Event Notification Report for October 22, 1999
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
10/21/1999 - 10/22/1999
** EVENT NUMBERS **
35183 35790 36079 36255 36325 36326 36327 36328
!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35183 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 12/21/1998|
| UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 19:16[EST]|
| RXTYPE: [1] GE-4 |EVENT DATE: 12/21/1998|
+------------------------------------------------+EVENT TIME: 16:20[EST]|
| NRC NOTIFIED BY: PETE ABBOTT |LAST UPDATE DATE: 10/21/1999|
| HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |JOHN WHITE R1 |
|10 CFR SECTION: | |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP | |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | |
|NLCO TECH SPEC LCO A/S | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 25 Power Operation |25 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| -HIGH PRESSURE COOLANT INJECTION SYSTEM INOPERABLE DUE TO SYSTEM FLOW |
| OSCILLATIONS- |
| |
| WHILE TESTING THE HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM AT 25% |
| POWER, THE LICENSEE OBSERVED SYSTEM FLOW OSCILLATIONS. THE LICENSEE REMOVED |
| THE HPCI TURBINE FROM SERVICE TO DETERMINE THE CAUSE AND TAKE CORRECTIVE |
| ACTIONS AND DECLARED THE HPCI SYSTEM INOPERABLE. TECH SPEC LCO A/S |
| 3.5.C.1.a REQUIRES THE LICENSEE TO RESTORE THE HPCI SYSTEM TO OPERABLE |
| STATUS WITHIN 7 DAYS. |
| |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. |
| |
| * * * UPDATE AT 1332 ON 10/21/99 BY BOB STEIGERWELD TO JOLLIFFE * * * |
| |
| This notification retracts an earlier report made at 1916 on 12/21/98 per |
| 10CFR50.72(b)(2)(iii)(B) and (D), due to observed flow oscillations during |
| HPCI System testing. On 12/23/98, the licensee determined that the flow |
| oscillation did not affect the operability of the HPCI System and this event |
| notification should have been retracted at that time. |
| |
| During HPCI System testing following a refueling outage, the HPCI System was |
| declared inoperable due to observed flow spiking indication on start up of |
| the system. Upon further investigation, the observed oscillations were |
| attributed to spiking on system startup due to either air in the flow |
| transmitter or electronic noise providing a false momentary indication. In |
| either case, it was demonstrated that the HPCI System was not affected by |
| the momentary spiking indication and the system was able to perform its |
| function and was determined to be operable. Therefore, this event |
| notification is being retracted. |
| |
| The licensee notified the NRC Resident Inspector. |
| |
| The NRC Operations Officer notified the R1DO Bill Cook. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 35790 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/03/1999|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:44[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/02/1999|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:30[CDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 10/21/1999|
| CITY: PADUCAH REGION: 3 +-----------------------------+
| COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION |
|LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 |
| DOCKET: 0707001 |DON COOL NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: THOMAS WHITE | |
| HQ OPS OFFICER: FANGIE JONES | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour |
| report) |
| |
| The following text is a portion of a facsimile received from Paducah: |
| |
| "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified |
| that numerous sprinkler heads were corroded, affecting 16 sprinkler systems |
| in C-337 and one system in C-333, such that the ability of the sprinklers to |
| flow sufficient water was called into question. Subsequently, these |
| sprinkler systems were declared inoperable, and TSR-required actions |
| establishing roving fire patrols were initiated. This deficiency was |
| detected during scheduled system inspections conducted by Fire Protection |
| personnel. Currently, functionality of the sprinkler heads has not been |
