Event Notification Report for August 23, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/20/1999 - 08/23/1999 ** EVENT NUMBERS ** 35790 36040 36045 36049 36050 36051 36052 36053 36054 36055 36056 36057 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35790 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/03/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:44[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/02/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:30[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/22/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 | | DOCKET: 0707001 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: THOMAS WHITE | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour | | report) | | | | The following text is a portion of a facsimile received from Paducah: | | | | "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified | | that numerous sprinkler heads were corroded, affecting 16 sprinkler systems | | in C-337 and one system in C-333, such that the ability of the sprinklers to | | flow sufficient water was called into question. Subsequently, these | | sprinkler systems were declared inoperable, and TSR-required actions | | establishing roving fire patrols were initiated. This deficiency was | | detected during scheduled system inspections conducted by Fire Protection | | personnel. Currently, functionality of the sprinkler heads has not been | | fully evaluated by Fire Protection personnel, and the remaining cascade | | buildings are currently being inspected, and if necessary, this report will | | be updated to identify any additional areas. | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | The NRC resident inspector has been notified of this event. | | | | | | * * * UPDATE AT 1022 ON 06/04/99 FROM CAGE TO TROCINE * * * | | | | "Two sprinkler heads on system D-1 in C-337 and two sprinkler heads on | | system 27 in C-335 were identified to also be corroded. These were | | identified to the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively, | | and determined to require an update to this report by the PSS. | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | Paducah personnel notified the NRC resident inspector of this update. The | | NRC operations officer notified the R3DO (Hills) and NMSS EO (Combs). | | | | * * * UPDATE AT 2152 ON 06/17/99 FROM WALKER TO POERTNER * * * | | | | "Three sprinkler heads on system C-15 and five sprinkler heads on system B-8 | | in C-333 were identified to also be corroded. The PSS was notified of this | | condition at 1300 CDT on 06/17/99 and determined that an update to this | | report was required." | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | Paducah personnel notified the NRC resident inspector of this update. The | | NRC operations officer notified the R3DO (Madera). | | | | * * * UPDATE 1440 6/18/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system C-15 and one sprinkler head on system B-8 in | | C-333 were identified to have corrosion. The PSS was notified of this | | condition at 1350 CDT on 06/18/99. The area of the fire patrol for system | | C-15 was expanded to include the two heads identified as corroded. The one | | head on system B-8 was in the area already being patrolled. The PSS | | determined that an update to this report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Madera). | | | | * * * UPDATE 1315 6/25/1999 FROM WALKER TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system D-8 and three sprinkler heads on system D-7 | | in C-337 were identified to have corrosion. The PSS was notified of the | | condition on system D-8 at 0125 CDT on 06/25/99 and at 1019 CDT on 06/25/99 | | for system D-7. Both systems were immediately declared inoperable and LCO | | fire patrol actions were implemented. It was determined that an update to | | this report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Jordan). | | | | * * * UPDATE 2119 7/30/1999 FROM CAGE TAKEN BY STRANSKY * * * | | | | "Five sprinkler heads and one sprinkler piping tee on C-337 system D-7 were | | identified to have corrosion. The PSS was notified of these corroded system | | parts and declared the system inoperable at 0931 CDT on 07/30/99. LCO | | required fire patrols of the affected area were initiated. The PSS | | determined that an update to this event report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Wright). | | | | * * * UPDATE 1655 7/31/1999 FROM WHITE TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on