determined to be inoperable as a result of the discharge check valve being | | stuck partially open. This condition was discovered during investigation of | | a low injection header pressure alarm, and subsequent attempts to fill and | | vent the discharge header were unsuccessful. It is believed that the check | | valve stuck partially open when the system was secured after a low pressure | | surveillance test at about 0305. The discharge check valve was mechanically | | agitated at 0700, and reseated as evidenced by an audible sound and rise in | | injection header pressure. | | | | At the time of discovery, the plant was in Operational Condition 2 with | | reactor power at 4% and reactor pressure at approximately 500 psig. All | | other safety related equipment was operable at the tune of discovery, with | | the exception of the 'A' Residual Heat Removal Pump, which was aligned for | | suppression pool cooling mode of operation. There was no significant impact | | to overall plant safety as a result of this condition. | | | | Plant maintenance and engineering personnel are currently evaluating the | | failure of the HPCI System discharge check valve. lnjection header fill and | | vent is in progress to determine the amount of air that is present and | | restore the system to an available condition. This information will be used | | to determine if the safety function of the HPCI System was unavailable as a | | result of the discharge check valve malfunction. | | | | A root cause investigation team has been assembled, and evaluation of system | | and personnel performance is in progress. | | | | The licensee notified the NRC Resident Inspector and plans to notify local | | officials. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37022 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 05/23/2000| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 11:07[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/23/2000| +------------------------------------------------+EVENT TIME: 09:40[CDT]| | NRC NOTIFIED BY: CHRIS ALEXANDER |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLAUDE JOHNSON R4 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A LOOSE CONNECTION WHICH CAUSED INOPERABLE PROCESS COMPUTER | | SYSTEM (PCS) SITE DATA SYSTEM (SDS) COMMUNICATION IN THE EMERGENCY | | OPERATIONS FACILITY (EOF) | | | | The following test is a portion of a facsimile received from the licensee: | | | | "During troubleshooting of an unrelated LAN problem, Telecommunications | | [personnel] apparently bumped a cable causing the connection to become | | loose. This loose connection caused the communication to TT10 and TT11 PCS | | SDS in the EOF to become inoperable. The SDSs were inoperable from 05/22/00 | | [at] 1523 [CST] to 05/23/00 [at] 0739 [CST] for a total of 16 [hours and] 16 | | [minutes]." | | | | The licensee stated that the control room was notified of this condition at | | 0940 CST on 05/23/00. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37023 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: LAKEHEAD PIPELINE |NOTIFICATION DATE: 05/23/2000| |LICENSEE: LAKEHEAD PIPELINE |NOTIFICATION TIME: 11:23[EDT]| | CITY: SUPERIOR REGION: 3 |EVENT DATE: 09/30/1997| | COUNTY: DOUGLAS STATE: WI |EVENT TIME: [CDT]| |LICENSE#: 22-26732-01 AGREEMENT: N |LAST UPDATE DATE: 05/23/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PATRICK HILAND R3 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT POLLOCK | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |IBBF 30.50(b)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HISTORICAL EVENT REGARDING THE LOSS OF SHUTTER POSITION INDICATION ON A | | BERTHOLD DENSITY GAUGE | | | | A nuclear gauge shutter failed during a routine semi-annual shutter test on | | 09/30/97. The manufacturer of the nuclear gauge (Berthold Instruments) was | | notified immediately, and a repair date of 10/07/97 was established. The | | shield mechanism was replaced on 10/07/97. | | | | It was assumed that the shutter was in a partially closed position, but | | there was no way to tell for sure. The gauge has a shaft control rod that | | runs from the shutter to the turn knob. Apparently, the shaft control rod | | broke, and the licensee could no longer determine the position of the | | shutter. | | | | The licensee stated that survey meter readings near the gauge are normally | | quite low when the shuttle is fully open. The licensee also stated that | | this failure held no danger to employees or the public because normal | | operation of the gauge is with the shutter fully open at all times. | | | | The nuclear gauge is located on a pipeline, and it is used for density | | determination of the fluid flowing through the pipe. It has a 1,000-mCi of | | cesium-137 source located on one side of the pipe and a detector located on | | the other side of the pipe. | | | | The licensee stated that this issue was determined to be reportable during a | | recent NRC inspection/audit. The licensee notified the NRC Region 3 office | | (Mike Lafranzo). (Call the NRC operations officer for a site contact | | telephone number.) | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021