| fully evaluated by Fire Protection personnel, and the remaining cascade |
| buildings are currently being inspected, and if necessary, this report will |
| be updated to identify any additional areas. |
| |
| "It has been determined that this event is reportable under |
| 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to |
| function as designed." |
| |
| The NRC resident inspector has been notified of this event. |
| |
| |
| * * * UPDATE AT 1022 EDT ON 06/04/99 FROM CAGE TO TROCINE * * * |
| |
| "Two sprinkler heads on system D-1 in C-337 and two sprinkler heads on |
| system 27 in C-335 were identified to also be corroded. These were |
| identified to the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively, |
| and determined to require an update to this report by the PSS. |
| |
| "It has been determined that this event is reportable under |
| 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to |
| function as designed." |
| |
| Paducah personnel notified the NRC resident inspector of this update. The |
| NRC operations officer notified the R3DO (Hills) and NMSS EO (Combs). |
| |
| * * * UPDATE AT 2152 EDT ON 06/17/99 FROM WALKER TO POERTNER * * * |
| |
| "Three sprinkler heads on system C-15 and five sprinkler heads on system B-8 |
| in C-333 were identified to also be corroded. The PSS was notified of this |
| condition at 1300 CDT on 06/17/99 and determined that an update to this |
| report was required." |
| |
| "It has been determined that this event is reportable under |
| 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to |
| function as designed." |
| |
| Paducah personnel notified the NRC resident inspector of this update. The |
| NRC operations officer notified the R3DO (Madera). |
| |
| * * * UPDATE 1440 EDT 6/18/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * * |
| |
| "Two sprinkler heads on system C-15 and one sprinkler head on system B-8 in |
| C-333 were identified to have corrosion. The PSS was notified of this |
| condition at 1350 CDT on 06/18/99. The area of the fire patrol for system |
| C-15 was expanded to include the two heads identified as corroded. The one |
| head on system B-8 was in the area already being patrolled. The PSS |
| determined that an update to this report was required." |
| |
| The NRC resident inspector has been informed of this update. Notified R3DO |
| (Madera). |
| |
| * * * UPDATE 1315 EDT 6/25/1999 FROM WALKER TAKEN BY STRANSKY * * * |
| |
| "Two sprinkler heads on system D-8 and three sprinkler heads on system D-7 |
| in C-337 were identified to have corrosion. The PSS was notified of the |
| condition on system D-8 at 0125 CDT on 06/25/99 and at 1019 CDT on 06/25/99 |
| for system D-7. Both systems were immediately declared inoperable and LCO |
| fire patrol actions were implemented. It was determined that an update to |
| this report was required." |
| |
| The NRC resident inspector has been informed of this update. Notified R3DO |
| (Jordan). |
| |
| * * * UPDATE 2119 EDT 7/30/1999 FROM CAGE TAKEN BY STRANSKY * * * |
| |
| "Five sprinkler heads and one sprinkler piping tee on C-337 system D-7 were |
| identified to have corrosion. The PSS was notified of these corroded system |
| parts and declared the system inoperable at 0931 CDT on 07/30/99. LCO |
| required fire patrols of the affected area were initiated. The PSS |
| determined that an update to this event report was required." |
| |
| The NRC resident inspector has been informed of this update. Notified R3DO |
| (Wright). |
| |
| * * * UPDATE 1655 EDT 7/31/1999 FROM WHITE TAKEN BY STRANSKY * * * |
| |
| "Two sprinkler heads on C-337 System D-1 were identified to have corrosion. |
| The PSS was notified of these corroded system parts and declared the system |
| inoperable at 1155 CDT on 7/31/99. LCO required fire patrols of the |
| affected area were initiated. The PSS determined that an update to this |
| report was required." |
| |
| The NRC resident inspector has been informed of this update. Notified R3DO |
| (Wright). |
| |
| * * * UPDATE 1546 EDT 8/10/1999 FROM WHITE TAKEN BY STRANSKY * * * |