C-337 System D-1 were identified to have corrosion. | | The PSS was notified of these corroded system parts and declared the system | | inoperable at 1155 CDT on 7/31/99. LCO required fire patrols of the | | affected area were initiated. The PSS determined that an update to this | | report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Wright). | | | | * * * UPDATE 1546 8/10/1999 FROM WHITE TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on C-337 system C-15 were identified to have corrosion. | | The PSS was notified of these corroded system parts and declared the system | | inoperable at 1130 CDT on 8/10/99. LCO required fire patrols of the | | affected area were initiated. The PSS determined that an update to this | | report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Burgess). | | | | * * * UPDATE AT 1154 8/22/99 FROM WALKER TO POERTNER * * * | | | | Four adjacent sprinkler heads on C-333 System B-1 were identified to have | | corrosion. The PSS was notified of the corroded system parts and declared | | the system inoperable at 0918 CDT on 8/22/99. LCO required fire patrols | | were initiated. The PSS determined that an update to this report was | | required. | | | | It has been determined that this event is reportable under 10CFR76.120(c)(2) | | as an event in which equipment is disabled or fails to function as | | designed. | | | | The NRC resident inspector will be notified. | | | | The NRC operations officer notified the R3DO (Clayton). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36040 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 08/18/1999| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 21:04[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 08/18/1999| +------------------------------------------------+EVENT TIME: 19:56[EDT]| | NRC NOTIFIED BY: PHIL NORTH |LAST UPDATE DATE: 08/20/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KENNETH BARR R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO A GENERATOR LOCKOUT FOR UNKNOWN REASONS | | | | At 1956 on 08/18/99, Oconee Unit 1 automatically tripped from 100% power, | | and the cause of the trip is currently under investigation. At this time, | | the licensee believes that an electrical generator lockout (for unknown | | reasons) cause a turbine trip and subsequent reactor trip. Post-trip | | response was normal. All control rods fully inserted. There were no | | emergency core cooling system or engineered safety feature actuations, and | | none were required. The main steam safety valves lifted and reseated as | | expected. There were no maintenance or surveillance activities occurring at | | the time of the generator lockout. There were no storms in the area, and | | the weather was stable and hot. All systems functioned as required, and the | | cause of the generator lockout is the only thing that is not understood at | | this time. | | | | The reactor is currently subcritical, and shutdown margin is within | | technical specification limits. Reactor coolant system inventory control is | | being provided via normal makeup. The power-operated relief valves and | | pressurizer code safety valves are closed. Primary system transport is | | being controlled by forced circulation via all four reactor coolant pumps. | | Secondary steam is being dumped to the main condenser via the turbine bypass | | valves, and main feedwater is supplying water to the steam generators. | | | | The licensee notified the NRC resident inspector. | | | | *** UPDATE AT 1242 EDT ON 8/20/99 FROM NICHOLSON TO POERTNER *** | | | | The original cause of the Oconee Unit 1 trip on 8/18/99 was believed to have | | been an electrical generator lockout based on annunciation available at the | | time. Subsequent evaluation has concluded that the trip was caused by an | | internal voltage problem within the solid state programmer for the group 5 | | control rods. This voltage anomaly caused the Group 5 rods to drop into the | | core. The entire programmer has been replaced, with the defective equipment | | being returned to the manufacturer for additional evaluation. | | | | The NRC resident inspector has been notified. | | | | The HOO notified the R2DO (BARR) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36045 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: IDAHO NAT ENGR & ENVIRONMENTAL LAB |NOTIFICATION DATE: 08/19/1999| |LICENSEE: IDAHO NAT ENGR & ENVIRONMENTAL LAB |NOTIFICATION TIME: 16:24[EDT]| | CITY: IDAHO FALLS REGION: 4 |EVENT DATE: 08/19/1999| | COUNTY: STATE: ID |EVENT TIME: 13:34[MDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 08/20/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA HOWELL R4 | | |JOSIE PICCONE NMSS | +------------------------------------------------+JOSEPH GIITTER IRO | | NRC NOTIFIED BY: SCOTT SCHUM |WILLIAM BEECHER PAO | | HQ OPS OFFICER: WILLIAM POERTNER |YATES DOE | +------------------------------------------------+BLANCHARD EPA | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DOE ALERT DECLARED DUE TO A FIRE IN THE DESERT ON DOE CONTROLLED PROPERTY. | | | | This event was classified as an alert at 1334 MDT in accordance with | | Department of Energy (DOE) procedures. This is not a classification driven | | by the Three Mile Island Independent Spent Fuel Storage Facility (ISFSI) | | emergency plan. | | | | A range fire occurred on DOE controlled property. The Idaho Nuclear | | Engineering and Environmental Laboratory (INEEL) fire department and Bureau | | of Land Management (BLM) are fighting the fire. The fire is not threatening | | any site area. The fire is presently located 12 miles east of the ISFSI | | facility and is traveling north, away from the facility. Eight BLM rigs are | | in route to the fire. | | | | DOE made notifications per procedures to activate the Emergency Operations | | Center (EOC) and Emergency Control Center (ECC). DOE notified State and | | Local Authorities. | | | | NRC assistance was not requested. | | | | *** UPDATE AT 2039 EDT ON 8/20/99 FROM SCHUM TO POERTNER *** | | | | The DOE Alert was terminated at 1833 MDT when the range fire was | | extinguished. | | | | HOO notified R4DO (Howell), NMSS EO (Holonich), IRO (Giitter), PAO | | (Beecher), FEMA (Bagwell), HHS-CDC (Davis), EPA-NRC (Gauter), DOE (Young), | | and USDA (Conley) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 36049 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ST. CLARES HOSPITAL/DOVER |NOTIFICATION DATE: 08/20/1999| |LICENSEE: ST. CLARES HOSPITAL/DOVER |NOTIFICATION TIME: 11:48[EDT]| | CITY: DOVER REGION: 1 |EVENT DATE: 08/20/1999| | COUNTY: STATE: NJ |EVENT TIME: 11:00[EDT]| |LICENSE#: 29-13746-02 AGREEMENT: N |LAST UPDATE DATE: 08/20/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PETER ESELGROTH R1 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOSEPH BARBIERI | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST I-125 SEEDS | | | | At 0900 EDT 8/19/99, 80 seeds of I-125 were delivered to the loading dock at | | ST. Clares Hospital/Dover. The seeds were inadvertently sent to ST. Clares | | Hospital/Denvile from the loading dock. The I-125 seeds were located at | | 1100 EDT and secured in the ST. Clare Hospital/Denvile Nuclear Medicine | | Department. The activity of each seed was 0.7 mCi. | | | | *** UPDATE AT 1454 EDT ON 8/20/99 FROM BARBIERI TO POERTNER *** | | | | Licensee determined that loading dock person opened the cardboard package | | and found name of person formally located at ST. Clares Hospital/Denvile on | | papers located inside the package. He then sent the package to ST. Clares | | Hospital/Denvile. The licensee surveyed inner package and found no | | contamination. | | | | HOO notified R1DO (ESELGROTH) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36050 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 08/20/1999| |LICENSEE: UNIVERSITY OF TEXAS |NOTIFICATION TIME: 12:00[EDT]| | CITY: HOUSTON REGION: 4 |EVENT DATE: 03/10/1999| | COUNTY: STATE: TX |EVENT TIME: [CDT]| |LICENSE#: L00466 AGREEMENT: Y |LAST UPDATE DATE: 08/20/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA HOWELL R4 | | |JOE DECICCO NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM OGDEN (FAX) | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT OF A MEDICAL MISADMINISTRATION AT ANDERSON CANCER | | CENTER IN HOUSTON TEXAS. | | | | The following text is a portion of a facsimile received from the Texas | | Department of Health Bureau of Radiation Control: | | | | " Incident 7471 - Broad License L00466, The university of Texas, M.D. | | Anderson Cancer Center, Houston, Texas" | | | | "Date of Event: March 9, 1999." | | | | "Initial Report: Telephonic report March 10, 1999. (Lost)" | | | | "On the afternoon of March 9, 1999, a patient was loaded with a 51.25 mgRaeq | | (127.35 millicurie Cesium-137) gynecological implant for a planned treatment | | time of 44.77 hours. Late that evening the patient was discovered to have | | removed the implant. The implant was discovered in the bed beside the | | patient's hand/arm at hip level. Nursing staff