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Event Notification Report for July 27, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           07/26/1999 - 07/27/1999

                              ** EVENT NUMBERS **

35959  35960  35961  

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   35959       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  US ARMY (ACALA)                      |NOTIFICATION DATE: 07/26/1999|
|LICENSEE:  US ARMY (ACALA)                      |NOTIFICATION TIME: 15:58[EDT]|
|    CITY:  ROCK ISLAND              REGION:  3  |EVENT DATE:        08/15/1998|
|  COUNTY:                            STATE:  IL |EVENT TIME:             [CDT]|
|LICENSE#:  12-00722-06           AGREEMENT:  Y  |LAST UPDATE DATE:  07/26/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JOHN KINNEMAN        R1      |
|                                                |GEOFFREY WRIGHT      R3      |
+------------------------------------------------+SCOTT MOORE          NMSS    |
| NRC NOTIFIED BY:  JEFF HAVENNER                |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|BAB1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| CHEMICAL AGENT DETECTOR DISCOVERED MISSING DURING AN INVENTORY CHECK.        |
|                                                                              |
| A M43A1 CHEMICAL AGENT DETECTOR CONTAINING 250 MICROCURIES OF AMERICIUM-241  |
| WAS DISCOVERED MISSING DURING AN INVENTORY CHECK PERFORMED ON 07/24/99 BY    |
| THE 458th ENGINEER BATTALION (RESERVE).   IT IS BELIEVED THAT THE MISSING    |
| CHEMICAL AGENT DETECTOR WAS LOST IN AUGUST, 1998, WHILE THE BATTALION WAS    |
| PERFORMING RESERVE TRAINING AT FORT DRUM MILITARY RESERVATION, NEAR          |
| WATERTOWN, NY.  A SEARCH FOR THE MISSING CHEMICAL AGENT DETECTOR WILL        |
| PERFORMED.                                                                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35960       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 07/26/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 19:24[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        07/26/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        15:44[EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  07/26/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |GEOFFREY WRIGHT      R3      |
|  DOCKET:  0707002                              |LARRY CAMPER         NMSS    |
+------------------------------------------------+JOSEPH GIITTER       IRO     |
| NRC NOTIFIED BY:  RON CRABTREE                 |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SIZE OF PLASTIC BAGS PLACED OVER SMALL DIAMETER CONTAINERS DOES NOT MEET     |
| NCSA REQUIREMENT.                                                            |
|                                                                              |
| NRC BULLETIN 91-01, 4 HOUR REPORT.                                           |
|                                                                              |
| AT 1544 ON 07/26/99, THE PLANT SHIFT SUPERINTENDENT WAS NOTIFIED OF A        |
| NONCOMPLIANCE WITH NUCLEAR CRITICALITY SAFETY APPROVAL (NCSA) PLANT 001.A02, |
| REQUIREMENT #1, WHICH STATES: "THE MAXIMUM SIZE BAG PLACED OVER A SMALL      |
| DIAMETER CONTAINER SHALL BE A MAXIMUM OF 12 INCHES WIDE WHEN LAID FLAT BY A  |
| MAXIMUM OF 36 INCHES TALL".  NUCLEAR CRITICALITY SAFETY PERSONNEL DISCOVERED |
| THAT A BAG ISSUED FROM PORTSMOUTH STORES STOCK (ITEM #16-999-0314) HAS A     |
| WIDTH OF 12-3/16 INCHES AND AN OVERALL HEIGHT OF 36-3/8 INCHES, THUS         |
| VIOLATING ONE OF THE TWO CONTROLS REQUIRED BY THE NCSA.  PLANT PERSONNEL ARE |
| CURRENTLY PERFORMING WALKDOWNS OF ALL AFFECTED SMALL CONTAINER STORAGE AREAS |
| TO ASSURE COMPLIANCE WITH THIS NCSA REQUIREMENT.  THIS EVENT IS REPORTABLE   |
| TO THE NRC AS AN NRC BULLETIN 91-01, 4 HOUR REPORT DUE TO A VIOLATION OF THE |