| |
| "Two sprinkler heads on C-337 system C-15 were identified to have corrosion. |
| The PSS was notified of these corroded system parts and declared the system |
| inoperable at 1130 CDT on 8/10/99. LCO required fire patrols of the |
| affected area were initiated. The PSS determined that an update to this |
| report was required." |
| |
| The NRC resident inspector has been informed of this update. Notified R3DO |
| (Burgess). |
| |
| * * * UPDATE AT 1154 EDT 8/22/99 FROM WALKER TO POERTNER * * * |
| |
| Four adjacent sprinkler heads on C-333 System B-1 were identified to have |
| corrosion. The PSS was notified of the corroded system parts and declared |
| the system inoperable at 0918 CDT on 8/22/99. LCO required fire patrols |
| were initiated. The PSS determined that an update to this report was |
| required. |
| |
| It has been determined that this event is reportable under 10CFR76.120(c)(2) |
| as an event in which equipment is disabled or fails to function as |
| designed. |
| |
| The NRC resident inspector will be notified. |
| |
| The NRC operations officer notified the R3DO (Clayton). |
| |
| * * * UPDATE 2015 EDT ON 8/28/99 FROM W.F. GAGE TO S. SANDIN * * * |
| |
| The following information was provided as an update to this report: |
| |
| "Two adjacent sprinkler heads on C-337 System D-11 were identified to have |
| corrosion. The PSS was notified of these corroded system parts and declared |
| the system inoperable at 1420 [CDT] on 8/28/99. LCO required fire patrols |
| of the affected area were initiated. The PSS determined that an update to |
| this report was required." |
| |
| Paducah personnel informed the NRC resident inspector. The NRC operations |
| officer notified the R3DO (Leach) and NMSS EO (Piccone). |
| |
| * * * UPDATE 2037 EDT ON 8/29/99 FROM KEVIN BEASLEY TO S. SANDIN * * * |
| |
| The following information was provided as an update to this report: |
| |
| "Two adjacent sprinkler heads on C-337 System D-15 were identified to have |
| corrosion and the PSS declared the system inoperable at 0925 [CDT] on |
| 8/29/99. Also two adjacent heads on C-337 System D-10 were identified to |
| have corrosion and the PSS declared the system inoperable at 1450. LCO |
| required fire patrols for both of the affected areas were initiated in the |
| time frame required by TSR. The PSS determined that an update to this |
| report was required." |
| |
| Paducah personnel informed the NRC resident inspector. The NRC operations |
| officer notified the R3DO (Leach) and NMSS EO (Piccone). |
| |
| * * * UPDATE AT 0930 EDT ON 9/1/99 BY ERIC WALKER TO FANGIE JONES * * * |
| |
| Add two adjacent sprinkler heads on C-337 D-14. Paducah personnel informed |
| the NRC Resident Inspector. The NRC operations officer notified the R3DO |
| (David Hills) and NMSS (Robert Pierson). |
| |
| * * * UPDATE AT 1133 EDT ON 9/8/99 BY TOM WHITE TO FANGIE JONES * * * |
| |
| Add two adjacent sprinkler heads on C-331 System 26, system declared |
| inoperable at 2155 CDT on 9/7/99. An LCO required fire patrol for the |
| affected area was initiated in the time frame required by the TSR. Paducah |
| personnel informed the NRC Resident Inspector. The NRC operations officer |
| notified the R3DO (Monte Phillips) and NMSS (Josie Piccone). |
| |
| * * * UPDATE AT 0948 ON 9/30/99 BY ERIC WALKER TO DOUG WEAVER * * * |
| |
| Add two adjacent sprinkler heads on C-333 System B-15 were identified to |
| have corrosion and the PSS declared the system inoperable at 0815 on |
| 9/30/99. An LCO required fire patrol for the affected area was initiated in |
| the time frame required by the TSR. The PSS determined that an update to |
| this report was required. |
| Paducah personnel informed the NRC resident inspector. The NRC operations |
| officer notified the R3DO (Vegel) and NMSS (Cool). |
| |
| |
| *** UPDATE ON 10/13/99 @ 1600 BY WALKER TO GOULD *** |
| |
| Two adjacent sprinkler heads on C-333 System A-11 were Identified to have |
| corrosion and the PSS declared the system inoperable at 1307 on 10-13-99. An |
| LCO required fire patrol for the affected area was initiated in the time |