removed the loading to the | | far side of the room, placed a rolling lead shield between the source and | | the patient, then notified the Gynecological physician on duty and the | | Brachytherapy Services staff. Estimated treatment time was only about 8.833 | | hours. This treatment time differed from the prescribed treatment dose by | | more than 10%. The patient treatment was terminated without additional | | treatment. The event was reported telephonically on the afternoon of March | | 10, 1999. This message was never delivered to the proper authorities within | | the Agency. An initial written report filed by the hospital stated that the | | facility Radiation Safety Committee did not consider this a | | misadministration but a refusal of treatment by the patient. The 10% rule | | was considered by the Agency and a full report was filed by the hospital." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36051 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/20/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 19:06[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/20/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 12:15[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/20/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRENT CLAYTON R3 | | DOCKET: 0707001 |JOE HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC WALKER | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01, 24 HOUR REPORT | | | | At 1242 CDT on 8/20/99, the Plant Shift Superintendent was notified that | | adjacent system post-removal Non-Destructive Assay (NDA) was not performed | | as required by NCSA GEN-10 for the Unit 3, Cell 7, Stage 8B blowout | | preventer actuator removed in the C-335 cascade building. The post-removal | | NDA is required to be performed within 24 hours of the equipment being | | removed. The post-removal NDA measurement is used to independently verify | | the mass of any potential adjacent system deposit is less than an always | | safe mass and can be characterized as Uncomplicated Handling (UH). The | | pre-removal NDA indicated no significant deposit in the adjacent system. | | | | The post-removal NDA measurement was subsequently performed within 4 hours | | of discovery which confirmed the adjacent system to be UH. | | | | This event is being categorized as a 24 hour event in accordance with Safety | | Analysis Report Table 6.9-1, Criteria A.4.a and Bulletin 91-01, Supplement | | 1. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36052 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 08/21/1999| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 12:51[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/20/1999| +------------------------------------------------+EVENT TIME: 16:45[EDT]| | NRC NOTIFIED BY: JOHN HUNTER |LAST UPDATE DATE: 08/21/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETER ESELGROTH R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL INITIATION OF HVAC CHLORINE ISOLATION MODE | | | | At 1645 EDT on 8/20/99 an equipment operator reported a faint smell of | | chlorine in the Unit 2 reactor building (253 foot elevation). The floor | | supervisor was dispatched to investigate. The main control room personnel | | placed the Main Control Room (MCR) HVAC system in a chlorine isolation mode | | as a planned conservative measure. No indication of chlorine was ever | | present on the MCR HVAC chlorine detectors. The floor supervisor reported | | that there was a slight, barely detectable, chlorine like odor in the area | | but that it had dissipated. The MCR HVAC system was returned to the normal | | mode of operation at 2304 EDT 8/20/99. There was no adverse impact to plant | | operations. | | | | A subsequent review of the reportability requirements was made on 8/21/99 at | | 1000 EDT and it was determined that a four hour report pursuant to | | 50.72(b)(2)(ii) should be made for the manual initiation of a MCR chlorine | | isolation. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 36053 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIVERSITY OF CT HEALTH CENTER |NOTIFICATION DATE: 08/21/1999| |LICENSEE: UNIVERSITY OF CT HEALTH CENTER |NOTIFICATION TIME: 14:31[EDT]| | CITY: FARMINGTON REGION: 1 |EVENT DATE: 08/20/1999| | COUNTY: STATE: CT |EVENT TIME: 17:45[EDT]| |LICENSE#: 0613022 AGREEMENT: N |LAST UPDATE DATE: 08/21/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PETER ESELGROTH R1 | | |JOE HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KEN PRICE | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATION | | | | On 8/20/99, a possible medical misadministration occurred at University of | | CT Health Center located in Farmington, Conn. The physician prescribed a | | dose of 13 millicuries P-32 (Chromic Phosphate) for a lung cancer patient. | | After injection, it was determined that only 6.9 millicuries of P-32 had | | been injected. The physician issued a revised written directive for 7 | | millicuries of P-32 based on the patients condition. | | | | (Call the NRC Operations Center for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36054 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 08/21/1999| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 16:18[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/21/1999| +------------------------------------------------+EVENT TIME: 15:05[EDT]| | NRC NOTIFIED BY: STEVE KOSHAR |LAST UPDATE DATE: 08/21/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT THE TECH SPEC ALLOWABLE LIMIT FOR DEGRADED BUS VOLTAGE | | SETTINGS MAY NOT PROTECT ALL SAFEGUARDS LOADS FROM THE EFFECTS OF AN | | UNDERVOLTAGE CONDITION UNDER ALL ACCIDENT CONDITIONS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 1305 [hours EDT on] 08/21/99, [the licensee] determined that the | | technical specification allowable limit for degraded bus voltage settings | | may not protect all safeguards loads from the effects of an undervoltage | | condition under all accident conditions. A recent calculation has verified | | that under certain plant conditions, the current degraded bus undervoltage | | settings are below that required to insure proper operation of equipment | | powered by our 600-volt safeguards buses. Safeguards loads on our 600-volt | | buses consists primarily of valves and ventilation equipment." | | | | "Currently, both units are in a defueled condition. In the current mode, | | the degraded bus voltage function is not required. Also, since the | | safeguards buses are lightly loaded during shutdown conditions, the impact | | due to low grid voltage is low. An operability determination has been | | performed to demonstrate that the condition does not affect the operability | | of the safeguards buses while the plant is in a shutdown condition." | | | | "Actions are in progress to correct the low degraded bus voltage settings as | | well as the limit specified in technical specifications." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36055 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 08/21/1999| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 16:27[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 08/20/1999| +------------------------------------------------+EVENT TIME: 23:58[EDT]| | NRC NOTIFIED BY: DEVON PRICE |LAST UPDATE DATE: 08/21/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETER ESELGROTH R1 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |70 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR REPORT REQUIRED BY STATION OPERATING LICENSE | | | | On August 20, at 2358, a lightning strike caused a momentary loss of a 500kv | | transmission line. The resulting electrical transient caused the trip of the | | following equipment: "A" Reactor Feedpump, "A" Electrohydraulic Control | | Pump, "A" and "B" Reactor Water Cleanup Pumps, "A" Technical Support Center | | Chiller, "A" Control Room Chiller, "A" and "B" Main Reactor FeedpumpTurbine | | Lube Oil Pumps, and the Drywell Coolers. The following equipment | | automatically started: "B" Technical Support Center Chiller, "B" Control | | Room Chiller, "B" Safety Auxiliaries Cooling System Pump and the "B" | | Electrohydraulic Control Pump. The trip of the "A" Reactor Feed Pump and | | the resulting lowering Reactor water level caused an automatic Reactor | | Recirculation system runback to approximately 70% Reactor power. | | | | This equipment was restored to normal operating configuration, and Reactor | | power was restored to 100% at 0449 on August 21,1999. At 0618, Station | | Operators recognized that the #6 Feedwater Heater extraction Steam isolation | | valves had automatically closed during the electrical transient. At that | | time, final feedwater temperature was approximately 365 degrees Fahrenheit. | | At 0646, a power reduction to 90% Reactor power was commenced and at 0826 | | the #6 feedwater heaters were returned to service. | | | | Hope Creek Operating License Condition 2.C(11) states that the facility | | shall not be operated with a feedwater heating capacity that would result in | | a rated power feedwater temperature of less than 400 degrees Fahrenheit | | unless analyses approving such operation are submitted by the licensee and | | approved by the staff. Contrary to this license condition, the plant was | | operated at rated power with feedwater temperature less than 400 degrees | | Fahrenheit. | | | | The plant is currently operating at 100% Reactor power, with feedwater | | temperature greater than 400 degrees Fahrenheit. The Hope Creek Staff is | | currently reviewing Plant response to the electrical transient. All required | | Safety systems are currently Operable and there are no active Limiting | | Conditions for Operation in effect. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36056 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 08/22/1999| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 02:32[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 08/21/1999| +------------------------------------------------+EVENT TIME: 22:55[CDT]| | NRC NOTIFIED BY: BENNETT |LAST UPDATE DATE: 08/22/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 78 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD A REACTOR SCRAM AT 78% POWER ON A LOW REACTOR WATER LEVEL | | SIGNAL. | | | | AN AUTOMATIC REACTOR SCRAM OCCURRED ON A LOW REACTOR WATER LEVEL(LEVEL 3, | | 12.5") AND WAS THE RESULT OF A FEEDWATER TRANSIENT WHICH OCCURRED DURING A | | PLANNED LOAD REDUCTION(REDUCTION IN REACTOR POWER). DURING THE PLANNED | | POWER REDUCTION, OSCILLATIONS WERE NOTED ON THE REACTOR FEEDWATER PUMPS, SO | | THE REACTOR OPERATOR TOOK MANUAL CONTROL OF REACTOR WATER LEVEL IN AN | | ATTEMPT TO STABILIZE THE VESSEL LEVEL. MANUAL CONTROL OF THE REACTOR LEVEL | | FAILED TO CONTROL LEVEL AND THE LEVEL REACHED THE AUTOMATIC SCRAM SETPOINT | | OF LEVEL 3 AND THE AUTOMATIC SCRAM OCCURRED. THE REMAINDER OF THE PLANT | | RESPONDED AS EXPECTED AND LEVEL WAS RESTORED TO NORMAL BAND. ALL RODS FULLY | | INSERTED AND NO ECCS INJECTION OCCURRED OR SAFETY RELIEF VALVES LIFTED. THE | | CAUSE OF THE EVENT IS BEING INVESTIGATED. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36057 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/22/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 09:30[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/21/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 19:55[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/22/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRENT CLAYTON R3 | | DOCKET: 0707001 |JOE HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WALKER | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE CRITICALITY ACCIDENT ALARM SYSTEM (CAAS) HORN DID NOT PASS TESTING | | CRITERIA. | | | | At 1824 on 8/21/99, the Plant Shift Superintendent was notified that there | | may be a problem with a specific model of CAAS horn. During testing of the | | new CAAS system in C-746-Q. the 30 watt AC/DC CAAS horn did not pass the | | testing criteria for horn actuation time. (Currently the new CAAS horns in | | C-748-Q building are not inservice and the building is serviced by the old | | System which does lot use these 30 watt AC/DC horns and remains operable) | | ANSI/ANS 8.3 identities that the CAAS System shall automatically initiate an | | evacuation alarm signal within one half second of the alarm setpoint being | | exceeded. Preliminary testing Indicated that the 30 watt AC/DC CAAS horn | | will not actuate in the required time frame (it takes 0.6 - 0.9 seconds). | | The C-710 facility uses the 30 watt AC/DC CAAS horn in its current inservice | | configuration. During the initial investigation of this event, it was | | identified that when this type CAAS horn was installed in C-710, it was not | | tested for response time, however the 15 watt AC horns which are also | | installed in C-710 were tested within an acceptable time frame. At that | | time, engineering did not suspect a deviation in horn activation response | | time between the two different horn types. Since reasonable assurance of | | operability is not maintained for the 30 watt AC/DC CAAS horn, the C-710 | | building was declared inoperable at 1955 on 8/21/99. | | | | This event is reportable as "equipment is disabled and equipment Is required | | by a TSR to be available and operable and no redundant equipment is | | available and operable". | | | | Corrective actions have not yet been determined. | | | | The NRC resident inspector has been notified of this event. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021