Event Notification Report for April 20, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/19/2000 - 04/20/2000 ** EVENT NUMBERS ** 36852 36891 36904 36905 36906 36907 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36852 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FT CALHOUN REGION: 4 |NOTIFICATION DATE: 04/01/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 11:02[EST]| | RXTYPE: [1] CE |EVENT DATE: 04/01/2000| +------------------------------------------------+EVENT TIME: 09:20[CST]| | NRC NOTIFIED BY: LARRY LEES |LAST UPDATE DATE: 04/19/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KRISS KENNEDY R4 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECH SPEC REQUIRED SHUTDOWN DUE TO EMERGENCY FEEDWATER STORAGE TANK LEVEL | | DECREASING BELOW TECH SPEC LIMIT | | | | THE PLANT ENTERED ABNORMAL OPERATING PROCEDURE (AOP) 30, "EMERGENCY FILL OF | | EMERGENCY FEEDWATER STORAGE TANK," AS A RESULT OF THE EMERGENCY FEEDWATER | | STORAGE TANK LEVEL FALLING BELOW TECH SPEC LOW LIMIT OF 91%. THIS RESULTED | | IN ENTRY INTO TECH SPEC 2.0.1 WHICH DIRECTS PLACING THE PLANT IN HOT | | SHUTDOWN WITHIN 6 HOURS, LESS THAN 300 DEGREES F IN ANOTHER 6 HOURS AND IN | | COLD SHUTDOWN IN 30 HOURS. AT THE TIME OF ENTRY INTO THIS TECH SPEC THE | | PLANT WAS ALREADY IN HOT SHUTDOWN. ACTIONS TO REFILL THE EMERGENCY | | FEEDWATER STORAGE TANK WERE TAKEN BY OPENING THE CONDENSATE FILL LINE AND | | EMERGENCY FILLING. FILLING WAS IN PROGRESS BEFORE GOING BELOW 91%, HOWEVER, | | SYSTEM DEMAND WAS GREATER THAN THE MAKEUP ABILITY OF THE DEMINERALIZED WATER | | SOURCE (STEAM GENERATOR WATER SUPPLY SWAPOVER). LEVEL WAS ABOVE 91% AT | | 0944CST AT WHICH TIME AOP 30 AND TECH SPEC 2.0.1 WERE EXITED. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1007 ON 4/19/00 BY MATZKE RECEIVED BY WEAVER * * * EVENT | | RETRACTION | | | | On April 1, 2000, at 1102 EDT, Fort Calhoun Station made a 1-hour | | notification of entry into a shutdown-required Technical Specification | | Limiting Condition for Operation (LCO) to the NRC Operations Center under | | 10CFR50.72(b)(1)(i)(A). At the time the plant had completed a normal | | shutdown to hot standby per plant procedures. While maintaining the plant | | in Hot Standby (Mode 3), the indicated level in the Emergency Feedwater | | Storage Tank (EFWST), FW-19, appeared to fall below the Technical | | Specification (TS) minimum level of 55,000 gallons. Operators conservatively | | entered TS 2.0.1 (equivalent to standard TS 3.0.3). This LCO would have | | required the plant to be placed in Cold Shutdown (Mode 4). The tank level | | was quickly recovered and the TS exited. Subsequent investigation determined | | that the TS for EFWST level had not been violated and TS 2.0.1 not entered. | | Therefore, the notification of April 1, is being withdrawn. | | | | The Resident Inspector was notified. Reg 4 RDO(Powers) was notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36891 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 04/14/2000| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 19:58[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/14/2000| +------------------------------------------------+EVENT TIME: 17:41[CDT]| | NRC NOTIFIED BY: TIM WITSCHEN |LAST UPDATE DATE: 04/19/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BURNT SMELL FROM HIGH PRESSURE COOLANT INJECTION (HPCI) STEAM SUPPLY VALVE | | BREAKER. HPCI DECLARED INOPERABLE AND 14 DAY LIMITING CONDITION OF | | OPERATION ENTERED PER TECHNICAL SPECIFICATION. | | | | An undervoltage alarm was received in control room from HPCI Direct Current | | Motor Control Center (DCMCC) D312 which is located in the HPCI room. An | | operator was immediately dispatched to investigate the undervoltage | | condition on D312. The operator discovered that HPCI Steam Supply Valve, ( | | MOV-2036), breaker, (D31206), had a burnt smell. The breaker was opened and | | HPCI Steam Supply Inboard Isolation Valve was closed. HPCI was declared | | inoperable and a 14 day Limiting Condition of Operation was entered per | | their Technical Specification. Emergency Core Cooling Systems and Reactor | | Core Isolation Cooling are fully operable if needed. Their was no fire and | | the licensee is investigating. | | | | The NRC Resident Inspector will be notified of this event by the licensee. | | | | * * * RETRACTION 1717 4/19/2000 FROM BISTODEAU TAKEN BY STRANSKY * * * | | | | "This notification retracts a notification made 4/14/00 for HPCI being | | declared inoperable due to a suspected electrical problem in a DC motor | | control center (MCC). An undervoltage alarm was received, and a burnt smell | | near the MCC was observed. The HPCI system was isolated per procedure. | | Investigation revealed a low voltage monitoring coil had failed The coil was | | replaced and successfully tested. The system was returned to its normal | | standby condition. | | | | "This coil performs a monitoring function only. Failure of the coil, or any | | effects of the failure would not have prevented the MCC or HPCI system from | | performing their required safety function. The HPCI system was fully | | operable until removed from service to investigate the condition and replace | | the coil." | | | | The NRC resident inspector has been informed of this retraction. Notified | | R3DO (Ring). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36904 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: HONEYWELL SENSOR AND GUIDANCE PRODS |NOTIFICATION DATE: 04/19/2000| |LICENSEE: HONEYWELL SENSOR AND GUIDANCE PRODS |NOTIFICATION TIME: 16:09[EDT]| | CITY: MINNEAPOLIS REGION: 3 |EVENT DATE: 03/23/2000| | COUNTY: STATE: MN |EVENT TIME: [CDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 04/19/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MARK RING R3 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: TOM OSTRATEG | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING AIR IONIZER | | | | A generally licensed NRD model P-2021-3000 air ionizer (s/n 115737) was | | discovered missing from a clean room at the Honeywell SGP facility in | | Minneapolis. The device had an initial activity of 10 mCi of Po-210, but the | | caller did not know the current activity. The device was declared lost on | | 3/23/00 after repeated searches of the facility and interviews of employees | | did not lead to its recovery. Honeywell has contacted the vendor regarding | | this matter. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36905 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 04/19/2000| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 17:55[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 04/19/2000| +------------------------------------------------+EVENT TIME: 14:33[EDT]| | NRC NOTIFIED BY: RUSSELL LONG |LAST UPDATE DATE: 04/19/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN WHITE R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INADVERTENT AFW ACTUATION FOLLOWING TESTING | | | | "At about 1433 hours on 19 April 2000, there was an inadvertent actuation of | | 32 Auxiliary Boiler Feedwater Pump (ABFP). The actuation occurred following | | the completion of the required monthly test of 32 Emergency Diesel Generator | | (EDG), when the diesel output breaker was opened. Normally the 'Non-SI | | Blackout Logic' circuitry prevents automatic starting of equipment until | | manually reset. For some reason, currently under investigation, this | | circuitry automatically reset when the EDG output breaker was opened. The | | cause of the automatic reset of the Non-SI Blackout Logic, and the automatic | | start of 32 ABFP is under investigation. 32 EDG was inoperable prior to this | | event for planned testing, and remains inoperable while the investigation | | continues. 32 EDG is currently available and aligned for automatic start. | | There were no plant conditions requiring operation of 32 ABFP and the | | automatic start sent no water to any steam generator (since this requires | | additional manual action). Immediate corrective action taken was to secure | | 32 ABFP." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36906 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/19/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 19:50[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 04/19/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:55[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/19/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MARK RING R3 | | DOCKET: 0707002 |PATRICIA HOLAHAN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETHE | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01 4 HOUR REPORT | | | | "At 1555 hrs April 19, 2000, laboratory personnel were preparing samples | | when they discovered that 8 uranium bearing samples (16-40 ml vials) were in | | an Environmental Safety & Health (ES&H) Analytical Laboratory without having | | had a gamma scan performed to determine total uranium. NCSA-0710_015.A02 | | administrative control #1, states in part, "Any sample containers that are | | postulated to contain uranium contamination >=100 ppm uranium based on their | | origin shall be gamma scanned for total uranium." Control #1 of the NCSA | | was lost, leading to a possible error in the mass tally for the high | | concentration containers. The total volume of the containers was 640 ml, | | and the concentration of the containers was subsequently determined to be | | 500 ppm U-235. Mass control was lost for the high concentration | | containers. Mass control for low concentration containers and volume | | controls for process waste were maintained. | | | | "At the direction of the Plant Shift Superintendent (PSS) the requirements | | for an NCS anomalous condition were initiated. At 1920 hrs compliance was | | regained by scanning the samples and properly logging them into the | | container mass inventory. | | | | "At the direction of the PSS the X-710 management staff will conduct | | briefings with the respective personnel to prevent re-occurrence." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36907 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 04/19/2000| | UNIT: [1] [2] [] STATE: VA |NOTIFICATION TIME: 21:36[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/19/2000| +------------------------------------------------+EVENT TIME: 18:16[EDT]| | NRC NOTIFIED BY: ALLEN HARROW |LAST UPDATE DATE: 04/19/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FILTERED EXHAUST FANS CANNOT BE OPERATED IN PARALLEL | | | | "Based on Unit 1H and 1J emergency bus logic testing performed on 4/18/00 | | and 4/19/00 in accordance with 1-OPT-ZZ-001 and 1-OPT-ZZ-002, it has been | | concluded that the Cat 1 Filtered Exhaust Fans, 1-VS-F-58A & B, will not | | operate in parallel without tripping one or both fans. As a result, an event | | or condition that alone could have prevented the fulfillment of a safety | | function of structures or systems that are needed to control the release of | | radioactive material, or mitigate the consequences of an accident exists for | | Surry Units 1 and 2. This condition is reportable in accordance with 10 CFR | | 50.72(b)(2)(iii). | | | | "Both fans have been tested by operating the fans individually. This testing | | has determined that operation and performance of each fan is entirely | | satisfactory when operated independently. | | | | "The current system alignment is that one of the two fans is in the | | pull-to-lock position, and the other fan is in automatic stand-by. In this | | configuration, one fan is operable, and fully capable of performing its | | required functions. Unit 2 entered a 7 day Technical Specification 3.22.B | | action statement on 4/18/00 at 1240 hours as a result of this condition. | | | | "The Surry Emergency Operating Procedures provide required directions to | | place a Cat 1 Filtered Exhaust Fan in service, if the fans fail to | | automatically start upon initiation of a Safety Injection. In the current | | configuration, if the operable Cat 1 Filtered Exhaust fan fails to start, | | the fan that is currently in PTL can be immediately placed in service." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021