| frame required by the TSR, The PSS determined that an update to this report |
| was required. Paducah personnel informed the NRC resident inspector. The |
| NRC operations officer notified the R3DO (Madera) and NMSS (Moore). |
| |
| * * * UPDATE 1520 10/19/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * * |
| |
| Six sprinkler heads on C-337 System D-16 were identified to have corrosion |
| and the PSS declared the system inoperable at 1052 CDT on 10/19/99. An LCO |
| required fire patrol for the affected area was initiated in the time frame |
| required by the TSR. The PSS determined that an update to this report was |
| required. The NRC resident inspector has been informed of this update. |
| Notified R3DO (Jorgensen). |
| |
| * * * UPDATE 2140 10/19/1999 FROM WALKER TAKEN BY STRANSKY * * * |
| |
| Seven sprinkler heads on C-337 System A-7 were identified to have corrosion, |
| and another four had been painted over. In addition, three adjacent |
| sprinkler heads pm C-337 System A-8 were identified to have corrosion. The |
| PSS declared the systems inoperable at 1900 CDT on 10/19/99. LCO required |
| fire patrols for the affected areas were initiated in the time frame |
| required by the TSR. The PSS determined that an update to this report was |
| required. The NRC resident inspector has been informed of this update. |
| Notified R3DO (Wright). |
| |
| * * * UPDATE AT 1713 ON 10/21/99 FROM CAGE TAKEN BY JOLLIFFE * * * |
| |
| Four sprinkler heads on C-337 System A-5, twelve sprinkler heads on C-337 |
| System A-8, three sprinkler heads on C-337 System A-9, and six sprinkler |
| heads on C-337 System B-8 were identified to have corrosion. On 10/21/99, |
| the PSS declared System A-5 and A-9 inoperable at 1028 CDT, System A-8 |
| inoperable at 1227 CDT and System B-8 inoperable at 1406 CDT. An LCO |
| required fire patrol for the affected areas was initiated in the time frame |
| required by the TSR.. The PSS determined that an update to this report was |
| required. The NRC Resident Inspector has been informed of this update. The |
| NRC Operations Officer notified R3DO Bruce Jorgensen. |
+------------------------------------------------------------------------------+
!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36079 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 08/27/1999|
| UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 06:48[EDT]|
| RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/27/1999|
+------------------------------------------------+EVENT TIME: 06:00[EDT]|
| NRC NOTIFIED BY: DAVE WALSH |LAST UPDATE DATE: 10/21/1999|
| HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |KATHLEEN MODES R1 |
|10 CFR SECTION: | |
|AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| EMERGENCY SERVICE WATER SYSTEM DEGRADATION (ONLY ONE OF FOUR PUMPS |
| OPERABLE) |
| |
| The following text is a portion of a facsimile received from the licensee: |
| |
| "On 08/26/99, Susquehanna Unit 1 and Unit 2 were operating at 100% power |
| with the 'B' loop of emergency service water [(ESW)] out of service for |
| scheduled maintenance. During testing on the ESW system, with all ESW pumps |
| in service, it was identified that the 'C' and 'D' ESW pumps' discharge |
| check valves were closed. The ESW flow surveillance was performed, and the |
| 'C' and 'D' ESW pumps failed to achieve the required flow and were declared |
| inoperable. Concurrently, the 'B' loop of ESW was returned to service. |
| During the time the 'B' ESW loop was inoperable, the 'A' ESW pump was the |
| only one operable ESW pump. This constitutes a serious degradation of the |
| plant in that it is a condition which is outside of design basis and, |
| therefore, reportable under 10 CFR 50.72(b)(1)(ii) requiring a 1-hour ENS |
| notification." |
| |
| The licensee notified the NRC resident inspector. |
| |
| * * * UPDATE 1453EDT ON 9/3/99 FROM GRANT FERNSLER TO S. SANDIN * * * |
| |
| "This Notification is a retraction of a previous ENS Notification made |
| 8/27/99 (Event # 36079)." |
| |
