Event Notification Report for December 17, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/16/1999 - 12/17/1999 ** EVENT NUMBERS ** 36515 36516 36517 36518 36519 36520 36521 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36515 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 12/16/1999| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 01:01[EST]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 12/15/1999| +------------------------------------------------+EVENT TIME: 23:25[EST]| | NRC NOTIFIED BY: WILSON |LAST UPDATE DATE: 12/16/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING A BUNKER-C OIL SPILL AT THE FOSSIL UNITS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Units 1 and 2 (fossil) are notifying [the Department of Environmental | | Resource Management (DERM)] of [a] Bunker-C oil spill on [a] permeable | | surface. [It is] estimated that 100 - 150 gallons of bunker C [are] | | contained by an earth/rock berm around the fuel tank." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36516 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 12/16/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 14:19[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 12/16/1999| +------------------------------------------------+EVENT TIME: 13:45[EST]| | NRC NOTIFIED BY: GEORGE E. STOROLIS |LAST UPDATE DATE: 12/16/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BILL RULAND R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 SERVICE WATER PUMP 'C' MAY NOT HAVE BEEN CAPABLE OF PERFORMING DESIGN | | FUNCTION DURING A 7-DAY OUTAGE OF SERVICE WATER PUMP 'B.' | | | | "Routine operations plant surveillance revealed, at approximately 0056 hours | | on 11/21/99, that the discharge metal expansion joint of Beaver Valley Power | | Station (BVPS) Unit 2 Service Water System (SWS) pump 2SWS*P21C was deformed | | outward. 2SWS*P21C was supplying the SWS 'B' Train, since approximately | | 0425 hours on 11/15/99, while the train normal supply pump, 2SWS*P21B, was | | out of service for replacement of the pump vacuum break check valve. Due to | | the unknown condition of the expansion joint, 2SWS*P21C was declared | | inoperable, and [the] required action of Technical Specifications (TS) | | 3.7.4.1 was entered. At approximately 0154 hours (same day), Standby | | Service Water System (SWE) Pump 2SWE*P21B was placed into service to supply | | [the] 'B' SWS Train, and 2SWS*P21C was removed from service. 2SWS*P21B was | | returned to service to supply [the] 'B' SWS Train, and the required action | | of TS was exited at approximately 0035 hours on 11/22/99. | | | | "Investigation has determined that the subject expansion joint most likely | | deformed, at approximately 1149 hours on 11/09/99 due to water hammer of the | | 'B' SWS Train piping during safeguards protection system slave relay | | testing. Subsequent engineering assessment of the as-found condition of the | | expansion joint is indeterminate whether the capability of the SWS system to | | perform its intended function under all design basis events was | | significantly affected. Therefore, during the time frame that 2SWS*P21C was | | relied upon to maintain operability of the SWS (11/15/99 until 2SWS*P21B was | | placed into service to supply 'B' SWS Train), it cannot be assured that Unit | | 2 would have remained within the plant design basis with an additional | | postulated single failure of redundant SWS Train 'A' that would have | | prevented the train from mitigating a design basis accident. Throughout the | | time 2SWS*P21C was relied upon for SWS Train 'B,' the Unit SWE remained | | fully operable. This notification is applicable to the 1-hour non-emergency | | event reporting criteria of 10 CFR 50.72(b)(ii)(B), for having been 'in a | | condition that is outside the design basis of the plant'." | | | | The water hammer which occurred on 11/09/99 was attributed to a failed | | vacuum break check valve which had corroded closed. The SWS Pump 'C' | | bellows has been replaced, and required maintenance will be completed by | | 12/24/99. The pump will be declared operable following post-maintenance | | testing. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36517 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 12/16/1999| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 16:40[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 12/16/1999| +------------------------------------------------+EVENT TIME: 12:48[EST]| | NRC NOTIFIED BY: KEN CHISM |LAST UPDATE DATE: 12/16/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING SYSTEM DECLARED INOPERABLE ON BOTH UNITS DUE | | TO UNDERSIZED THERMAL OVERLOADS INSTALLED ON THREE (3) VALVES WHICH MAY HAVE | | PREVENTED OPERATION UNDER WORST CASE CONDITIONS. | | | | "On December 16, 1999, at 1248, the Reactor Core Isolation Cooling System | | was declared inoperable because the thermal overloads on three system valves | | were determined to be sized such that the affected valves might not operate | | during worst case conditions. The affected valves are: 1 (2)-E51-V8 | | (Turbine Trip and Throttle Valve), 1(2)-E51-F019 (Minimum Flow Bypass to | | Torus Valve), and 1(2)-E51-F046 (Cooling Water Supply Valve). Analysis also | | determined that 1(2)-E41-F059 (High Pressure Core Injection Cooling System | | Water Supply Valve) also contains inappropriately sized thermal overloads; | | however, the [High Pressure Coolant Injection] System has not been declared | | inoperable because this valve have been repositioned to its accident | | position (open), and administrative measures have been taken to