| DOUBLE CONTINGENCY PRINCIPLE WHERE DOUBLE CONTINGENCY CANNOT BE              |
| REESTABLISHED IN 4 HOURS, AFTER THE INITIAL OBSERVATION OF THE EVENT.        |
|                                                                              |
| SAFETY SIGNIFICANCE OF THE EVENT:                                            |
|                                                                              |
| THE NCSA APPROVES THE USE OF A BAG THAT MEASURES 12 INCHES WHEN LAID FLAT.   |
| THESE BAGS ARE TO BE USED ONLY TO LIMIT THE SPREAD OF SURFACE CONTAMINATION  |
| AND TO SEAL CONTAINERS FOR SECURITY REASONS.  THEY ARE NOT TO BE USED TO     |
| CONTAIN MATERIAL IN THE CONTAINERS.  THEREFORE, AS LONG AS THE CONTAINER HAS |
| NOT CATASTROPHICALLY FAILED, THE SAFETY SIGNIFICANCE IS LOW AND A            |
| CRITICALITY IS NOT POSSIBLE.                                                 |
|                                                                              |
| CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED:   |
|                                                                              |
| PLANT PERSONNEL ARE CURRENTLY WALKING DOWN ALL SMALL DIAMETER CONTAINER      |
| STORAGE AREAS TO RESTORE NCSA COMPLIANCE.  A "STOP WORK NOTICE" HAS BEEN     |
| ISSUED BY THE NUCLEAR SAFETY MANAGER TO ASSURE THE OUT-OF-SPECIFICATION BAGS |
| ARE NOT USED.                                                                |
|                                                                              |
| THE NRC RESIDENT INSPECTOR HAS BEEN NOTIFIED BY THE CERTIFICATE HOLDER.      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35961       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: WATERFORD                REGION:  4  |NOTIFICATION DATE: 07/27/1999|
|    UNIT:  [3] [] []                 STATE:  LA |NOTIFICATION TIME: 00:45[EDT]|
|   RXTYPE: [3] CE                               |EVENT DATE:        07/26/1999|
+------------------------------------------------+EVENT TIME:        21:52[CDT]|
| NRC NOTIFIED BY:  BILL CROWLEY                 |LAST UPDATE DATE:  07/27/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |BILL JONES           R4      |
|10 CFR SECTION:                                 |                             |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP           |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LICENSEE DETERMINED THAT UNDER CERTAIN METEOROLOGICAL CONDITIONS, THE        |
| ULTIMATE HEAT SINK (DRY COOLING TOWERS) MAY NOT BE WITHIN THE LICENSING      |
| BASIS OF THE FACILITY.                                                       |
|                                                                              |
| "WATERFORD 3 IS NOT ABLE TO MEET LICENSING BASIS FOR ANALYZED RAINFALL       |
| EVENTS.  SPECIFICALLY, A SITE PROJECT STORM WITHOUT ANY DRY COOLING TOWER    |
| SUMP PUMPS AVAILABLE AND A PROJECT MAXIMUM PRECIPITATION WITH ONLY ONE DRY   |
| COOLING TOWER SUMP PUMP AVAILABLE.  SINCE IT IS POSSIBLE THAT WATERFORD MAY  |
| HAVE OPERATED IN A CONDITION WITH ONE DRY COOLING TOWER INOPERABLE AND THE   |
| OTHER DRY COOLING TOWER HAVING ONLY ONE SUMP PUMP AVAILABLE, A PROJECT       |
| MAXIMUM PRECIPITATION COULD HAVE INCAPACITATED THE OPERABLE DRY COOLING      |
| TOWER.  BASED ON THE CURRENT DRY COOLING TOWER SUMP PUMP CONFIGURATION AND   |
| PREDICTED RAINFALL, BOTH DRY COOLING TOWERS REMAIN OPERABLE.  THE PLAN IS TO |
| INSTALL A HIGH CAPACITY PORTABLE DIESEL SUMP PUMP IN EACH DRY COOLING AREA   |
| WITHIN 24 HOURS."                                                            |
|                                                                              |
| THE ABOVE CONDITION WAS DISCOVERED BY THE LICENSEE DURING A REVIEW OF A      |
| DESIGN MODIFICATION.                                                         |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+


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