| "Subsequent evaluation by Engineering has concluded that the plant had at |
| least two Emergency Service |
| Water pumps capable of performing their specified safety function at all |
| times. As such, the plant was not |
| in a condition outside of its design basis and the report previously made |
| pursuant to 10CFR50.72(b)(1)(ii) |
| is hereby retracted." |
| |
| The licensee informed the NRC Resident Inspector. Notified R1DO(Rogge). |
| |
| * * *UPDATE 0316EDT ON 09/23/99 FROM MIKE PEAL TAKEN BY MACKINNON* * * |
| |
| The licensee is Retracting the Retraction they called in on 09/03/99 at |
| 1453EDT. |
| |
| "On 09/22/99 at 2230, an Engineering evaluation concluded that the |
| operability determination associated with the above stated event was not |
| adequate, specifically relating to the potential for pump interaction to |
| create low flow conditions. " |
| |
| "The Engineering evaluation was being performed in response to an anomaly |
| identified on 09/20/99 during the run of 'D' Diesel Generator. During the |
| preparation of the operability statement for the 09/20/99 anomaly, |
| engineering personnel realized that incorrect assumptions were used in the |
| previous operability statement. The 'C' and 'D' ESW pumps were declared |
| inoperable at 2230 on 09/22/99. Evaluation continues to determine if other |
| combinations of equipment out of service times result in additional |
| reportable conditions." R1DO (Bob Summers) notified. |
| |
| The NRC Resident Inspector will be notified of the Retraction to the |
| Retraction of this event by the licensee. |
| |
| * * * UPDATE AT 1325 ON 10/21/99 BY MIKE PEAL TO JOLLIFFE * * * |
| |
| Based on additional evaluations by Licensee Engineering, Operations and |
| Licensing spanning the time frame of 06/03/99 to 09/28/99, the licensee |
| concluded that the plant had at least one Emergency Service Water Pump per |
| loop capable of performing its specified safety function at all times. As |
| such, the plant was not in a condition outside of its design basis, was not |
| in an unanalyzed condition, and there was no loss of safety function. The |
| report previously made pursuant to 10CFR50.72(b)(1)(ii) on 09/23/99 is |
| hereby retracted. |
| |
| The licensee plans to notify the NRC Resident Inspector. |
| |
| The NRC Operations Officer notified the R1DO Bill Cook. |
+------------------------------------------------------------------------------+
!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36255 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 10/02/1999|
| UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 21:03[EDT]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 10/02/1999|
+------------------------------------------------+EVENT TIME: 19:05[CDT]|
| NRC NOTIFIED BY: FRAWLEY |LAST UPDATE DATE: 10/21/1999|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |JEFF SHACKELFORD R4 |
|10 CFR SECTION: | |
|DDDD 73.71 UNSPECIFIED PARAGRAPH | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 94 Power Operation |94 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| UNACCOUNTED FOR ACCESS KEY. COMPENSATORY MEASURES WERE PUT INTO PLACE. |
| |
| SEE HOO LOG FOR DETAILS. |
| |
| THE RESIDENT INSPECTOR WAS NOTIFIED. |
| |
| * * * UPDATE AT 1658 ON 10/21/99 BY KATHLEEN WORK TO JOLLIFFE * * * |
| |
| THE LICENSEE DESIRES TO RETRACT THIS EVENT AS A REPORTABLE EVENT AND WILL |
| LOG THIS EVENT IN THEIR SAFEGUARDS EVENT LOG SINCE SECURITY IMPLEMENTING |
| COMPENSATORY ACTIONS WERE IMPLEMENTED WITHIN 15 MINUTES FROM THE TIME THE |
| LICENSEE DISCOVERED THAT THE KEY WAS MISSING. |
| |
| SEE THE HOO LOG FOR DETAILS. |
| |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. |
| |
| THE NRC OPERATIONS OFFICER NOTIFIED THE R4DO LINDA SMITH. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 36325 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 10/21/1999|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:37[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 10/20/1999|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 10:30[EDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 10/21/1999|