maintain the | | valve in the open position. | | | | "The Reactor Core Isolation Cooling system is a single-train system used to | | prevent overheating of the reactor fuel in the event of a reactor isolation | | accompanied by a loss of feedwater. The high pressure High Pressure Coolant | | Injection system (approximately ten times the flow rate as the Reactor Core | | Isolation Cooling System) remains operable. Plant technical specifications | | allow continued operation for 14 days with the Reactor Core Isolation | | Cooling system inoperable. The Reactor Core Isolation Cooling system is not | | considered an engineered safety feature at the Brunswick Plant although it | | is included in plant technical specifications. For these reasons, the | | safety significance of this event is considered to be low. Engineering | | calculations are currently in progress to confirm the operability of the | | [High Pressure Coolant Injection] System. | | | | "Engineering and maintenance personnel are working to determine a corrective | | action plan at this time." | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36518 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/16/1999| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 19:03[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/16/1999| +------------------------------------------------+EVENT TIME: [EST]| | NRC NOTIFIED BY: ALAN RABENOLD |LAST UPDATE DATE: 12/16/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR REPORT INVOLVING POSSIBLE VIOLATION OF CONDITION OF LICENSEE | | | | "Preliminary investigations indicate that during the preceding operating | | cycle, the Perry Plant potentially exceeded its rated power level. A GE | | software change disabled feedwater temperature compensation (FWC). Perry | | plant uses the 3D MONICORE output in subsequent calculations for power | | indication. Perry plant reduced power to 98% as a precaution, while Reactor | | Engineering confirms the power calculation error. A corrective action | | response team has been assembled, and the scope of the software change is | | being reviewed for any other possible effects on the plant. | | | | "In February of 1999, during plant coastdown to RFO7, and during subsequent | | removal of the '6B' feedwater heater, a condition was created in which the | | plant was operated at 100% power while at a reduced feedwater temperature. | | Preliminary investigations indicate that the plant could have violated its | | Operating License during this 2-day period of time. | | | | "This condition is being reported as a possible violation of the Operating | | License, and accordingly, it is required to be reported (24 hour, and | | Licensee Event Report) under the Perry Operating License section 2.F." | | | | The licensee plans to inform the NRC Resident Inspector. | | | | * * * UPDATE AT 2040 EST ON 12/16/99 BY S. SANDIN * * * | | | | "The 3D MONICORE did not have a problem. The problem was the 'databank.' | | This databank has cycle-specific data to support 3D MONICORE calculations. | | | | "The revision of 3D MONICORE was baseline 94 installed in 1996. There were | | NO changes to the MONICORE programs. | | | | "The databank was the BOC7 databank installed in October 1997." | | | | A value in the databank was set to zero following instructions from the | | vendor. The licensee did not recognize, and the vendor was unaware, that | | this data was utilized by another program. This resulted in incorrect | | temperature compensation during coastdown between 02/07 through 02/09/99 | | when the "6B" feedwater heater was removed from service. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36519 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 12/16/1999| | UNIT: [1] [] [] STATE: FL |NOTIFICATION TIME: 20:20[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 12/16/1999| +------------------------------------------------+EVENT TIME: 20:03[EST]| | NRC NOTIFIED BY: DAVE FIELDS |LAST UPDATE DATE: 12/16/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 CABLE SEPARATION INSIDE CONTAINMENT IS NOT AS DESCRIBED IN THE NRC | | SAFETY EVALUATION REPORT (SER) SUBMITTED FOR AN EXEMPTION GRANTED IN 1985. | | | | "Description of Condition: | | | | "FPL has identified inconsistencies between FPL's original exemption request | | for cable separation inside containment (K1) and the NRC SER for Unit 1 | | Appendix R. The 1985 NRC SER granted approval stating cables were routed on | | separate elevations, approximately 25 feet apart. However, the NRC 1987 SER | | granted approval stating cables were separated vertically by at least 25 | | feet. FPL's original submittal never stated that the cables were vertically | | separated by 25 feet but that the design was that redundant cables were | | routed at separate containment elevations. Although the 1987 NRC SER | | changes appear to be editorially based, it resulted in FPL not being in | | strict compliance with the latest NRC SER. | | | | "FPL has concluded that its original bases for the Unit 1 inside containment | | K1 Appendix R exemption remain valid The probability, magnitude, and | | consequences of a fire in these areas inside containment is extremely low | | for the following reasons: | | | | 1. The containment has a large volume with a high ceiling, which would | | dissipate the hot gases from a fire to the upper area of containment away | | from the affected area. | | | | 2. The cables in the effected cable tray are self-extinguishing which will | | minimize fire propagation along the cables. | | | | 3. The bottom cable trays are designed with solid bottoms, which | | effectively act as a radiant energy shield. | | | | 4. The main source of combustion inside containment is the oil in the RCP | | motors. However, the RCP motors are not in the vicinity of the affected | | cable trays. The affected cable trays are separated from the RCP motors by | | the biological shield. | | | | 5. The combustible loading in this portion of containment is low and in the | | area where the lack of separation occurs consists of mostly cable | | insulation, which has a high ignition temperature. | | | | 6. There are no fire hazards or ignition sources in the area. | | | | 7. All non-IEEE 383 cables are covered with a fire retardant coating. | | | | 8. This area has fire detectors, which would provide prompt notification of | | a fire to the control room. | | | | 9. The containment is inspected prior to operation for items that could | | impact sump operability; therefore, the potential for transient combustibles | | is precluded. In addition, the containment is a radiation control area with | | very limited access during power operation. The possibility of introducing | | new transient combustibles is very small. | | | | "FPL concludes that non-compliance with the NRC approved Unit 1 Appendix R | | exemption K1 does not constitute an operability concern. The original bases | | for FPL's exemption request provides reasonable assurance that a fire inside | | containment would not prevent the loss of any safe shutdown function. | | | | "Immediate Corrective Actions: | | | | 1. A containment loose debris inspection is performed following each | | containment entry during Modes 1-4. | | | | 2. If containment entry is being provided for maintenance purposes, an | | inventory of all material, tools, and other items intended to go into | | containment is performed. | | | | 3. All cable trays on the 18 foot and 23 foot elevations were verified to | | be free of debris and other fire hazards prior to heatup from the previous | | refueling outage. | | | | "The NRC resident inspector has been informed of this notification by the | | licensee." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36520 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CRYSTAL RIVER REGION: 2 |NOTIFICATION DATE: 12/16/1999| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 23:05[EST]| | RXTYPE: [3] B&W-L-LP |EVENT DATE: 12/16/1999| +------------------------------------------------+EVENT TIME: 20:47[EST]| | NRC NOTIFIED BY: RICKY RAWLS |LAST UPDATE DATE: 12/16/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STATE OF FLORIDA NOTIFICATION INVOLVING RESCUED LOGGER HEAD SEA TURTLE | | | | "[An] endangered Logger Head Sea Turtle was rescued at the Crystal River | | (CR-3) intake area. The turtle was injured but is expected to live. The | | Turtle was transported to Florida Power Corp. Mariculture Center. The | | Florida Department of Environmental Protection was notified at 2047 EST on | | 12/26/99." | | | | The licensee also informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36521 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 12/17/1999| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 00:30[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/16/1999| +------------------------------------------------+EVENT TIME: 20:52[EST]| | NRC NOTIFIED BY: SCOTT RICHARDSON |LAST UPDATE DATE: 12/17/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: |ROBERT GALLO NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION |FRANK CONGEL IRO | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC STARTING AND LOADING OF AN EMERGENCY DIESEL GENERATOR FOLLOWING A | | LOSS OF OFFSITE POWER TO THE TRAIN 'A' RESERVE AUXILIARY TRANSFORMER | | RESULTING IN A LOSS OF SPENT FUEL POOL COOLING FOR APPROXIMATELY 38 MINUTES | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[At 2052 on 12/16/99, the] Unit 1 Train 'A' [emergency diesel generator | | (CD EDG)] automatically started and loaded following [a] loss of offsite | | power to the 4-kV safeguards buses on Train 'A.' The apparent cause was the | | trip of the Unit 2 Train 'A' reserve feed transformer (201CD) sudden | | overpressurization relay. Trip of the 201CD sudden overpressurization | | relay resulted in opening of breaker 12CD which feeds the Unit 1 reserve | | feed transformer (101CD) as well as 201CD." | | | | "[Both] units were defueled at the time of the event with the Unit 1 [spent | | fuel pit (SFP)] pump in service. The loss of offsite power in Unit 1 caused | | the in-service SFP pump to be de-energized. The Unit 2 SFP pump was | | [manually] started at 2130 hours. SFP temperature remained constant at 85�F | | throughout this event." | | | | "The 201CD sudden overpressure relay was defeated, and offsite power was | | restored to the 101CD transformer. The CD EDG will be unloaded once offsite | | power is made available." | | | | "Actuation of the 201CD reserve transformer sudden overpressure relay was a | | result of filling the transformer with dry nitrogen following [planned] | | corrective maintenance activities." | | | | The licensee stated that both units were defueled with fuel in the common | | SFP. At the time of this event, offsite power to Unit 2 was being supplied | | by the normal auxiliary transformer (backfeed). All systems functioned as | | required and there was nothing unusual or not understood. At the time of | | this event notification, the licensee was in the process of removing the CD | | EDG from service and restoring the Train 'A' reserve feed transformer as the | | offsite power supply for Unit 1. | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021