Event Notification Report for April 24, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/21/2000 - 04/24/2000 ** EVENT NUMBERS ** 36840 36912 36913 36914 36915 36916 36917 36918 36919 36920 36921 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36840 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 03/28/2000| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 15:21[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 03/28/2000| +------------------------------------------------+EVENT TIME: 12:41[EST]| | NRC NOTIFIED BY: MATTHEW ARSENAULT |LAST UPDATE DATE: 04/21/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHELE EVANS R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PRIMARY COMPONENT COOLING WATER SYSTEM INOPERABLE DUE TO THE AREA | | VENTILATION SYSTEM INCAPABLE OF PERFORMING ITS SAFETY FUNCTION | | | | "On 03/26/00 Seabrook Station entered Tech Spec (TS) 3.0.3 due to both | | trains of the Primary Component Cooling Water (PCCW) system being declared | | inoperable. Both trains of PCCW were declared inoperable because the PCCW | | Area Ventilation System was determined to be incapable of performing its | | intended function. | | | | "The PCCW system is a two train closed loop cooling system used to remove | | heat from plant components during plant operation, plant cooldown and during | | various phases of an accident. The PCCW pumps are located within the Primary | | Auxiliary Building (PAB). The operation of the PCCW pumps is supported by | | the PCCW Area Ventilation system. This ventilation system has redundant, | | automatically controlled auxiliary supply fans and associated dampers to | | ensure that the temperature in this area does not exceed design limits | | should the normal PAB ventilation system fail. | | | | "During surveillance testing of the PCCW Area Ventilation system, an exhaust | | damper (PAH-DP-357) failed to open as required. During a subsequent local | | investigation by the Shift Manager and Unit Supervisor it was determined | | that recent painting activities may have affected both PAB Exhaust Dampers | | (PAH-DP-357 and PAH-DP-358). A subsequent test of PAH-DP-358 indicated that | | it also failed to open as required. TS 3.0.3 was entered on 03/26/00 at | | 0346. TS 3.0.3 was subsequently exited at 0425 on 03/26/00 after plant | | personnel reestablished operability for PAH-DP-358. The subject dampers | | automatically open to provide an exhaust flow path for the PCCW Pump Area | | ventilation system which supports operation of the PCCW pumps. An initial | | review of this condition concluded that a report pursuant to the | | requirements of 10CFR50.72 was not required. A subsequent review of this | | event determined that it is reportable pursuant to the requirements of | | 10CFR50.72(b)(2)(iii) as a condition that alone could have prevented the | | fulfillment of a safety function." | | | | The licensee will inform the NRC resident inspector. | | | | HOO Note: The event time was the time the licensee determined this | | condition to be reportable to the NRC. | | | | * * * RETRACTION ON 04/21/00 AT 1330 HOURS BY M. KILEY TAKEN BY MACKINNON * | | * * | | | | Upon further Engineering review, North Atlantic has determined that the PCCW | | system remained capable of performing its intended function during the | | period when the PAB Exhaust Dampers (PAH-DP-357 and PAH-DP-358) were painted | | between March 12, 2000 and March 26, 2000 when the condition was corrected. | | North Atlantic analyzed the area heat-up conditions as they pertain to the | | operation of the PCCW system and other associated safety-related equipment | | and concluded that the PCCW system would have performed its intended | | function even with the subject dampers isolated. Therefore, this condition | | is not reportable pursuant to the requirement of 10 CFR 50.72(b)(2)(iii) as | | a condition that alone could have prevented the fulfillment of a safety | | function. R1DO (John White) notified. | | | | The NRC Resident Inspector has been notified of this retraction by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36912 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ABI LABORATORY, INC. |NOTIFICATION DATE: 04/21/2000| |LICENSEE: ABI LABORATORY, INC. |NOTIFICATION TIME: 09:14[EDT]| | CITY: SPRINGFIELD REGION: 1 |EVENT DATE: 04/20/2000| | COUNTY: STATE: PA |EVENT TIME: 14:00[EDT]| |LICENSE#: 37-30215-01 AGREEMENT: N |LAST UPDATE DATE: 04/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN WHITE R1 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KIMBERLY MOORE | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAD1 20.2202(a)(1) PERS OVEREXPOSURE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE OVEREXPOSURE | | | | On 04/20/00 the Radiation Safety Officer for ABI Laboratory, Inc., received | | a phone call from Troxler informing her that one of the film badges that | | they had read had a reading of 30,677 mrem (30.7 Rads). Troxler will check | | the film badge again on Monday, 04/24/00, since Friday is a holiday. The | | film badge belongs to an ABI Laboratory, Inc., employee who is currently | | working at a construction site located at the Philadelphia International | | Airport . The film badges for ABI Laboratory, Inc., are checked quarterly | | by Troxler. The film badge mentioned above had been used during the | | December 1999 through February 2000 time period. | | | | The ABI Laboratory, Inc. construction site has 2 Troxler and 2 Humboldt | | Density Gauges. The Density Gauges were all leak tested and radiation | | surveys were taken inside and around the building containing the gauges. All | | radiation surveys and leak tests were within expected values. | | | | From December 1999 through February 2000, the employee in question used a | | Density Gauge on 20 different days. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36913 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SC DIV OF HEALTH & ENV CONTROL |NOTIFICATION DATE: 04/21/2000| |LICENSEE: BANKS CONSTRUCTION COMPANY |NOTIFICATION TIME: 13:59[EDT]| | CITY: CHARLESTON REGION: 2 |EVENT DATE: 04/21/2000| | COUNTY: STATE: SC |EVENT TIME: 02:00[EDT]| |LICENSE#: SC-518 AGREEMENT: Y |LAST UPDATE DATE: 04/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANN BOLAND R2 | | |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM PETERSON | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |NDAM DAMAGED GAUGE/DEVICE | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT: DAMAGED TROXLER MOISTURE DENSITY GAUGE - | | | | At 0200 on 04/20/00, an automobile struck a Banks Construction Company | | (License #SC-518) truck on I-26 in Charleston, SC, damaging a Troxler | | Moisture Density Gauge, model #4640. The 9 mCi Cs-137 and 44 mCi Am-241-Be | | sources were undamaged. The damaged gauge, containing its undamaged | | sources, was placed into its transport case and will be sent to Troxler for | | repairs. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36914 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MARYLAND DEPT OF THE ENVIRONMENT |NOTIFICATION DATE: 04/21/2000| |LICENSEE: U OF MD AT BALTIMORE HOSPITAL |NOTIFICATION TIME: 15:04[EDT]| | CITY: BALTIMORE REGION: 1 |EVENT DATE: 04/20/2000| | COUNTY: STATE: MD |EVENT TIME: 13:00[EDT]| |LICENSE#: MD-07-014-05 AGREEMENT: Y |LAST UPDATE DATE: 04/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN WHITE R1 | | |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RAY MANLEY | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT: MEDICAL MISADMINISTRATION - | | | | At 1300 on 04/20/00, a 52 year old female patient received a medical | | misadministration of a gamma knife treatment at the University of Maryland | | at Baltimore (UMAB) Hospital to reduce the cancerous tumor in her head. | | | | The gamma knife is a UMAB specific license that uses 201 sealed Cobalt-60 | | sources of 30 curies each in a Model 23016 Leksell Gamma System for the | | radiation treatment of human patients. | | | | The patient received 12.6 gray to an unintended site of approximately 0.18 | | cubic centimeters. The unintended site was approximately 4.2 centimeters | | from the intended site. | | | | The medical directive for this treatment was defined as approximately 18 | | gray administered over six administrations. The misadministration occurred | | during the first administration only. The treatment planning for the patient | | was uneventful and was prepared and reviewed by a hospital gamma knife team | | of a Radiation Oncologist, a Neurosurgeon and a Medical Physicist. It | | appears from preliminary interviews that when two of the team members were | | adjusting the coordinates on the device's steriotactic frame, the Y and Z | | coordinates were reversed. This frame adjustment is accomplished by | | loosening the frame via the use of allen screws and manually adjusting it. | | One person calls out the coordinate and the other conducts the adjustment. | | According to the licensee procedures, this adjustment is to be checked for | | accuracy by a nurse and the Medical Physicist. Normally the coordinates are | | read out in a specific order. The licensee indicated that the order might | | have been reversed due to a specific frame orientation problem that occurs | | approximately once in every 20 treatments. When the licensee started to set | | up for the second administration, the error was noted. The treatment plan | | was reevaluated to include some partial dose to the tumor from the first | | administration and the treatment was completed in seven administrations | | instead of six. | | | | The patient and her referring physician have been notified of this | | misadministration. This misadministration constitutes no negative medical | | impact on the patient. | | | | A MD DOE representative requested that UMAB Hospital personnel review | | previous medical files to assure that this switching of coordinates has not | | happened before without a misadministration being identified. | | | | The gamma knife is not scheduled to be used again at UMAB Hospital until | | 04/25/00. On 04/24/00, a hospital management meeting has been scheduled | | among personnel from Hospital Administration, Oncology, Neurosurgery and the | | Radiation Safety Office to discuss this incident. The RSO's position at | | this meeting will be that all use of the gamma knife be suspended until the | | incident has been fully investigated and assurances are in place to prevent | | recurrence. | | | | A written report of this incident will be submitted to NMED within 30 days. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36915 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 04/21/2000| | UNIT: [1] [] [] STATE: AZ |NOTIFICATION TIME: 16:46[EDT]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 04/21/2000| +------------------------------------------------+EVENT TIME: 11:10[MST]| | NRC NOTIFIED BY: DAN MARKS |LAST UPDATE DATE: 04/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DALE POWERS R4 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS-FOR-DUTY REPORT - | | | | A licensed employee was for-cause tested for the presence of alcohol and was | | determined not to be unfit for duty. The employee's access authorization to | | the plant protected area which had been suspended, was restored. | | | | The licensee notified the NRC Resident Inspector. | | | | | | | | | | On April 21, 2000 at approximately 11:10 MST, the Unit I Shift Manager, a | | licensed senior reactor operator, opened his lunch box and discovered that | | it contained an unopened can of beer. By approximately 11:15 MST, the shift | | manager completed notifications to station management and security, and | | isolated the alcoholic beverage. | | | | Although behavior observation by supervision detected no degradation in | | performance, impairment, or changes in employee performance, the shift | | manager's access to the protected area was suspended and he was escorted to | | the Palo Verde health clinic for fitness-for-duty testing. Testing | | for-cause, conducted in accordance with 10CFR26.24(a)(3), was negative, | | demonstrating that the Shift Manager was not unfit for duty due to the | | consumption of alcohol. Upon completion of satisfactory testing, access to | | the protected area was restored. | | | | The unopened can of beer has been removed from the protected area. | | | | The Shift Manager stated that the can of beer, instead of a can of soda, had | | been placed in the lunch box inadvertently by himself when preparing to come | | to work. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36916 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 04/21/2000| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 18:38[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/21/2000| +------------------------------------------------+EVENT TIME: 13:45[CDT]| | NRC NOTIFIED BY: BOB SCARBOROUGH |LAST UPDATE DATE: 04/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DALE POWERS R4 | |10 CFR SECTION: |OTHER FEDS VIA FAX | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - NOTIFICATION OF FEDERAL, STATE & LOCAL AGENCIES OF A HYDRAZINE CHEMICAL | | SPILL ONSITE - | | | | At 1345 CDT on 04/21/00, Unit 1 experienced a chemical spill of 38 gallons | | of hydrazine that had leaked from a line that leads to an onsite storage | | tank. The licensee isolated the leak, contained the spill onsite and is | | cleaning up the spill. | | | | The licensee notified the NRC Resident Inspector and is in the process of | | notifying the DOT National Response Center, Texas Natural Resources | | Conservation Commission and the Local Emergency Planning Committee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36917 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 04/22/2000| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 11:08[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 04/22/2000| +------------------------------------------------+EVENT TIME: 08:03[CDT]| | NRC NOTIFIED BY: ROY SCOTT |LAST UPDATE DATE: 04/22/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK RING R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Intermediate Shut|0 Intermediate Shut| | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MAIN STEAM ISOLATION VALVE FAILED TIMING TEST | | | | The licensee determined that the 'B' steam generator main steam isolation | | valve shut in 6 seconds during testing. The requirement is 5 seconds in the | | surveillance test of technical specifications and in the Updated Safety | | Analysis Report. The plant will remain shutdown until repairs and testing | | are complete. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36918 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 04/22/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 16:19[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 04/22/2000| +------------------------------------------------+EVENT TIME: 15:06[EDT]| | NRC NOTIFIED BY: STEVE FREGEAU |LAST UPDATE DATE: 04/22/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN WHITE R1 | |10 CFR SECTION: | | |AMED 50.72(b)(2)(v) OFFSITE MEDICAL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 54 Power Operation |54 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - POTENTIALLY CONTAMINATED PLANT EMPLOYEE TRANSPORTED TO OFFSITE HOSPITAL - | | | | | | A potentially contaminated plant employee who sustained a broken leg onsite, | | was transported offsite to Oswego hospital for treatment accompanied by a | | plant radiation technician. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | * * * UPDATE AT 1712 ON 04/22/00 BY STEVE FREGEAU TO JOLLIFFE * * * | | | | The plant radiation technician determined that the plant employee was not | | contaminated. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO John White. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36919 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 04/22/2000| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 17:05[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 04/22/2000| +------------------------------------------------+EVENT TIME: 14:28[EDT]| | NRC NOTIFIED BY: SANJEEV ARAB |LAST UPDATE DATE: 04/22/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK RING R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - SHUTDOWN COOLING LOST FOR 48 MINUTES; NO REACTOR VESSEL TEMPERATURE RISE | | - | | | | On 04/22/00, Unit 2 was in Condition 5 in a Refueling Outage with the | | reactor vessel cavity flooded up to higher than 20 feet 6 inches above the | | reactor vessel flange with the fuel pool gates removed. | | | | At 1428, shutdown cooling was lost due to a technician inadvertently pulling | | a wrong electrical fuse causing the Residual Heat Removal (RHR) shutdown | | inboard suction isolation valve #E1150-F009 to auto close. The closure of | | this valve was in response to an invalid reactor vessel water level three | | signal causing the 'A' RHR pump to trip due to loss of suction flow. | | | | At 1516, shutdown cooling was restored. No temperature rise in the reactor | | vessel was noted during the time that shutdown cooling was out of service. | | | | The licensee plans to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36920 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DAVIS BESSE REGION: 3 |NOTIFICATION DATE: 04/23/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 00:38[EDT]| | RXTYPE: [1] B&W-R-LP |EVENT DATE: 04/23/2000| +------------------------------------------------+EVENT TIME: 00:10[EDT]| | NRC NOTIFIED BY: STEVE ROBERTS |LAST UPDATE DATE: 04/23/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |M. DAPAS R3 | |10 CFR SECTION: |DAVID MATTHEWS NRR | |AAEC 50.72 (a) (1) (I) EMERGENCY DECLARED |JOSEPH GIITTER IRO | | |CEGIELSKI FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER | | | | During preparation for a bus transfer test, the wrong relay was energized | | which caused the loss of offsite power to the 'A' and 'B' 13.8 Kv busses. | | An Unusual Event was declared with the loss of offsite power. Only one of | | the offsite sources was energized at the time and the relay tripped during | | test setup causing the loss of that source. The 4160 volt essential busses | | were reenergized by their respective emergency diesel generators. The plant | | was defueled at the time and spent fuel pool cooling was restarted. | | | | There was no release of radioactivity and no recommended protective actions | | necessary. | | | | The licensee is conducting a review of the event and all testing activities | | are suspended until completed. | | | | The Unusual Event was terminated at 0054 EDT with the restoration of normal | | power configuration. | | | | The licensee notified the State of Ohio and the local counties, Ottawa and | | Lucas, as well as the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36921 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 04/23/2000| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 06:49[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/23/2000| +------------------------------------------------+EVENT TIME: 03:35[EDT]| | NRC NOTIFIED BY: BRIAN MOTZ |LAST UPDATE DATE: 04/23/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK RING R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 TRAIN 'B' ESSENTIAL SERVICE WATER PUMP STARTED AUTOMATICALLY | | | | While setting up for testing the Solid State Protection System (SSPS) on | | Unit 2, the clearance permit did not anticipate the start of the Unit 1 | | train 'B' Essential Service Water (ESW) Pump. | | | | "To perform maintenance on the SSPS, a clearance to deenergize the SSPS | | cabinets in Unit 2 was written. The Unit 2 SSPS was in inhibit at this | | time. During the deenergization per this clearance, an automatic start of | | the Unit 1 East ESW Pump occurred. The ESW Pump autostart was not | | anticipated or described in the clearance. | | | | "A Safety Injection (SI) signal through SSPS in either Unit 1 or Unit 2 will | | cause the ESW Pumps in both units to autostart for the train effected. | | Similarly, the removal of power from the control room instrumentation | | distribution circuit, which is what occurred here, will cause the autostart | | of the ESW pumps. | | | | "There were no adverse consequences as a result of the auto pump start and | | the actuation was per the system design. No SI signal was generated." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021