| CITY: PIKETON REGION: 3 +-----------------------------+
| COUNTY: PIKE STATE: OH |PERSON ORGANIZATION |
|LICENSE#: GDP-2 AGREEMENT: N |BRUCE JORGENSEN R3 |
| DOCKET: 0707002 |BRIAN SMITH EO NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: LARSON | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|NBNL RESPONSE-BULLETIN | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| 24 HOUR 91-01 BULLETIN RESPONSE |
| |
| ON 10/20/99 AT 1030 HOURS, A NUCLEAR CRITICALITY SAFETY ANALYSIS (NCSA) |
| NONCOMPLIANCE WAS IDENTIFIED IN THE X-330 PROCESS BUILDING. THIS |
| NONCOMPLIANCE WAS DISCOVERED WHILE REVIEWING OBSERVATIONS FOUND DURING A |
| WALKDOWN OF IMPLEMENTED NCSAs. |
| |
| AT COLUMN C-53 ON THE CELL FLOOR OF X-330, A DRIP PAN CONNECTED TO A PAIR OF |
| LUBE OIL STRAINERS DID NOT MEET THE REQUIREMENTS OF NCSA-PLANT054 FOR LUBE |
| OIL SYSTEMS. NCSA-PLANT054 REQUIRES ALL LUBE OIL LEAK COLLECTION CONTAINERS |
| IN AREAS WHERE SIGNIFICANT UF6 RELEASES ARE CONSIDERED CREDIBLE, MEET |
| CERTAIN SIZE RESTRICTIONS. IN X-330, THE MAXIMUM ALLOWED DEPTH OF A LUBE OIL |
| DRIP PAN ON THE CELL FLOOR IS 3.6 INCHES. THE DRIP PAN FOUND WAS 5.76 INCHES |
| DEEP. THIS VIOLATES THE CONTAINER SIZE REQUIREMENT OF THE NCSA. THE DRIP PAN |
| CONTAINED APPROXIMATELY 25 QUARTS OF OIL AT TIME OF DISCOVERY. THERE WAS NO |
| EVIDENCE OF ANY UF6 RELEASES IN THE AREA. |
| |
| THE CONTAINER SIZE LIMIT WAS EXCEEDED RESULTING IN THE LOSS OF GEOMETRY. THE |
| OTHER CONTROL OF THE DOUBLE CONTINGENCY PRINCIPLE (CONCENTRATION) WAS |
| MAINTAINED THROUGHOUT THIS EVENT. |
| |
| DOUBLE CONTINGENCY WAS REESTABLISHED BY OPENING AND TAGGING (DO NOT CLOSE) |
| THE DRAIN VALVE IN THE BOTTOM OF THE DRIP PAN. THIS PREVENTS THE |
| ACCUMULATION OF LUBE OIL TO A DEPTH GREATER THAN 3.6 INCHES. A WORK PACKAGE |
| WAS DEVELOPED TO REMOVE THE DRIP PAN AND REPLACE IT WITH ONE THAT IS IN |
| COMPLIANCE WITH NCSA-PLANT054. AT 1400 HOURS |
| ON 10/20/99, THE NONCOMPLIANT DRIP PAN WAS REMOVED AND REPLACED WITH A PAN |
| HAVING A DEPTH OF UNDER THREE INCHES, REESTABLISHING NCSA-PLANT054 |
| COMPLIANCE. |
| |
| THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR |
| RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. |
| |
| THE NRC RESIDENT INSPECTOR AND THE DOE REPRESENTATIVE WERE NOTIFIED. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36326 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 10/21/1999|
| UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 15:04[EDT]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 10/21/1999|
+------------------------------------------------+EVENT TIME: 10:22[PDT]|
| NRC NOTIFIED BY: DICK LUCKETT |LAST UPDATE DATE: 10/21/1999|
| HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |LINDA SMITH R4 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N N 0 Refueling |0 Refueling |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| - OFFSITE AGENCIES NOTIFIED OF A SPILL OF 3 OUNCES OF HYDRAULIC FLUID INTO |
| PACIFIC OCEAN - |
| |
| THE LICENSEE NOTIFIED THE NATIONAL RESPONSE CENTER (EPA CASE #503190), THE |
| CALIFORNIA OFFICE OF EMERGENCY SERVICES, AND THE NRC RESIDENT INSPECTOR OF A |
| SPILL OF APPROXIMATELY THREE OUNCES OF BIODEGRADABLE HYDRAULIC FLUID FROM A |
| KELP HARVESTER INTO THE PACIFIC OCEAN. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 36327 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: ALLIED-SIGNAL INC. |NOTIFICATION DATE: 10/21/1999|
| RXTYPE: URANIUM HEXAFLUORIDE PRODUCTION |NOTIFICATION TIME: 17:31[EDT]|
| COMMENTS: UF6 CONVERSION (DRY PROCESS) |EVENT DATE: 10/21/1999|
| |EVENT TIME: 16:00[CDT]|
| |LAST UPDATE DATE: 10/21/1999|
| CITY: METROPOLIS REGION: 3 +-----------------------------+
| COUNTY: MASSAC STATE: IL |PERSON ORGANIZATION |
|LICENSE#: SUB-526 AGREEMENT: Y |BRUCE JORGENSEN R3 |
| DOCKET: 04003392 |CHARLEY HAUGHNEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: HUGH ROBERTS | |
| HQ OPS OFFICER: DICK JOLLIFFE | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|KBBF 70.50(b)(2)(ii) EQUIP DISABLED/FAILS | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| - PLANT FIRE WATER DELUGE SYSTEM LINE RUPTURED INSIDE THE PLANT - |
