Event Notification Report for February 24, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/23/2000 - 02/24/2000 ** EVENT NUMBERS ** 36713 36719 36720 36721 36722 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36713 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 02/21/2000| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 16:16[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/21/2000| +------------------------------------------------+EVENT TIME: 08:40[CST]| | NRC NOTIFIED BY: GREG JANAK |LAST UPDATE DATE: 02/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN PELLET R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 94 Power Operation |94 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - 24 hour Report, Violation of Operating License, condition existing longer | | than permitted by Plant Tech Specs - | | | | Carbon samples obtained from Fuel Handling Building Exhaust Filtration Unit | | Train A failed laboratory tests. The Plant Technical Specification | | 4.7.8.a.2 limit of less than 1% methyl iodide penetration was exceeded. The | | as-found methyl iodide penetration results were 1.07%. This resulted in the | | Train A Fuel Handling Exhaust Filtration Unit being inoperable since the | | time that the carbon samples were obtained at 0900 CST on 02/17/00. This | | results in the system being inoperable for longer than 7 days which is a | | violation of Technical Specification 3.7.8. Action a. The sample results | | were obtained at 0840 CST on 02/21/00. | | | | This notification is being made pursuant to Operating License NPF-76, | | Section 2.G for operation or condition prohibited by Plant Technical | | Specifications. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1604 ON 02/23/00 BY GREG JANAK TO JOLLIFFE * * * | | | | Plant Technical Specification Surveillance Requirement 4.7.8 (b) requires | | that periodic samples be taken from charcoal beds and analyzed within 31 | | days after removal. These requirements were met and action to declare that | | train inoperable was taken upon notification of unsatisfactory results. | | Based on previous practice, a 24-hour report for a violation of the | | operating license was made to the NRC as a result of this failure. | | | | While onsite for an inspection of the Effluents Program, an NRC inspector | | questioned the reportability of this event. After further investigation | | into the issue, and input from both Region IV and NRR on this issue, the | | licensee has determined that this event is not reportable to the NRC as long | | as the charcoal in question is replaced within the allowed outage time, as | | specified in the Plant Technical Specifications. Based on the above, the | | licensee retracted this event. | | | | The licensee plans to notify the NRC Resident Inspector. The NRC Operations | | Officer notified the R4DO Charles Marschall. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36719 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/22/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 23:29[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/21/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 23:45[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 02/23/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JAMES CREED R3 | | DOCKET: 0707002 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH DISCHARGE ALARM FOR THE W-2 COMPRESSOR. LEAK TESTING OF THE W-2 | | COMPRESSOR INDICATE A SEAL FAILURE WITH POTENTIAL FOR URANIUM HEXAFLUORIDE | | OUT GASSING. | | | | At approximately 2347 hours, 02/21/00, operations personnel received a | | Cascade Automatic Data Processing (CADP) smoke head alarm for Extended Range | | Product (ERP) W-2 withdrawal station compressor. Operations personnel had | | responded to a High Discharge Alarm for the W-2 compressor and upon arrival | | discovered the compressor shutdown and the CADP smoke head in alarm. No | | smoke was discovered during the investigation of the alarm, however the | | smoke head is located inside a heated housing not readily accessible to | | operations personnel. Leak testing of the W-2 compressor indicated a seal | | failure with potential for uranium hexafluoride outgassing. | | | | Operations and engineering personnel are continuing to investigate the cause | | of the smoke head alarm, but have not provided evidence at this time to | | invalidate the alarm. PORTS is reporting this alarm as a valid actuation to | | a "Q" Safety System. | | | | There was no loss of hazardous/radioactive material or | | radioactive/radiological contamination exposure as a result of this event. | | | | The NRC Resident Inspector was notified of this event by the certificate | | holder. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36720 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 02/23/2000| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 18:00[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 02/23/2000| +------------------------------------------------+EVENT TIME: 14:00[CST]| | NRC NOTIFIED BY: ELLIS PFEFFER |LAST UPDATE DATE: 02/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: |WILLIAM BECKNER NRR | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Discovery of unfiltered leak path from Secondary Containment to outside | | atmosphere via the SBGT System - | | | | During Standby Gas Treatment (SBGT) System testing, the pressure in the room | | containing the SBGT System was found to be at a lower pressure than | | Secondary Containment (SC). The SBGT System draws a negative pressure on | | the SC during accident scenarios. The SBGT System room is located outside | | SC. With the SBGT System room being at a lower pressure than SC, a possible | | leakage path is created from SC into the SBGT System room, into the SBGT | | System (downstream of the filters) and out the plant stack. This path | | bypasses the SBGT System filtering assumed in the offsite dose analysis. | | This leakage path is small, but is not currently assumed in the accident | | analysis. | | | | The licensee is determining corrective actions and plans to resolve this | | issue prior to restarting the plant. | | | | The licensee notified state and local officials and the NRC Resident | | Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36721 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/23/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 19:11[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/23/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 08:35[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 02/23/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JAMES CREED R3 | | DOCKET: 0707002 |WILLIAM BRACH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RICK LARSON | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Emergency response procedures implemented due to a smoke head alarm and | | high pressure vent actuation - | | | | At approximately 0835 on 02/23/00, Portsmouth operations personnel received | | a smoke head alarm for extended range product (ERP) compressor W-3 in Area | | Control Room (ACR)-4. At the same time, another operator in ACR-4 looked at | | the TV monitor for the ERP compressors and saw a "puff" of smoke around | | compressor W-3. The plant's "SEE & FLEE" emergency procedures were | | immediately implemented. The ERP stations' high pressure vent actuated | | taking the station below atmospheric pressure. Results of all surveys | | performed during the emergency response were less than minimum detectable | | activity. At 0949, the emergency response was cancelled. The ERP station | | was made inoperable to allow for testing of the system by operations and | | engineering personnel. Portsmouth is reporting this alarm as a valid | | actuation of a "Q" Safety System. | | | | This event is reportable to the NRC as a valid actuation of a "Q" Safety | | System in accordance with Safety Analysis Report, Section 6.9 (24-HOUR | | REPORT). | | | | There was no loss of hazardous or radioactive material nor radioactive or | | radiological contamination exposure as result of this event. | | | | The NRC Resident Inspector and DOE site representative were notified of this | | event. | | | | PTS-2000-020 PR-PTS-00-01079 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36722 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 02/24/2000| | UNIT: [3] [4] [] STATE: FL |NOTIFICATION TIME: 02:48[EST]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 02/24/2000| +------------------------------------------------+EVENT TIME: 02:10[EST]| | NRC NOTIFIED BY: NEWTON |LAST UPDATE DATE: 02/24/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES OGLE R2 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | |4 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY RESPONSE DATA ACQUISITION AND DISPLAY SYSTEM (ERDADS) INOPERABLE | | GREATER THAN 30 MINUTES. | | | | | | ERDADS LOCKED UP FOR GREATER THAN 30 MINUTES. PERSONNEL HAVE BEEN CALLED OUT | | TO REPAIR ERDADS. ALL OTHER SYSTEMS OPERATING PROPERLY. | | | | THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED OF THIS EVENT BY THE LICENSEE. | | | | * * * UPDATE ON 02/24/00 AT 0515 ET BY MR. MORRIS TAKEN BY MACKINNON * * * | | | | ERDADS RETURNED TO SERVICE AT 0400 ET. | | R2DO (CHARLES OGLE) NOTIFIED. | | | | THE NRC RESIDENT INSPECOTR WILL BE NOTIFIED BY THE LICENSEE OF THIS EVENT | | UPDATE. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021