| |
| A SIX INCH RECTIFIER 'A' & 'B' PLANT FIRE WATER DELUGE SYSTEM LINE RUPTURED |
| INSIDE THE PLANT. THE LICENSEE ISOLATED THE RUPTURE AND PLANS TO POST A |
| FIRE WATCH AND REPAIR/REPLACE THE RUPTURED SECTION OF LINE. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 36328 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 10/22/1999|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 03:01[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 10/21/1999|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:00[EDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 10/22/1999|
| CITY: PIKETON REGION: 3 +-----------------------------+
| COUNTY: PIKE STATE: OH |PERSON ORGANIZATION |
|LICENSE#: GDP-2 AGREEMENT: N |BRUCE JORGENSEN R3 |
| DOCKET: 0707002 |CHARLEY HAUGHNEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: SPAETH | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|NBNL RESPONSE-BULLETIN | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| 24 HOUR 91-01 BULLETIN RESPONSE |
| |
| On 10/21/ 1999 at 1500 hrs the Plant Shift Superintendent(PSS) was notified |
| that a Nuclear Criticality Safety Approval (NCSA) requirement was not being |
| performed in the X-710 ES&H Analytical Labs. NCS Engineering, while |
| performing an NCS Self Assessment, noticed an operation where samples were |
| brought to a staging area "INSIDE" a room when they were logged in and |
| verified. (NCSA-0710_025.AOO) |
| |
| Requirement #1 of NCSA-071_25.AOO states in part; Samples in any room |
| enriched to 1% or greater U-235, will be limited to one group of 30g U-235 |
| per room. This will be ensured by maintaining a room inventory log of U-235 |
| mass in labeled containers. Each log entry will consist of the U-235 mass |
| value plus analytical uncertainty and will be: |
| |
| a. made by a knowledgeable person "PRIOR" to bringing the samples into the |
| room, and |
| b. verified by a second knowledgeable person "PRIOR" to bringing the samples |
| into the room. |
| |
| At the direction of the Plant Shift Superintendent the requirements for an |
| NCS anomalous condition were initiated and the area baundaried off. |
| |
| The safety significance of the event is very low. The U-235 mass in material |
| is being maintained less than 30 grams as required. This is more than a |
| factor of 10 less than the always safe mass of 350 grams U-235. The samples |
| were brought to a staging area inside the room where they were logged in and |
| verified. After logging and verifying the samples were moved to the |
| operational area of the room, where they could interact with other materials |
| in the room. |
| |
| Samples in any room enriched to 1% or greater U-235, with a concentration |
| greater or equal to 500 ppm U-235, shall be limited to one group of 30 g |
| U-235 per room. This shall be ensured by maintaining a room inventory log of |
| U-235 mass in labeled containers. Each log entry shall consist of the U-235 |
| mass value plus analytical uncertainty and shall be: |
| |
| Mass is the only parameter controlled |
| |
| The actual amount of material In the room is less than 30 grams U-235, at an |
| enrichment of less than or equal to 100%. This value is obtained from sample |
| data that was logged after the material was brought Into the room. This is |
| approximately 4% of the worst case critical mass. |
| |
| Verbatim compliance with both mass controls was lost because the material |
| was supposed to be checked and verified prior to bringing the material into |
| the room. The samples were brought to a staging area inside the room where |
| they were logged in and verified. After logging and verifying the samples |
| were moved to the operational area of the room, where they could interact |
| with other materials in the room. |
| |
| THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR |
| RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. |
| |
| The Resident Inspector was notified and the DOE Representative will be |
| notified. |
+------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021